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2013 Feedwater OPEX Round-Up
Eric BackusFW System Engineer
Exelon - LaSalle StationFSRUG Executive Board Member
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Summary of 2013 OPEX Issues137 OPEX entries
Feedwater, Heater Drains, Condensate, MSR
FW HD FWLC UFM CD MSR TotalI&C 5 9 8 1 5 4 32Control Valve 9 8 3 1 21Human Performance 8 4 1 2 2 2 19Ageing 2 2 1 4 2 11Electrical 6 3 9Design 6 2 8Pump 5 1 1 7UFM 7 7Oil System 5 5Other 8 8 1 1Total 53 32 12 11 18 10 137
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Feedwater Scrams12 Feedwater Scrams occurred during 20131. Failed fuse on an inverter on a non-safety vital
bus. This caused a loss of 120VAC instrumentation power and caused all Feed Pumps driving to minimum output. This was a known SPV in DFW.
2. Failure of air line on FRV actuator caused FRV to go closed. Caused by unanticipated harmonic vibrations after steam generator replacement.
3. Loss of condenser vacuum due to FW Long Cycle Return Valve due to vibration from seat leakage. The valve was not of a sufficient design.
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Feedwater Scrams (cont.)4. Loss of condenser vacuum from a leak on a
heater level control line. The leak occurred from vibrations due to failed tubes and leaking drain valves.
5. Loss of one Feedwater pump due to coupling failure. The coupling failed along a pump end weld seam, with damage found on a turbine end weld seam.
6. An instrument air line failed at a soldered coupling causing loss of air to FRV. Air line failed after excavation, was due to poor original quality.
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Feedwater Scrams (cont.)7. A secondary system transient occurred causing
both HD pumps to trip, causing a FW pump trip on low NPSH, causing a scram on low level. There was inadequate procedure guidance on the automatic control of heater bypass control valve.
8. Short in flex conduit caused false indication of low FW pump seal cooling on both FW pumps. Both FW pumps tripped due to the lost indication.
9. Loss of bus caused instrument loop on all 3 FW pump recirculation valves to fail all recirc valves open. This known SPV was introduced in a mod.
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Feedwater Scrams (cont.)10.A coding error in FWLC logic caused high
water level and trip when transitioning FWLC modes during a planned shutdown.
11.Online maintenance of FW turbine caused loss of condenser vacuum when turbine casing was lifted because of excessive leakage past exhaust valve.
12.Feedwater level oscillations occurred due to air leakage past degraded o-rings in the FRV actuator. Operators manually scrammed due to being unable to stop oscillations in manual control.
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Questions?
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Full OPEX Summary Table CD FW FWLC HD MSR UFM TotalI&C 5 5 8 9 4 1 32Control Valve 3 9 8 1 21Human Performance 2 8 1 4 2 2 19Ageing 4 2 1 2 2 11Electrical 3 6 9Design 6 2 8Pump 1 5 1 7UFM 7 7Oil System 5 5Unknown 2 1 1 1 5Process/Procedure 3 3FW SCS 2 2Heater 2 2Check Valve 1 1Engineer (Good) 1 1HD System 1 1N/A 1 1Strainer 1 1Vendor Issue 1 1Total 18 53 12 32 10 11 137