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INTERIM REPORT ON ROOT CAUSE ANALYSIS ON VALVE STRUCK DURING OPERATION OBSERVED AT ARKAD
ENGINEERING & CONSTRUCTION COMPANY, FADHILI DOWNSTREAM PIPELINES PROJECT
Team Members:
Hari K S - Sr. DGM - Quality Control
Suresh J - Sr. DGM- Production
Gopalakrishnan S – DGM - Quality Control
Ganesh kumar – AGM, Manufacturing
Ramajeyam K – Manager- Quality Control
Sivasankaran C – Manager – FG Stores
RCA REF: 120002563 REV.0 (DT. 27TH NOV 2018)
2
CONTENTS
1.0 Background
2.0 Preliminary Analysis & Interim Containment Action
2.1 Verifications at L&T Valves Factory
2.2 Correction
3.0 Root Cause Analysis for Valve Struck
3.1 Problem Description –Valve struck
3.2 Cause and Effect Diagram Valve struck
3.3 Significant Causes Valve struck
3.4 Why Why analysis for Valve struck
4.0 Product & process verification at LTVL
5.0 Further Investigation
6.0 Conclusion
7.0 corrective action at Site
3
1.0 Background:
M/s Arkad Engineering & construction company reported that valve is damaged during operating by operational people inside WGP & valve is no more functional on L&T Valves supplied Globe valve for Fadhili downstream Pipelines project. Mail References: E- MAIL from M/s Arkad Engineering and construction company IMRAN HAQ
Dated: 7th Oct 2018.
Valve Details:
2.0 Preliminary Analysis & Interim Containment Action:
2.1 Verifications at L&T Valves Factory:
2.1.1 The following documents were verified and found in order:
Inspection Test Plan
General Assembly Drawing
Internal Valve Test Report
Internal coating inspection report – Witness by Aramco Inspector
SCN – Final inspection report
Valve Hydro offer list duly signed by Aramco Inspector
Painting & Packing Report
Pre Dispatch Inspection Report
Pre Dispatch Inspection Photographs
Valve Description GLOBE-6"-CL300-FF-WCB-254SMO+HS-GU
Material Construction ASTM A216 Gr. WCB with internal Belzona
Valve Type Globe valve
Valve Serial No 18C200168
Order Qty. 36 Nos.
Delivered Qty. 36 Nos.
NCR Qty. 01 No.
Leakage Details Valve not functional
4
In addition to the above we have verified all other relevant internal quality documents
from receipt to final related to these valves and found meeting specifications and
Approved Inspection Test Plan requirements.
2.1.2 The above valves were internally tested at L&T Valves as per approved ITP and
Aramco Specification 04-SAMSS-048 and found accepted.
Valves are pressure tested as per the sequence mentioned in the 04-SAMSS-048.
Shell test – 1125 Psig for 5 Minutes & 15 Minutes
Seat test –Hydro – 815 psig for 1 Minutes
No leakage was reported in any of these tests at LTVL shop.
Observation on the valve :-
LTVL Service Engineer requested Arkad Engineering to move the valves to
AVIMCO Mod shop and he visited on 29th Oct 2018 and he done a detailed
study along with Avimco personnel and sent initial inspection report with
observation on 29th oct 2018.
Leaked valves moved to AVIMCO service shop & observed as below.
The following are the observations while dismantling at Mod shop under the
supervision of L&T valves service engineer on 29th Oct 2018.
a. Guide rib which was Ni coated was found to be cut either using
cutter or gouged.
b. We are able to see Ni coating above the cut lengthy and below cut
smaller.
c. Heavy burr observed on the cut portion
d. These are 100% witnessed by TPIs at various stages starting from
RMO, FBE witness , hydro till packing. (LSTK – Techmas & Aramco – Intertek)
8
2.2 Correction:
Considering the damaged condition of the valve, it is recommended to replace
with the fresh valve.
9
3.0 Root Cause Analysis for Valve Struck during operation:
3.1 Problem description for Valve Struck during operation:
RCA - ROOT CAUSE ANALYSIS SHEET
DESCRIPTION OF THE PROBLEM DESCRIPTION DATA
WHAT What is the Discrepancy? Valve got struck during operation.
WHERE
Where specifically on the
Discrepancy?
Where geographically is the
Discrepancy observed?
Valve operation(Open/Close)
At Customer site (for Fadhili downstream Pipelines
project site)
WHEN
First seen - By the customer? Yes
When seen since? Oct 2018
When is the Discrepancy seen? Valve struck and not operational
HOW
BIG
How many Valves have the
Discrepancy? 01 No.
10
3.2 Cause and Effect Diagram –Valve struck during operation.
3.2.2 CAUSE AND EFFECT DIAGRAM
METHODS MATERIALS
MAN MACHINE
PROBLEM
STATEMENT
CAUSE AND EFFECT DIAGRAM - DEFINE & VERIFY ROOT CAUSE
Valve
struck and
not
operational
during
open/Close
Inadequate Knowledge of Tester
Internal rusting
Lack of contact on seating
surface (Blue match)
High hardness in Stem
material.
Contamination in DM
Water
In correct disc machining
& machine accuracy.
Body /disc - Poor
Machining & lapping
process
Damage in seat sealing
interface
Excess torque during
operation
Improper movement of valves
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3.3 Significant Causes –Seat Leak
S No CAUSES SIGNIFICANT / IN-
SIGNIFICANT
1 Inadequate Knowledge of Tester & Assembler
INSIGNIFICANT
2 In correct disc machining & machine accuracy INSIGNIFICANT
3 Lack of contact on seating surface (Blue match) INSIGNIFICANT
4 Excess Torque during operation
INSIGNIFICANT
5 Internal rusting INSIGNIFICANT
6 Body /Disc - Poor Machining & lapping INSIGNIFICANT
7 High hardness in Stem material.
INSIGNIFICANT
8 Contamination in DM water INSIGNIFICANT
9 Damage in seat sealing interface
INSIGNIFICANT
10 Improper movement of valve SIGNIFICANT
3.4 Why-Why Analysis
Significant Cause (Valve struck during operation)
Why? Improper movement of valves
Why? Improper handling at site lead to Stem bend,stem broken, Seat
damages, Internal coating peel off.
12
Root Cause:
During valve operation during installation, even though the valve accepted during site testing there is a functional issue during open/close which could had happened due to mishandling of valve which results in stem bend & stem broken and Valve
disc seat damage and guide rib damage & coating peel off.
6.0 Conclusion:
Based on the observations, we find the wrong handling method of valve at site lead
to Stem bend and Broken and also damages to the disc seating face and guide rib
damage. Also there is internal coating damage.
7.0 Corrective actions at site
Awareness to be given to site team for proper handing and proper preservation of the valves.
= = End of Report = =