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Apr. 16, 2007 Undulator Breakout 1 Dean R. Walters [email protected] Undulator Vacuum System Vacuum System Dean R. Walters Soon-Hong Lee, James Bailey, James Morgan, Dana Capatina, Scott Doran, ANL

Apr. 16, 2007 Undulator Breakout Dean R. Walters [email protected] 1 Vacuum System Undulator Vacuum System Dean R. Walters Soon-Hong Lee, James Bailey, James

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Apr. 16, 2007Undulator Breakout

1 Dean R. Walters

[email protected]

Undulator Vacuum System Vacuum System

Dean R. Walters

Soon-Hong Lee, James Bailey, James Morgan, Dana Capatina, Scott Doran, ANL

Apr. 16, 2007Undulator Breakout

2 Dean R. Walters

[email protected]

Beam Finder Wire

Undulator Vacuum ChamberPrototypes

Production

Vacuum SystemString Test Results

Undulator Vacuum System Vacuum System

Apr. 16, 2007Undulator Breakout

3 Dean R. Walters

[email protected]

BFW Production Plan

Chamber

Weldment Catalog Items

Machined PartsHardware

Fixtures

Assemble, Weldment/Chamber/CardLeak check and bake out

Wire Card

Procured Components

Work performed at ANL

Install Machined Parts/Catalog Items/Hardware on the Assembly

Perform Nominal Alignment Procedureand Operational Tests

Package and ship to SLAC

Apr. 16, 2007Undulator Breakout

4 Dean R. Walters

[email protected]

BFW Status of Production

Weldment, Machined Parts, Chamber, Catalog Items and all Hardware---- Design and Procurement Documents are complete and are in the procurement process

Wire Card is currently under final design.

Fixture designs are 90% complete.

Alignment and Assembly Procedures are 50% complete.

Apr. 16, 2007Undulator Breakout

5 Dean R. Walters

[email protected]

BFW Production ScheduleWhat is the current Schedule

Apr. 16, 2007Undulator Breakout

6 Dean R. Walters

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Prototype Vacuum ChambersCompound screws (Brass Screws & SST )

Vacuum Chamber

NW 50 Flange -Clamp Type (316L SST)

Top & Bottom Strips (316LN)

Chamber Strong-back (20Cb-3)

End Cap (20Cb-3)

Prototype A

Top & Bottom Strips (20Cb-3)

Chamber Strong-back (316 SST)

End Cap (20Cb-3)

Prototype B

Apr. 16, 2007Undulator Breakout

7 Dean R. Walters

[email protected]

Status of Prototype Efforts42 inch Prototype

Completed fabricationConstructed Laser Welding tooling for 42” prototype Leaks repaired with Ag brazeFirst coatingChamber cut up for visual examination

Proto B (12 ft proto)Completed all Fabrication’s stepsConstructed Laser Welding tooling for 12 ft prototypesRepaired leaks with Ag brazing and Sn-Ag-Cu solderingCompleted both Bakes & was coatedUnit completed vacuum performance measurementInstalled into SUT for straightness measurementChamber used in String Test

Proto A (12 ft proto)Completed all fabrications steps Repaired leaks by Laser WeldingCompleted both Bakes and was coatedUnit completed vacuum performance measurementChamber used in String TestChamber has been machined into parts for further examination

Coating fixture in place and in use.Pivoting fixture installedAll safety inspections completeEnd stations complete

Apr. 16, 2007Undulator Breakout

8 Dean R. Walters

[email protected]

Production Chamber Permeability (full length Prototype A)

As-received Alloy 20

1.009 ~ 1.010 (0.75” thick)

After fabrication, permeability 1.013

[spec: 1.02]

Apr. 16, 2007Undulator Breakout

9 Dean R. Walters

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Laser Seam Welding - 12 Foot Prototype

Fixturing for Strong Back Weld

Transferring Fixturing from Strong Back Weld Configuration to End Cap Weld

Fixturing for End Cap Weld

Apr. 16, 2007Undulator Breakout

10 Dean R. Walters

[email protected]

Prototype A Laser Welding

Drawing shows the location of the leaksThe majority of the leaks occur at the weld overlaps

The chamber was welded in three sectionsThe chamber was sent back to the vendor of weld repair

The chamber was baked after leak repair and none have re-opened

Apr. 16, 2007Undulator Breakout

11 Dean R. Walters

[email protected]

Final Machining Method

End CapStrong Back

Side Wall

Vacuum Chamber Xsection

1” wide cut by 2-0.030” and 4-0.010” deep

0.020” final wall thickness

1” wide cut by 1-0.100”

deep

Apr. 16, 2007Undulator Breakout

12 Dean R. Walters

[email protected]

12 foot Coating Set-up

Apr. 16, 2007Undulator Breakout

13 Dean R. Walters

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12 Foot Test – 2/2/2007

Sample

Location Sample

Location

Apr. 16, 2007Undulator Breakout

14 Dean R. Walters

[email protected]

Coating Results

Test were performed by inserting silicon samples into 13 mm ID SST spool. Each test had four samples down the length. In most cases the samples were measured in more than one locationUniformity down the length

In three different tests over the 12 foot lengthTest #1: Average thickness of 98 nm with uniformity of 10%Test #2: Average thickness of 325 nm with uniformity of 4.3%Test #3: Average thickness of 210 nm with uniformity of 12%

Results of surface finishTest #1 surface increased roughness by 1 nmTest #2 surface roughness was unchanged by the coatingTest #3 surface increased roughness by 2 nm

Plans for further measurements

Apr. 16, 2007Undulator Breakout

15 Dean R. Walters

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Coating of Proto A Coating of Proto B

Performed on 9 Feb. 2007

Repeated on 13 Feb. 2007

Performed on 16 Feb. 2007

Apr. 16, 2007Undulator Breakout

16 Dean R. Walters

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Baking the Prototypes

Baking of Prototypes A and B

Prototype A

Prototype B

Proto B 1st bake (before coating) at 200 deg C2nd bake (after coating) at 150 deg C

Proto A1st bake (before coating) at 150 deg C2nd bake (after coating) at 150 deg C

Proto B

Base Pressure : 5.9x10-9 / 1.1x10-9

Outgassing Rate : avg. of 6x10-13 Torr-Lit/sec/cm2

Proto A

Base Pressure : 2.2x10-9 / 2.5x10-9

Outgassing Rate : avg. of 3x10-13 Torr-Lit/sec/cm2

Measurements of Vacuum Performance

(Outgassing Rate Spec: 2x10-12 Torr-Lit/sec/cm2)

Apr. 16, 2007Undulator Breakout

17 Dean R. Walters

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Vertical Adjustment Screws (14)

Chamber Alignment/Survey ResultsSUT Mockup Chamber Prototype B Chamber

Results showed the vertical centerline of vacuum chamber can be within tolerance of ± 200 µm

Apr. 16, 2007Undulator Breakout

18 Dean R. Walters

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X-Adjustor

Z-Adjustor Support Assembly

Production Vacuum Chamber Ass’y

Vacuum Chamber Assembly

Apr. 16, 2007Undulator Breakout

19 Dean R. Walters

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Fabrication Processes

Apr. 16, 2007Undulator Breakout

20 Dean R. Walters

[email protected]

Preparations for ProductionAdvanced Procurement Plan written and in the process of being signed.Support Assembly

SOW completedPurchase requisition in system

Chamber MaterialAlloy 20 for first 4 units in houseAlloy 20 for next 8 units have a requisiton placed in the ANL purchasingPurchase requisition for next 25 in system

Side Wall Vendor making first articleDraft SOW is complete

StrongbackSOW is complete and being signedRequisition is in the ANL system

End CapSOW is complete and being signedRequisition is in the ANL system

All drawings for the chamber and the support have been completed and released.Minor updates have been incorporated.

(4) Full sheets of polished 316LN have been bought, samples have had the surface finish measured and accepted for use.

Strips have been made from this material and used in Prototype A. The (2) sheets are sufficient for the entire production run.A test run is under way to water jet cut strips and to machine the edges, if this is satisfactory then this vendor will produce the rest of the parts.

Material for the first (4) strongbacks have been bought and are ready to be shipped to machining vendors.Samples of material have already been submitted for permeability measurement and have been accepted.

Material for the first (8) end caps have been bought and are ready to be shipped to machining vendor.Tooling has been made, and used, for: machining the strongback, laser welding, and final machining.

Apr. 16, 2007Undulator Breakout

21 Dean R. Walters

[email protected]

Chamber Schedule

Apr. 16, 2007Undulator Breakout

22 Dean R. Walters

[email protected]

String Test Results

Apr. 16, 2007Undulator Breakout

23 Dean R. Walters

[email protected]

Concerns & Open IssuesHave developed Laser Welding and built tooling with vendor in Iowa.Need qualified strongback machining vendors

Will need 2 for productionNeed to locate qualified Final Machining vendor

All Final Machining of prototypes were performed by ANL Central Shops.Continue coating development now that contact is reestablished with thin film consultant.Cost of Nickel is raising, pricing of Alloy 20 is subject to increase.

Attempt of offset that by placing order now for future deliveryPermeability of Alloy 20 is of concern, since the material used in Proto A is measurably lower in relative permeability than first antisapated further measurements will be performed. Proto A has been cut up and a section will be used for measuring permeability in an ANL undulator.Since performing a vacuum pumpdown string test, Proto A has been cut apart to inspect the internal surfaces.

Apr. 16, 2007Undulator Breakout

24 Dean R. Walters

[email protected]

ConclusionsTwo full sized prototypes have been built.All planned fabrication steps have been performed.Seam Welds were performed by Laser Welding.

Even though leaks were found, they have been repaired.The vendor is organizing further work to address them.

Construction of the 12 foot fixture and initial development of the AC Diode Sputtering process has lead to Aluminum coatings applied to both prototypes.The chambers have been baked and their measured outgassing rate is lower than the specification Many preparations for production are in-process or in place.