Transcript
Page 1: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

I _ -

f

ERNMENT OF URlTlSH COLUMBIA 4 :- _ _ ----=y

........ ................................. TO l .

: - . . ~ . P ~ ~ ~ ~ . ~ . . ~ ~ . ~ k s . . . ~ ~ ~ ~ i ~ i o n .......................... MInis.L?::* of Highways & PEbiic Works BrnLE.XN.GS.. ................................................................

J'

1

J. C. Foweraker , Head

Hydrology Division FROM Groundwater Section

........... Ma.ter..In~es.t igatia ns.. Branch ......

..................... March..24 ................................. 19.27 ....

YOUR FILe .................................

Further t o your memorandum of December 2 , 1976 and the services being pro- vided by our Groundwater Section i n a s s i s t i n g you t o retest and t o b r ing the above w e l l s i n t o production, please f ind at tached a memorandum prepared by M r . A.P. Kohut, Senior Hydraulic Engineer with the Groundwater Section, e n t i t l e d "Abbotsford Trout Hatchery Production Well Retests, Well #8 (Hatchery W e l l #l)".

I would emphasize M r . Kohut's conclusions t h a t the performance of Well #8 appears t o have declined by a f a c t o r ranging from 11 t o 22%. The cause of this decl ine may be due t o i r o n encrus ta t ions of the w e l l screen and/or of t he n a t u r a l aqui fe r pack around the w e l l screen. W e recommend a review of the chemical qua l i t y of the groundwater a t the s i t e and an ana lys i s of the cncrus ta t ion material found on the pump column, i n order t o determine the co r rec t maintenance and cleaning procedure, i f required, t o be undertaken i n a l l production w e l l s a t the s i te . Our Groundwater s t a f f should be consulted as t o timing p r i o r t o the implementation of any cleaning program.

There i s a l s o s t i l l some question on the accuracy of t he flow meters used on the tests and t h i s f ac to r may a l s o have t o be considered i n assessing the drop off i n w e l l performance, mechanical fl-m meters on a l l w e l l s .

W e s t i l l recommend i n s t a l l a t i o n of in- i ine

We a l so s t rongly recommend t h a t a l a rge capacity (2,000 USgpm) standby w e l l be completed a t the Hatchery s i t e as soon as possible . t i o n i n the above-mentioned w e l l is implemented, i t may temporarily a f f e c t groundwater qua l i t y i n the v i c i n i t y of the production w e l l s and i t would be advisable t o loca t e the standby w e l l a s u f f i c i e n t d i s tance away t o avoid any p o t e n t i a l contamination during t h e cleaning operations.

I f the cleaning opera-

I JCF/ j s

Encl,

J.C. Foweraker, Head Groundwater Section Hy d r 010 gy Division Water Invest igat ions Branch Ministry of the Environment

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*GOVERNMENT OF BRITISH COLUMBIA 1) MEMORANDUM

)I TO.. ......... D.r ...... J., .... C ..... P . ~ w . ~ x . a ~ ~ ~ . , . . ~ ~ . a ~ ......

....... Gr.0 ...... ..............................

FROM A. P. Kohut Senior Geological Engineer

.......... Hydrology..l3iuision ..............................

H ~ d r . o l . o ~ . . . D ~ ~ ~ ~ ~ ~ ~ .......................................... 1) ..... M a ~ c h . 2 2 . ~ ......................................... 19.7.7. ....

SUBJECT. .Abbots~fo.ra~.T.~a.u.t...Ha~~he~~..Er.aduet ion We1 1 Retests , OUR FILE ...02390.1.6 ...............

YOUR FILE ................................. Well 8 (Hatchery Well No. 1)

On February 2 1 and 22, 1977, Mr. Chwojka and myself attended the s t a r t u p and running of the retest on Well 8 (Hatchery No. 1 ) . The first day was spent t r a v e l l i n g t o t h e s i t e , reviewing procedures f o r the r e t e s t with Mr. Les Gilber t and checking water leve ls and operation of t h e other wells.

,The 32-day automatic recorder with 2 : l recording chart was removed from Observation Well 3 located 250 f e e t north of Well 8 and replaced with a 2-day recorder with 5 : l char t . s t a r t i n g a t 8:45 a.m., f o r f i v e hours u n t i l 2:05 p.m. Flow was measured with a portable flow meter and discharge elbow i n t h e same manner as t h e previous retest carr ied out i n Well 7 i n January, 1977. Due t o uncertain- t i es i n the accuracy of the flow meter, Mr. Les Gibert r e t e s t e d t h e well fur ther on February 24, 1977.

The r e t e s t was car r ied out the second day,

Well ODeration P r i o r t o Retesting of Well 8

Well 7 (Hatchery No.2) was not i n operation, being shut down after February 15, 1977, due t o mechanical f a i l u r e . Well 1 (Hatchery N0.3) was operating a t a constant rate near 600 I g p m following t h e shutdown of Well 7. This well would remain i n operation during the r e t e s t i n g of Well 8. During the retest carr ied out February 24, 1977, Well 8,however, was i n operation a t about 1000 USgpm p r i o r t o being upstepped t o higher pumping rates (pers. comm.L.Gi1bert).

Retest Procedures

With Well 1 (Hatchery No.3) pumping continuously t h e evening and morning p r i o r t o the test , t h e water leve l i n Observation Well 3 was monitored with the automatic recorder and found t o be r i s i n g s l i g h t l y a t a r a t e of 0.08 feet p e r 24-hour period. following the shutdown of Wells 8 and 7 which had been operating earlier i n the month and normal seasonal response of t h e water t a b l e t o f a l l and ear ly winter prec ip i ta t ion . s t a b i l i z e d p r i o r t o s t a r t i n g Well 8, so t h e e f fec t of Well 1 pumping would not be a major problem i n assessing the performance of Well 8.

The r i s i n g conditions may have been due t o recovery

Water level conditions, however, were r e l a t i v e l y

. . . 2

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- 2 -

I

D r . 0 C. Foweraker March 22, 1977

Procedures f o r the s t a r t u p were t o set the flow control valve t o a low s e t t i n g , s ta r t the pump and adjust t h e flow meter and flow valve t o obtain an i n i t i a l ra te of 600 t o 700 USgpm. t h i s r a t e f o r a few hours and then t h e rate would be increased t o 1500 and then 2000 USgpm f o r t h e remainder of the test .

The w e l l would be run a t

Results

Drawdown d a t a obtained during the retest are shown i n Table 1. 135 minutes the drawdown reached 14.6 feet a t a pumping r a t e of 1054 USgpm according t o t h e flow meter, indicat ing a s p e c i f i c capacity of 72.2 USgpm per foot of drawdown. feet, indicat ing a s p e c i f i c capacity of 76.1 USgpm per foot of drawdown and a t the f i n a l r a t e of 1863 USgpm, drawdown reached 23.95 feet (77.8 USgpm per foot of drawdown). These s p e c i f i c capacity values, however, a r e about 17 t o 23 percent lower than those obtained (94 t o 101 USgpm per foot of drawdown) during i n i t i a l t e s t i n g of the well i n 1969 (Hall, 1970).

Recovery measurements (Table 1) were taken i n the pumped well and Observation Wells 3 and 5 after shutdown, over a period of 50 minutes, with the water level returning t o within 0.4 f e e t of the i n i t i a l pre-pumping leve l i n t h e pumped well and 0.5 f e e t i n Observation Well 3. Slow recovery, as i n the case of previous tests, may be due t o trapped a i r within the cone of influence of t h e well under water t a b l e conditions.

After

A t a rate of 1483 USgpm the drawdown reached 19.5

Since it appeared t h a t the overa l l performance of Well 8 had decreased by as much as 23 percent from t h a t observed i n 1969, it was decided t o check the flow meter f o r accuracy. The flow meter was, therefore , cleaned and reca l ibra ted a t t h e manufacturer's. Results of the February 24, 1977, retest are summarized i n t h e following Table 2.

TABLE 2. SUMMARY OF FEBRUARY 24. 1977 RETEST OF E L L 8

Pumping Rate Water ieve l Feet Drawdown From Assumed Spec i f ic Below Bottom Pre-pumping Level C ap aci t y

1443 1521 1666 2100

48.40 49.23 51.67 55.46

18.0 80.17 18.83 80.78 21.27 . 78.33 25.06 83.80

... 3

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e - 3 -

D r . . J . C. Foweraker March 22, 1977

Although somewhat improved, the s p e c i f i c capacity of t h e Well s t i l l appears t o have decreased by a f a c t o r of 11 t o 22 percent from the i n i t i a l t e s t i n g i n 1969.

An a l t e r n a t i v e means of checking the rate of pumping was t o compare the actual drawdowns i n t h e obse'rvation w e l l with t h e theore t ica l drawdowns which would be expected. Results of t h i s comparison a r e shown i n Table 3. An aquifer t ransmissivi ty of 1.8 x l o5 USgpd/ft and storage fac tors of 0.04 and 0.10 (from Hall, 1970) were u t i l i z e d i n the analyses.

TABLE 3. COMPARISON OF ACTUAL VERSUS THEORETICAL DRAWDOWNS FEBRUARY 22, 1977, RETEST WELL 8.

Pumping Rate Duration Actual Drawdown Theoretical Drawdown

(USgpm) (Minutes) Well 3 Well 5 Well 3 Well 5 i n Well 8 of Pumping i n Feet i n Feet

1054 135 1.59 0.48 0.64 0.07

1256 255 2.35 0.77 1.17 0.25

(average r a t e )

This method of analysis , however, did not give any s a t i s f a c t o r y r e s u l t s as t h e actual drawdowns were much grea te r than expected, suggesting pumping rates were several times those measured with t h e flow meter. The difference i s a t t r i b u t e d t o the probable e f f e c t s of delayed gravi ty drainage which takes place under water t a b l e conditions. drawdown r e s u l t s would be obtained, however, only af ter longer duration pumping.

More meaningful

In summary, t h e performance of Well 8 appears t o have declined by a f a c t o r ranging from 11 t o 22 percent, providing there are no e r r o r s i n the flow meter measurement. This means t h a t f u t u r e drawdowns i n the Well a t various pumping r a t e s w i l l be 11 t o 22 percent grea te r than t h a t which occurred during i n i t i a l t e s t i n g of t h e Well i n 1969. Projected drawdowns, therefore , i n the Well may be g r e a t e r than ant ic ipated, thereby af fec t ing t h e safe ty margin i n t h e Well.

I t should be pointed out t h a t t h i s drop i n performance i s r e l a t e d t o the w e l l i t se l f and not necessar i ly t h e aquifer. decl ine i n performance are:

Some possible reasons f o r t h e

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I , r '

Dr ,"; Foweraker

- 4 -

March 22,- 1977

1.

2 .

encrustat ion of t h e well screen and/or aqui fe r around the screen

s i l t i n g of t h e na tura l aqui fe r pack around the screen

3. sanding of t he well screen, thereby reducing the open area of t h e screen.

The la t ter two p o s s i b i l i t i e s a r e remote, however, as t h e well had been i n operation f o r a few-years, and the w e l l was sounded f o r sand p r i o r t o i n s t a l l i n g t h e new pump. aquifer , however, may have occurred while t he well was i n temporary production. were observed on the pump column of t h e former pump t h a t was i n t h e well . Similar mater ia l may have been deposited i n t h e screen openings or within the aquifer , thereby reducing the permeabili ty of t h e na tura l pack around t h e screen. f u r t h e r with t i m e under pumping conditions. Periodic maintenance, including cleaning of t he w e l l , preferably every year o r so , is recommended t o prevent i ron buildup. clean the screen. acid and chlor ine treatment.

P a r t i a l encrustat ion of t he well screen and/or

Iron deposi ts i n r ings upo to & t o thick, f o r example,

If t h i s is t h e problem, then the w e l l performance may de te r io ra t e

If allowed t o continue, it may be impossible t o e f f ec t ive ly Procedures f o r cleaning i ron deposi ts general ly involves 1

In summary, t h e performance of Well 8 appears t o have,declined by a f a c t o r ranging from 11 t o 22 percent. encrustat ion of t h e well screen and/or of t h e na tura l aqui fe r pack around t h e screen. The problem a t t he moment i s not se r ious , but regular year ly maintenance and cleaning of t he well is recommended t o prevent a buildup of i ron deposi ts i n the well. however, a review should be made of t h e chemical qua l i t y of t he groundwater a t t h e s i t e and analysis should be made of t h e material encrusted on the former pump column t h a t was i n the w e l l . Well 8 should be carefu l ly monitored over t h e next year f o r any changes.

Cause of t h i s decl ine may be due t o i ron

Before a cleaning program is i n i t i a t e d ,

Moreover, t h e performance of

Considering t h e possible maintenance of Well 8 i n t h e fu tu re , including rout ine pump and motor maintenance or cleaning of t h e Well, it would be advisable t o complete a l a rge capacity (2000 gpm) standby well a t t h e s i te . This well should be located a s u f f i c i e n t dis tance from Well 8, however, s o . t h a t it would not be a f fec ted during any cleaning operations of Well 8.

Withxegards t o fu tu re operation of the, two observation wells i n t h e v i c i n i t y of t h e production wells, no gear changes t o the automatic recorders

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- 5 - .*. Dr. J. C. Foweraker

0 March 22, 1977

w i l l be required a t t h i s time. t o be added t o each monitoring setup t o allow for ant ic ipated lowering of t h e water t a b l e under f u l l production conditions.

Additional f l o a t l i n e , however, w i l l have

A. P. Kohut Senior Geological Engineer

APK:wf

Reference: H a l l , P. L. (1970) - Notes on Pumping Tests Carried Out on Well 8, Sept.-Oct.1969, Fraser Valley Trout Hatchery, Water Invest igat ions Branch F i l e 0239016.

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I Height of 1

water i n tube on

orifice Pipe

in inches

Time Time ( t ) since

start of pumping i n mins.

I

lepth t o rsater i n

Drawdown i n well

I

Page /#h

3f casing i = 1 in feet 3'+=t

L ,O _ -4 --.- --l.____l-...._ ... ...

__ .. __ . -. . ...... ..

__ . -

. ......... __ . . . . . . . . . . . . . . . . . . . . . . . . .

-___-.

... .- . ._ . - .

......................

3. ......

~- & i .......... 3s

........ ........ 4 0 0 . - __..- I _-

I--- __-.

9

13.95 .... - /1/./2

/VI 0 b

. - - 13-97 __--_

.............

I

i 20

_I__. -. -.

........ ......

..

-.-____I -

-- .....

.... - .......... .- ....

..............

. .. .....

. . . . . . .

. . . I

.. - .....

_ _ ! - 3 . 0 . . w-.. ................

-- !-t.t.S Y... 1 .

. . . . / 3 + v . . I !

/3*88 I /3*40 1

.-I----.--- ..-I --.--_-_I._.._ I

....... _- ......... ,.. ........... - ... - .. i

..................

. . . . . . / 3 * 9 0 ! .................

. . ........ ___ -

..... .__.l._..ll__. .. -. ..... . -_ .........

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I

i , . -.

I '

e s'

APPENDIX

"CONSTAFR RATE" PUMPING TEST DATA FROM WELL NO. ? &/TwEZ?y #I'

~ ~~~~

! U.S.gals. I permin. j discharqe 1 from w e l l 1

!

Time (t) since

start of pumping i n mins.

{eight of water i n tube on w i f i ce

Pipe in inches

Depth t o water i n

w e l l from top of casing in feet

Drawdown i n w e l l i n f ee t

( s tat ic 1 -3d y z

-

~ .-

.--__ . . . _I__._ ...

~

.. .~ x

.. -. ..... - -_ ...... __ __ ...... - .......

~ . . . . . . . . . . . . . . . . . . . . . . . . . . -

- .......... -

... .- ... . - .

...................

__ - ____I___xI --

- . . - . .__-----I- .... -__ __ ...................... . _ _ _ _ _ _ _ _ _ r . __.__...._I-_.-.-.. ..

.-- --

----

.. .........

- .. .... ..... _.___I_ ..

,-- 23.95 z :o&r ! ! 320

........

! !

.- ----A---

J~ I- - ._________

I

j - ! -- -. .......

........... 1 -----..--... 1 ...--_..._I .

i .... ---. --_A

._ . . . . * ._ . ......... ... I

. .

! i I . __I-- L - -. ...... I

- ..........

I ; I

I . I

I I . . .

I

-. 1

..... ... ..... .. i

.. ........ .......... ...........

.. .I . . . -. . . . . . . - ... - .......

. . --__ ... -. .....

........ . . . . .

- - .- . .-. _.

- - .

.. - . . . . . .

...... -. ... - .

.. ..... . . . . . . . . - . .

...... . . . . . ..... . _ ............

.. -- ...... .- _ _ - ......

. . . . . . . . . . .

. . . - ...........

......

. . . . . _. ... .... . " -

. . . . . . . . . . . . . . . ... - . . . . . 1

I

1 . . . . I

... . . . . . . . . . . , . . _. . . . . . . . . . . . . . -.-. -

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Time (t) 1 Depth t o Drawdown I Height of T h e since I water i n 1 i n wel l 1 water i n

I U.S.gals. 1 per min. j

I 0 s t a r t of 1 wel l j i n f e e t tube on , discharge

pumping 1 f ron top j ( s t a t i c j o r i f i c e I from w e l l '

----i- i

...... .-__ ........ I ---. .....

i : . . .......

.......... . . . . . . . . . .. ..

. . ......... ....... ............ .

_. --

.. - ...... . . .

0.82

-

.. . . . . .

.... ...... . . . . . .... .

..

k ... ... .... ... '

- 1

-. ,

-.-.

-

... ...... 1 ____ ................... _ _ .. ... .

... .... ... ...... .......... ..... ..

..... .-.&<.E .......

50 ............ -. 6 0 --._

7.0

30 .......... .. - .-

9:zo 9 .'85

___ - .... - .. - _. ............ . -. __ ..

.- - ._ .- ... .. ... - ... - ... .. .- . . -. __ t i ......... ...... . . ~ -

.. . . . . . . . . . .._. ....... .. - ..... --

. - ... 93 .

...... 5 ... ..-de.- . ..

........ .- 79 ...... __

.. 80

... .....

- --I ... - ....

........... -. .

.- . . 3:55. .

.- 10: 0 5

/o ,' /5

........ +-. .......... ....

......... I .. -- ..................... --._I . ...... ----- I 36e37 f 6 ...... 90 - . . . -. . -_ .. I .... .... ......... - 1 . __ _. .... .- .

................. ........ -. PP ..... ... ...$% . . . . . . . . . . . '

. . . . . . . . . . . - .... - . ............... _. . . . .

. ,. . -.+ . . . . . . . . . . . . . . . . . . . . . .

100

/PO' . . .

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APPENDIX

RECOVERY READINGS or1 OBSEBVATION WELL NO.^ AFTEH . RATE PUMPING TEST ON WELL NO.

rn/9S€R /&LL E Y

Time ( t ) ! T i m e (t ') ~

since since

started stopped i n mins. ' in mins.

pumping ' pumping

Depth 1 Residual o water I drawdown i n w e l l i i n w e l l from top i n feet of casing' (stat ic

Time V a l u e of

t; 1 t'

3Za $. . . . . . . . . . . 0-5 _-

....... 3 w %. . i ...... L!-K..- . . . . .

322 % i . . . .

....

3 z/ ! /. a

3032 : 2 . B

.... - __ ............. - ..... _- .......

i

. . . . .

323 .. -..+ i 3,o 323% j 3,5

.. -. .....

. . . . . . . _ ......... . ... - ...... - -. .

. 324 -+ 4@ 3 3 . P 23 .. I... . 9%

.. 3R5 I z o 326 I 60.

.......... ._

... i

- ........ .-.c ....

I_ ....... -. ..... .. _-__ ... ___ ... -_ .....

..................... - .... ___ ._. ..... . - .- -.

-. - ...... ............ ._ - ................ -. ...

... ...... -.___.I .. -. .... ... ................... -

-. ..... ................. ..........

........ - ........... . . . . . - . - ....... _. .

-. . . - ...... I

...........

-- .............

.......... 9,o ... 3 3 -. .. . _ _ ...... - . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

38

35 ......... -. .. .

. . . . . . . . . . .

.... f! ........ -

95- ... ..............

$0 - ......... -. ........

.. _. . . .... ..

355 j ....

36u / I /

.... 29.0Z _. . . 1 0.5Z 29.00 i He50

~ ~ . . - ~ ............... -.

. . I .............. I

.................. .- .. .. __ .... ... 1

.--- ._ . - -.+ ...- __

- 365 - . . - .

- 370 . ._.

.- ... _. . . . . . . . . . . - . . . . ...

I . . . . . . -. ..................... _. . . . . . . .

i i . . . . . . . . . .. _. .- .... ....... ................... _- . . . . . . . .

....... -1. ........... - . . . . . . . . . . . . . . . : . . . . .- . . . - ........... ................... -- ..........

. . . . . . . . . . . . . . . . . . . . . . . . . . . .

- . . . . .

1 . . . . . . . . . I . . - I

.... : . . . . . . . . . . . . . . :

! ....

. -. .......

i

. . !

I

i ! I 4

I I . -.

- I 1

- !

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W

5 ~~CONSTAIX RATEII PUNPING TEST DATA FRON ~ L L NO. - Date FE&+ 32/77 w d2 PUnlrc;7//UG

&==2&??#e YdLLE y mw7- 447cA/&&y

I Time Time ( t) 1 Depth t o !Drawdown I Height of U.S.ga1s.

s ince water i n i n w e l l I water i n per min. ' well , in feet I tube on 1 discharge start of pumping I f ron t o p ( s t a t i c o r i f i c e , from w e l l I

' i n feet /6*5,9 i n inches

I

1 A i n mins. ' of casing = 1 j Pipe ' 1

1

I I I

Ad0 A43

I

. .. i

I I I I

i - I r - - - - I- - - - I I .I ........ . .- .... I . . . . .I... .... -- . . . .

I i 4 ...... .. ... . . . . . .... b 1 t I

.____._.__-.I

.

- - __I I

1 i I I ..-.--I -. __ _I_I .. __.I_ .- - ......... i ... -. .. 1 ............. -. 4 .... I

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Page 14: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

- The

. . .

. ..... _ - .

- . . . . . .

__ .. . . - ..

- . . . . . . . . . . . .

___ ... _. ...

- -

. _. ..............

-. ..... ....

. -- - - .

_ ........

........ _. ......

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. . ~ I_

.............

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...........

. .

..........

APPENDIX

RECOVERY READINGS or1 OBSERVATION WELL NO. - 5 AFTER . CONSTANT RATE PUMPING TEST ON WELL NO. - 8

I I

Time ( t ) ; ~ i m e (t') since since

PmPing pumping started stopped i n mins. i n mins.

3/5 0 . .- . . .; ......... - -

. . .3 92. . . . . 2 7 . . . . . - ...

! i

I

I . . . . . . . . -

_. .L .. . . . . . - I

.............

I

! i

.I-.. ..

....... ................... _- -. I

... - 2

i 1 ...... -.._--.I._.-

_. . . . - I ..

i ........ :.., . .......

i

. . . . . . . . . . . . I I

- ..... ,. ..... ......... 1

..... - .. . __ ......... _ _ .... -

- . . . . . . ............ - I .... .~..- _ ......

i .... - . . . . . . . - .- - .... - -

. I ..... .. ... I

.. - -. ... ._. ......... .

- ... ............... - . . _-

........... - . . . . . _ - .. - .. - ... - ..

...... .. - - . ......

-. ... -. ..... ... ..

I ..... .- .... .. __ .___. . ._ ....... .- ....

I - ... . .... . I

... .. .-I. -. . . . . . . . .

Value of

ti / t'

. .

t - I

.- . . . . . . . . ... -_ .. ...... 1 .. I ! - . . . ! ....... . . .

I I

I

- Date 22 ,/?77

I

Residual Depth ,o water drawdown i n w e l l j i n well from top in feet of casing' ( s tat ic

!

i i n feet I = j b q ) I /7&6 4.- i

I

. 17837 .. , 1 .....

..... - ....... . . -.._---_I .I ...... _- ........... v---- ... ...... .

~

--I__-

.--. . 4 ....

I ____ ... -.-+ ....... I

f - .......... ............

........ ...... __ ..

__ -. I -

... -. - ...

.......... . . -

_- _ ._ . __

. . . . . . . . . . . - . . .-

. .

I . . . . I

i

i . -

I 1 I

I

I -

!

Page 15: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

Depth t o I Drawdown Height of water i n I i n well

well 1 in feet from t o p 1 ( s ta t ic of casing : - - 1 in feet 1 3L3.yz

!

water i n tube on

o r i f i c e

i n inches ' P I P

Time (t) s ince

start of PwnPing i n mlns.

__ ......... .

. . . . . . . . . . . . . . . . . . . . - ...... - ... . __ ... - 3.

---------I.-- ...............

.. .-___ - .............. _--- ..........

I_--_

..... - _ ......

.- - ....

.

/.:?? Y+3? ... -_ ..... . . . . . ._ . . . . .

I... ... - ......... ..... -.-.. . - ........

........

. . . . . . . -

. . . . . . .

. ....

I

. . .

Page 16: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

"CONSTA!!" RATE" PLRPINC TEST DATA FROK WELL NO. - 6' / ~ ~ / ~ 7 ~ % % ! ~ -#I)

Date F ~ B . z Z ) 1 9 7 7 FR&%z J#LLE'/ %?0&'7 hy~C2(i$;tey --

Time since

s ta r t of well pumping I from t o p

! I in mins. ; of casing , = 3 d , 4L 1 in feet j !

yy* 8 2 -. c- . .. -_.____ -___ ...... ..... _- ............ ..I

~ -_-__.- _-.__-.-._ ..............

_ _ -_] - _-------- -..- .. __. - ~ -

______ _1 ....__.__-____.._._..... cY.s',g&- RR7.E ........ --. .- .... --

_____ ............. ... -_ .. I .. I -t- -- --

1 __ . .....

-----I 2:05 I : 32 0 -1 ----

-I---------- I T -- i

I -- __

I ~

__ --

_______ - ............. - ...

.

.---

... - - - -- ...

. . - ............

. . . . . . . . . .

. . .

. . . . _

I I

....... 1

.. 4 ~ .......

--I---.----- ---

I -: .....................

-- i . - -.- - . ........... ... -.-i .............. ..

I

. -___. ___ --.--- I I

i

I .... I ............ . --_ .

i . i" -. ............. -- ............

..................

--- .........

. . . . . . . .

. . . . . . .

........

. .

_. .

, -. . . . . . - . _. ...... , . .- _._ . . . . . . . . . . . . ...

. . . . . . ._ - . - . -. - .

. . . . . . . . . . . . . . -

. _ . . . .

. .

. . . . . .

- . -. . . . . . . . . . . . . . . . ..... - . . . . . .

. . . . . . . . . ! I

1: I

9

.. - . i

i . .

-. . . . . . . . . . . . . . ... . , . . .I

. . . I . I

. . . .

Page 17: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

. . . . : .. . . . . . . . . . . . " , .:jy . . r ,

. L2" $Y .P

/o;z5

// :R5

L -

---

__ _-- -- .-

__ --

. . . - . . .

.....

._%_.

. . . ..

. ._ . . . . . _.

. . . . . . . . . . . .

. .

- .+ - --- -. . ....

i; . . .

.-I-.-. _̂ ...._____ .-___ . . . . . . . . . . . . . . . - i. F E . _ _______._ - -. . __ - . -. -. . -. .- .

. _____________. __.__.___ ...... - . . .

..... ......... - .. ....... . ---

.. . - ........... ____ _--_ .

............. -- .-

. ...............................

. -- ....... - - ....

. . . . . . . . . . . . . . . . -

.................. 36,37 #6 _ _ > _ _ _ ...... ...

....... ........... ..__ -.. ...... .- .

. . . . . . . . . . . ...

Page 18: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

Time

,

Depth I Residual 1 i n wel l 1 i n well 1 of casing ( s t a t i c in feet I from top

t o water I drawdown

i n f e e t , =zg,59 1 1

I Time (t) Time (tl)

s ince s ince pumping pumping s t a r t e d stopped i n mins. i n mins.

Value of

t 1 t'

! i , .

I .

I i i

'3c.50 .... - .... - .......... / . . . . . . . . , .. .- . . . . . . . . c . . . . . . . . . . . . . . . . . . . . . . . _ _ ... ......

330.0 ... . -

....... - . . . . - ....

. . . . . . . . . . . . . . . . . . . . . . . . . . . - I i 23.58 i I /.08

..........

- .- I--. _-_ 2 9 . 3 9 *-.

29.35 0.85 . . . . . -. .. ..... ................... -.

....... ... 36.56 .. -

I - $9.33 ... .... f 0.83 . - I ........... - ......... - -. . . . . . . . . . . . . . . . . . .

29,zg -. . __- 1 0.78 1 ... ......... .- ............. 372 /z. 0 _ _ . . . . . . . . . . . . . . .

. . . . ,33f ........ 156 ......... - . .. - .. . . . . . . . . . . . . . . . . . . .

c.z9..92 . . . . . . a.5z . . . . -. ................... .- _. . . . - 1 ..-

._ 29.00 j a.50

. . . . . . . . .i- - .. ..... L- - - . . . . . . . . . . . . . . . . . . . _ _ _- . . . I

. ..... - ..... - .. - . . . . . . . . - . I . . . . . .-... - - + .. -. . . . - ...... .- - . . . . . - . . . -* .- .. . .

. . . . . . . . . . - I I ...... . . . . . . I

. . . . . . . . . . . . I . . I I

. . . . . .. I -. , I

. . . .

. - ...... I . . . . . . . . . . . . . . . . . . . . . .

I ' ........ - . I . . . . . . . --. ........ ....... _. . I - .....

.. I . . . . . . . . .

b . .

I

i I I 1 1 .

I

.-

I

Page 19: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

AT1’13 I X

. i. .

! I ... - ... _ ......... I .... __ .... I . - ..... ._ .......... - . . . i i I

* - ............ - - - ...... 1

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- ..... .... ... . ---- I I I

I !

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i .- - t

i

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i

. . . . . . . - .. !

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i I - I

4

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... ., . .- _-.--- ...... __ .- __

- ....... ._ .. - .. . . . . . . .

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, . . . . . . . . . .... . . . . .- . . . .

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Page 20: OF URlTlSH - a100.gov.bc.caa100.gov.bc.ca/appsdata/acat/documents/r5646/1227_1143237025139_af73e... · as the actual drawdowns were much greater than expected, suggesting pumping

. . . .

--

. . .

. - . .

. - . . . . -. .

__ - ..

--e-

...

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. . . . . .

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............ .-

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.............. .: ................

......

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.._ . - - . . . . . - i s - - 1 . .. --_ ____. ... . -. i ...... ....

-. _ . - .. .. . . . . . . . . . . . . - - ... - .

. . ' + i . . . . . I . . . . . . . .

L

.-_ . . _ . . . . . .

. . . . . . - ............. I ..... - -. .. __ ............

.... ........ - - .- -. -.

.. - . . . . . . . - ..... - - - 1 ..

..... .i ....

I 1 i i

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