Vibration Issues of Diesel Engine

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    Resolving Vibration Issues of Diesel EngineDriven Fire Water Pumps

    in QP Offshore

    Case Study

    By

    Isham Sudardjat Sherief Mekawey

    Reliability Engineer and Principal MDS EngineerQP Offshore Operation GE-Bently Nevada

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 2

    Introduction to QP Offshore

    BackgroundTechnical Data and Acceptance Criteria

    Contractual Vibration Points

    Vibration Measurement Locations at Field Analysis

    Conclusions from Investigation

    Proposed ActionsFinal Vibration Results

    Lessons Learnt

    Contents

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore

    Introduction to QP Offshore

    WELL HEADPLATFORM

    PS-3

    PS-2

    HALUL

    TERMINAL

    SBM

    TANKER

    WELL HEADPLATFORM

    WELL HEADPLATFORM

    WELL HEADPLATFORM

    TOTALQPDOXY

    QP Offshore Operations comprises of: Halul Storage and Loading Terminal 2 Production Platforms:

    Maydan Mahzam (MM): PS-2 Bul Hanine (BH) : PS-3

    3

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 4

    BackgroundProject was started in 2004

    The scopes were engineering, procurement,installation, and commissioning of:2 jockey pumps (motor driven vertical pumps)2 sea water utility pumps (motor driven vertical pumps)4 fire water pumps (diesel engine driven vertical pumps with right

    angle gearbox)Jockey and Sea Water Pumps passed SAT while FireWater Pumps failed to pass SAT in 2006 due to highvibration.2 vibration consultants were involved to solve theproblems without success3rd vibration consultant was involved in Oct 2009,implementation of recommendations started in 2010,hand over in 2012.

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 5

    Technical Data and Acceptance CriteriaPump:

    Vertically suspended centrifugalpump, 3 stages

    1750 rpm, water lubricated, 880cu.m/hr

    Drive Shaft :

    Double Universal Joint Cardan Shaft

    Gearbox :

    750 HP, 1750 RPM,

    1:1 Ratio, Right Angle

    Threaded Coupling Type

    Diesel Engine :

    12 Cylinders, DITA, 800HP, 1750 RPM

    Acceptance Criteria:

    As per NFPA 20 article 7.6.1.5which refers to HydraulicInstitute Standard (5.84 mm/srms) at Pump Head

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 6

    Contractual Vibration Points

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 7

    Vibration Measurement Locations at Field

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 9

    Foundation/supporting arrangement for Diesel Engine, Gearbox and Pump.

    Reason could be: vibration isolators are not installed either underthe engine feet nor under the frame on which the engine ismounted.

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 10

    Observation:2 Startup/coast down waterfall indicated resonance inthe speed range 1200 to 1400 rpm Most likely from the cordonshaft or coupling hub

    Critical speed in the range of 1200-1400rpm

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 11

    Pump-B

    Pump-A

    Pump-D

    Observation:3 Bump testdata on the Gearboxstructure indicated aresonance at 22.5Hz and33 Hz, which is less than

    20% separation margin(Pump Running speed28.75Hz)

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 12

    Pump-A

    Pump-B

    Pump-D

    Observation:4 Highfrequency spectrumindicated 1X GMF withsidebands, indicatedpremature wear of gear

    teeth/excessivebacklash.

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 13

    Conclusions from Investigation

    Unbalance of Gearbox cordon shaft or couplinghub mounted at gearbox input shaftTransfer of vibrations from diesel engine to thegearbox and pump assembly

    Structural resonances from gearbox supportassembly.Premature wear of gear teeth / excessivebacklash .

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 14

    Proposed Actions

    In situ balancing of gearbox cordon shaft and GBO/P shaft.Installation of vibration isolators below theengine feet or the base frame

    Modify the Gearbox structure to shift the naturalfrequency with 30% separation margin.Inspection of Gearbox for excessive gearwear/backlash.

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 15

    Action-1: Balancing attemptedon GB I/P and GB O/P shaft toreduce unbalance on cordonshaft and to reduce excitation onthe GB structure respectively.(coupling between Engine andGB used to balance the GB I/Pshaft. GB fan at the top used tobalance the GB O/P shaft).

    Actions in Sequence

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 16

    1X componentbefore balancing

    Vib component at 22Hzshown after balancing

    1X component afterbalancing

    Action-1 (contd): In-situbalancing resulted in reductionof 1X. However the amplitude

    shifted to the frequency of 22 Hz(0.8X).

    Waterfall signaturebefore balancing

    Waterfall signatureafter balancing

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 17

    Action-2: The engine stand was replaced with a new stand withvibration isolators

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 19

    Action-3: Pump Head/Gearbox structure modified

    Old Pump head New Pump head

    GB TOP

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 20

    Bump test on the GB and pumphead (with modified head) showednatural frequency at 41.25 Hz(achieved 41% separation margin)

    GB TOP

    Pump head

    GB Bottom

    b d d f d l h

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 21

    Action-4: Gearbox inspected and found only 70% teeth contact.GB OEM brought to site, gear backlash was checked and adjustedto conform to OEM specifications

    f b b f d f h b kl h

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    Resolving Vibration Issues of Diesel Engine Driven Fire Water Pumps in QP Offshore 22

    Before

    Now

    Comparison of vibration spectrum before and after the backlashadjustment on the Gearbox

    High frequency GMFcomponents & side bands

    Drastic reduction of High frequency GMFcomponents & side bands

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    Pump-D selected as pilot, implemented all the mentioned actionitems and resulted in great improvement. Red highlighted in tablebelow is the contract specified location (Limit 5.84 mm/s rms)

    Final Vibration Results

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    Lessons Learned

    All contractual limits must be carefully acknowledgedduring design and verified during FAT.Solving the problems in factory is much easier thandoing it on site.Get the right consultant involved at the first chance.Understand the size of problem since beginning couldsave time, cost and efforts.Major modifications might be a solution whenever theproblem is complex.