Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )

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  • 8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )

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    Model Defect Defect cause Corrective actionTKC0600 Transformer - Lead Dirty The acidification film which on the surface of i) Additional Checking frequency to ensure that " Solder Slot "

    contamination. solder slot not completely wipped off. So, free from the " Acidification Slot ".when PIN terminal getting tin,it attached on. Before : Checking 1 time pershift.

    After : Checking 3 times pershift.

    ii). Add checker to inspect for " Lead Pin " surface during mass prod.

    Supplier : Ryhoso

    TKC0800 Input Lead Set - Lead Oxidize Excess flux cover the wire lead re-action i) Improve process control by revise the soldering process towith solder become Oxidize if kept for prevent the flux re-action with solder.long storage time ( 6 Months ) Before : Dipping 100% of wire lead into the solder flux.

    After : Dipping 75% of wire lead into solder flux.

    ii) 100% re-inspection if the solder products was kept morethan 6 months after process.

    Lead withOK Condition

    Lead Oxidize( NG )

    Before and After Improvement :-

    Before:

    After :

    Solder Slot Dirty Contamination

    ( NG Condition )

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    No. Model Part Name DefectDetected

    RejectedRatio

    Defect (Rootcaused) Supplier Improvement activties

    1 TKC0601 Transformer Lead Dirty 130/ 21600 The acidification film which on the surface o i) Additional Checking frequency to ensure that " Solder Slot "Contamination solder slot not completely wipped off. So, free from the " Acidification fi lm ".

    when PIN terminal getting tin,it attached on. Before : Checking 1 time pershift.After : Checking 3 times pershift.

    ii). Add checker to inspect for " Lead Pin " surface during mass pr

    iii) Update work instruction for future monitoring.

    iv) Provide training to related PIC regarding defectrootcaused and action taken.

    Worst Defect 1 ( June 2013 )

    Dirty Contamination( NG Condition )

    Training Record

    Work Instruction

    Monitor List

    Process Flow

    Solder Slot

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    No. Model Part Name Defect Detected Rejected Defect (Rootcaused)1 TKC0800 I nput Lead Set Lead Oxidize NG 89/556 Excess flux cover the wire lead re-act

    with solder become Oxidize if kept folong storage time ( 6 Months )

    Worst Defect 2 ( JUNE 2013 )

    Lead withOK Condition

    Lead Oxidize( NG Condition

    Before :

    After :

    Before and After Improvement Action:-

    Work Instruction

    Attention Note Attention Note

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    Supplier Improvement activtiesi) Improve process control by revise the soldering process toprevent the flux re-action with solder.Before : Dipping 100% of wire lead into the solder flux.After : Dipping 75% of wire lead into solder flux.

    ii) 100% re-inspection if the solder products was kept more

    than 6 months after process.

    iii) Update work instruction for future monitoring.

    iv) Provide training to related PIC regarding defectrootcaused and action taken.

    Training Record

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    Monitor List

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    pcs pcs.