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8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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Model Defect Defect cause Corrective actionTKC0600 Transformer - Lead Dirty The acidification film which on the surface of i) Additional Checking frequency to ensure that " Solder Slot "
contamination. solder slot not completely wipped off. So, free from the " Acidification Slot ".when PIN terminal getting tin,it attached on. Before : Checking 1 time pershift.
After : Checking 3 times pershift.
ii). Add checker to inspect for " Lead Pin " surface during mass prod.
Supplier : Ryhoso
TKC0800 Input Lead Set - Lead Oxidize Excess flux cover the wire lead re-action i) Improve process control by revise the soldering process towith solder become Oxidize if kept for prevent the flux re-action with solder.long storage time ( 6 Months ) Before : Dipping 100% of wire lead into the solder flux.
After : Dipping 75% of wire lead into solder flux.
ii) 100% re-inspection if the solder products was kept morethan 6 months after process.
Lead withOK Condition
Lead Oxidize( NG )
Before and After Improvement :-
Before:
After :
Solder Slot Dirty Contamination
( NG Condition )
8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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No. Model Part Name DefectDetected
RejectedRatio
Defect (Rootcaused) Supplier Improvement activties
1 TKC0601 Transformer Lead Dirty 130/ 21600 The acidification film which on the surface o i) Additional Checking frequency to ensure that " Solder Slot "Contamination solder slot not completely wipped off. So, free from the " Acidification fi lm ".
when PIN terminal getting tin,it attached on. Before : Checking 1 time pershift.After : Checking 3 times pershift.
ii). Add checker to inspect for " Lead Pin " surface during mass pr
iii) Update work instruction for future monitoring.
iv) Provide training to related PIC regarding defectrootcaused and action taken.
Worst Defect 1 ( June 2013 )
Dirty Contamination( NG Condition )
Training Record
Work Instruction
Monitor List
Process Flow
Solder Slot
8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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No. Model Part Name Defect Detected Rejected Defect (Rootcaused)1 TKC0800 I nput Lead Set Lead Oxidize NG 89/556 Excess flux cover the wire lead re-act
with solder become Oxidize if kept folong storage time ( 6 Months )
Worst Defect 2 ( JUNE 2013 )
Lead withOK Condition
Lead Oxidize( NG Condition
Before :
After :
Before and After Improvement Action:-
Work Instruction
Attention Note Attention Note
8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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Supplier Improvement activtiesi) Improve process control by revise the soldering process toprevent the flux re-action with solder.Before : Dipping 100% of wire lead into the solder flux.After : Dipping 75% of wire lead into solder flux.
ii) 100% re-inspection if the solder products was kept more
than 6 months after process.
iii) Update work instruction for future monitoring.
iv) Provide training to related PIC regarding defectrootcaused and action taken.
Training Record
8/10/2019 Copy of IQC HQ Meeting June 2013 KGJ ( REV 3 )
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Monitor List
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pcs pcs.