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Now viewing document 14 ( 163859) of 71 in Search: 1 BP witnes ...
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BPXP
MDL2179VOL000006
Akins, Matt lAkins, Matti Guide, John I LeBleu, John 1 Shanghnessy, John I Atkins, Matti IIT -Rig Operations I IIT Targeted - Steve Robinson I IIT Targeted - Kent Corser I IIT- Corser, Kent I IIT Full Disk Laptop - Steve Robinson
BP-HZN-2179MDL00340813
BP-HZN-2179MDL00340824
BP-HZN-2179MDL00340813
12
BP- HZN-2179M DL00340813-BP-HZN-2179M DL00340824
Standalone
shaughjm
Microsoft PowerPoint- 4_DW LL - mar18_bpm .ppt
03/22/2010
05/13/2010
05/13/2010
1746282
2010%200318%20Brian%20Morei%20Horizon%20Update.pdf
Acrobat Distiller 8. 1.0 (Windows)
Desktop/20 10%200318%20 Brian %20Morel %20 Horizon %20U pdate . pdf
aD 18a 7cfd0edf928c51a86f2c33ff633
EXHIBIT# 'CJ( WIT: -----
http:/ lhorizon/i conect/i conect. dll ?F inishF il ter Fields 1126/2011
0 0 z , 0 m z --! )> r
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bp
Drilling Interval Clean-out run after Losses
0 0 z 'Tl
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Ul
Losses slowed from 360 ' 1 J 17 4 84 ppb - ,~ · ·~·~-· j Loss rate of 6 BPM I 360 BPH I "f !:~~ ~P!~!~w~~u~t~tic
Losses re-started after RIH to 2 LCM I 176 i 84 ppb wl additional fiber material. 9080' and staging pumps to 40 ! V
11
1 spm. Loss rate of 360 BPH i I I
------~r----------------------,,---------~~------------- f E
Pumped pill@ 5 BPM wl annular 3 Form-A-Squeeze 180 closed . Last 30 bbls w/ annular I Loss rate of 18 BPH.
open and no returns. 1 +-----------------------4
4 LCM 160 100 ppb. Pumped and disp w/11.1 ppg@ 6 BPM w/ annular closed.
. - --- __j
5 LCM 185 113 ppb. Pumped and disp w/ 11.1 ppg@ 6 BPM. Left 85 bbls inside
1 casing 1
Mixed at 11.1 ppg. Pumped pill@
Reduced BH pressure by 180 psi with 16.2 bbls base oil on kill line. Annulus static .
POOH to 8620'. Well static.
...
...
...
6 180 GPM (-4.3 BPM) w/annular Loss rate of96 BPH .._ Form-A-Set I 180 I closed.Left10bblinsidecasing .
7.1
7.2
8
(Did not mix properly) Pumped@ 35 SPM (-4.4 BPM) w/
Sweii-LCM I 109 ! annular, c&k lines closed . Chased Loss rate of 5 BPM (-300 with 5 bbls of mud. BPH)
I 1 I Pumped@ 35 SPM (-4.4 BPM) w/ .
EZ Squeeze 192 ! annular, c&k lines closed. Wait 2 . Well ~tat1c when checked after ., hrs. Hest Sqzd 150 bbls total. i pump1ng Sweii-LCM
Form-A-Squeeze 186 +Form-A-Set + 164
Disp w/11.1 ppg@ 5 BPM. Sqzd 75 bbls total.
Loss rate of 1.3 BPH v
Losses slowed to -18 BPH (in 5 min)
Losses at 2-2.5 BPM I -150 BPH
Losses at 7.5 BPM I -450 BPH
Well initially static. Losses at 21-96 BPH in next 3hrs.
8.5 hrs to mix pill. Losses at 19.5 BPH
Wait 9hrs after SQZ, losses at 1.3 BPH
Wait 2hrs after SQZ, well static.
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<!; Set 16" casing at 11 ,585' (765' off bottom- 12,3501
)
~ Cemented without returns
- Did not see Weatherford bottom plug release or land
- Top plug landed as expected
@ RIH with 14.75" x 16.5" Drilling BHA
-· Increased MW (11.5 ppg)
- Lesson Learned - DO w/ previous HS MW for LOT
- Drilled ratty shoe track
- Loss returns 3' above float equipment (channel)
G Pumped 160 bbls LCM pill (losses reduced 90 bph- 60 bph)
- Closed annular while cut mud back in pits and riser
~ Cut MW to 11.3 ppg (losses reduced to 24 bph) @ With annular closed cut MW in kill to 11.1 ppg (well static)
~ Cut MW in riser to 11.1 ppg and opened annular (losses static) ~~; RIH and cleaned out to -11 1619' TVD (bridge)
- 11.3 ppg mud I Gas at 419 units
- Spotted LCM pill
- Final losses 2.4 bph I Fill riser with 11.1 ppg
<!} POOH and pick up 3-1/2" stinger
"' Squeezed shoe with Halliburton CST tool and 195 bbls ¢$ Lesson Learned - CST worked well, base cement plug within 3'
bp
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® Lesson Learned- Running ramp squeeze very successful
~ LD tubing I RIH and drilled out 1 1000 -.-------------
~ Performed FIT to 12.55 ppg 1 900
- Lesson Learned: Always perform LOT in
sediment for exploration wells
$ Cleanout OH to 12,350'
- Hole packing off and sticking BHA
-- Fired jars on multiple occasions to free BHA
- · 405 bbls of cuttings back ( -33 avg hole size)
(.'$ Drilled head from 12,350' to 13,305'
- Increasing MW from 11.5 ppg - 11.9 ppg
800 -t-----1
Q)
;;_ 400 I * 300
200
100 0
2 3 4 5 Pump Rate
3
- 100 units of connection gas on connection (correlated to sandy section)
_, Sonic started to deviate near end of interval
··-· PP/FG estimate @13,305' -12.0 ppg (drilling w/ 12.3 ppg ESD)
2
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3510 :·.tl'\ ®
, . . I · T~~~~a I ~\':~119 ® Drilling wl11.9 ppg SMW 12.41 ECD I 12.3 ESD
I o,do . .. . t.20KI o Started taking influx while drilling at 936pm I shut
in at 1 0:09pm(30 mins) W()~•)l..vq
·.l<rb Flow.lJ)Ailg
·9 P,(n
Pit'VoluinaTotal. Qi)l
o:oc l .SK .1 ,QQKi 1.25K . . .. .-. - e
SPPA\rg PWO·ECD ::PSig'
Picked up off bottom 1 0'
Shut lower annular
35 - 40 bbls gas influx
SICP = 380 I Attempted to DP float with 500 psi
no communication
Pipe stuck- fired jars (5' movement) and took
overpull again
Shutdown and monitored pressures
Expected influx from 1 0' sand at 13,250' TVD
decrease 12.41-1 2.32
75 bbl flowback
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13.40
13.20
13.00
12.80
12.60
12.40
12.20
12.00
11.80
116~~
500
400
300
200
100
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-+-MAX- Estimate d Pressure@ Shoe
MIN -Estimated Pressure @ Shoe
·"'"' .r:::.<::. .r:::."' .r:::."' ..,,. ~· ..,,. ~· <::S ,<::S
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!1$ Monitored pressure in casing -max 520 psi
- Break down shoe at 520 psi (12.9 ppg-13.2 ppg EMMW)?
~ Rigged up Schlumberger wireline unit
t;'4 RIDP with 2.8" gauge ring (tag on xover@ DC)
e RIDP with Slim-CBL and temp log (1.69" OD) f ···trA·· "'{
® Tool stuck at 12,200' ·'
-· Lesson Learned- Don't run tools with large weak stabilizer
- Worked tool some downward movement
- Unable free
··- Pulled line max tension- 9700 lbs I
- Increased to 10700 lbs and came free
!1$ Ran 4" gauge ring run
@ Set Magna Range DP plug at 12, 150' ~r\ ( : I
Temp and slim CBl\.UJ - 34' long
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11} Severed OS at 12, 146' (6-518" HWOP)
- CP 330psi I OP 450 psi (50k tension)
@! Circulate kick out using driller method (11.9 ppg- 3 bpm)
-- Initial SICP 300 I SIOPP 110 psi (3 bpm)
- Final SICP 440 I SIOPP 380 psi
® Bleed off 4 bbls (c2501dp240), 3 bbls (180/220), 1.5 bbls (1701180), 2 bbls (150,130), after 15 min (180,120)
@ Circulated 12.1 ppg kill weight mud at 3bpm
-- SICP -150 psi I SIOPP -110 psi
-· After 1.5 hrs SICP- 130 psi I SlOP 120 psi
® Circulated 12.3ppg kill weight mud at 3 bpm
- SICP- 60 I SIOPP- 70
~~ Swept stack and opened riser- static
~ Circulated mud to clean-up gas
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:s: 0 r 0 0 w ~ 0 ()) N ---"-
13.40
13.20
13.00
12.80
12.60
12.40
12.20
12.00
11.60
116~~
500
400
300
200
100
0+
.<::;Ci> ,zl-'
' "<;::, g}
n}t:J
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·"' "1::> ~
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--+--MAX- Estimated Pressure @Shoe
.CI>Ci> .c;::,Ci> c;::,CI> .CI;Ci>
""'" !:I' .... ~- !:I '
' ·"' ' ·"' ~~ ~"<;::, "1::> .... ~~ ~ .... ~ n}"' n} n} n}
.CI>CI> .<::;(/; .CI>CI> .<::;Ci> .<::><::> .<::><::> .<::><;::, .<::>(/;
""' ' !:I' ""'' !:I' ""'' !:1' ,zl-' !:I' ,<::J '
,<s '
,<::J '
,<s ~"<::; "1:1 "1::> "1::> "1::> Ill 1::> <::;
...... ~ .... -v ~ ~ ti.-"' ti.-" 4" n} n} n} n} n} n}"' n}"' n}''
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~ Spotted 200 bbl plug@ 12,1 00'-11585' (gauge hole 515'- 20" hole)
® Tested choke/kill manifold
@ Tagged plug at 11,863' (237' or 29.5" hole)
w Weight tested plug per MMS with 16k down
'!!! Tested BOP
~ POOH and picked up 3-1/2" stinger
~ Spotted cement plug #2 (260 bbls)
& POOH with stinger and RIH with drilling BHA
OJ# Tagged cement at -11 ,600'
$ Kicked off using geo-pilot at 11, 700' with poor cement plug (2.25 deg/1 00' to 1 0 deg)
Plan Forward
lb
~
Drill to 13, 1 00'
Top. set pressure sands with 13-5/8" casmg
' Ml.·: @·!: -?:4j~1.f ' ~IQ"T:l(D 1 6.· ~:~PP~?~rief-taJ '::d¥:l.er .r;tt:. ~-f; :izi~_ ln 22-: f.)'.tens1~ii JC!II1t-
18.375~; ID : (~ iS"\ov.;;l_l pif"" abci'-'~?
-- ~~·.' @.'5~:i~'i;:t.Jn;h;f\t0:~f.25~~ l).n"ii' ·
:1P? ~~- :c :z.; l.l.f>$_:,J\< (1: . .trts!J>'.J:>[i~lj :- .
~I • ~
~ t1 ~-
1 \1-~~ li!:,-~~U'f ' ' fll'IJ; lTV ~ ,p~li ;'!- ' t]oi n l • :. f;'
tol-..-.11 ;t"es'
r¥ : ___ i2;_¢,~q; ·_-_ i~PirY~ .: l:o~ -~ 12 ,600'. i-.DfrVD
'r c,)c_: -17 -,2~0' ii'IOITVO:
·-···--·· ~!fo~:~J;~-:~2.9~~qfi.~.:-....
· i .. ·.;·'*-7tff· @::-i"aj5o· MD(TVO ·
· ·······c~c·:···cc:· ·-•c.-.::•··c~-7-.·-~-.-- -.--.-..,..,-..,,,, .. _-.:·coc·c-.:T•··
Se.:ovvRier
:t:.o IPP
9:.fi )F'fi..t:oT
Sl~- ~f' ..
~ 1~ : \~{-i:.,;).b .J) .. t_-'£1 '1 -SOBM
~ 122 · f JJfill[]!~~~~T---. . .. J.
-is~sm·(Sa:2 ppr· ~:·n::) tlY~1r_ir~2,~
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: i 'H',5~ IPP ·. rd~!i!;;;_ IFJH.OT
13.1 IPP.
''" -:-. · :-;-~ .. - ---·--··-···· ···----~ 1FIT,LOT
1.1 ~?If:(_ 7 !'-6 'pl?t :· ~-1--~~ I:IY~ril_ 5.1 .~
13.8 if"P. ' 1!>.5 - ]FIT.·l.:OT