Treatment of Sugar Mill Waste Waters

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    Processing

    TREATMENT

    OF

    SUGAR MILL WASTE WATERS

    R. R. ~ i t h ~ a t e ,. S. Keniry and A. W. Strong

    CSR Limited, Sydney, Australia

    The system installed at Victoria Mill for the treatment of waste

    waters is described and the design concgpts and operating procedures

    are discussed. The system involves two stage treatment of wastes in

    well-mixed ponds each with sludge re-cycle. The first or primary

    stage is equipped with two small surface aerators and operates in a

    primarily anaerobic condition with pH control and nutrient addition

    The second stage is an aerobic activated sludge system. A third pond

    is provided for pre-treatment of strong wastes prior to discharge to

    the primary pond. Retention time in the primary pond is approximately

    4 hours and slightly longer in the secondary pond. Suspended solids

    concentrations in each pond are controlled at about 2500 mg/l with

    excess sludge being disposed of to surrounding grazing land. In 1975

    season the system handled an average daily volume of 3598 mh a s t e

    containing on average 949 mg/l BOD5 and yielded final effluent

    containing on average 6

    mg/l

    BOD5

    and 58 mg/l suspended solids.

    INTRODU TION

    By the mid 1960 s it was apparent that increasing environmental

    awareness would necessitate a reduction in the amounts of

    BOD

    and other

    pollutants being discharged from many sugar mills in Queensland. In the

    particular case of CSR mills, the conclusion was reached that some form of

    treatment system would be required to treat, before discharge, effluents

    other than condenser cooling waters.

    Up to this time, there appeared to be little published work concerning

    the treatment of waste waters containing mostly carbohydrate wastes.

    Accordingly, in 1968 a development programme was commenced with the

    aim of developing a process to reduce the

    BOD

    level of mill effluents to

    about

    30

    mg/l at low suspended solids concentrations. The early stages

    of the programme involved both laboratory scale and plant scale pilot

    treatment trials, and culminated in the commissioning of a full-scale

    treatment plant at Victoria Mill late in 1973 season. A similar, but smaller,

    plant was commissioned at Goondi Mill in 1975 season, and a further plant

    is under construction at Macknade Mill.

    This paper briefly describes the full-scale liquid effluent treatment

    system at Victoria Mill and its operating performance in 1975 season. Par-

    ticular features of the current design and operating procedures, that have

    evolved during the laboratory and pilot plant stage, and since commissioning

    of the full scale system are also discussed.

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    PROCESSING

    DESCRIPTION OF PL NT

    A diagrammatic representation of the plant is given in Figure 1 and

    the specification of major items of equipment is tabulated in TAble I Factory

    waste waters, including spray pond overflow, are pumped to a preliminary

    treatment plant which consists of two 1.83 m wide D.S.M. screens with

    2 mm bar spacing to remove fibrous matter and then to a 27 m3 oil

    separation tank to remove heavy greases.

    The water then flows to the primary pond, except in the case of strong

    -wastes, generated on weekends or at other times, which are diverted to the

    weekend pond by means of motorised valves controlled from the factory.

    In the primary pond wastes are partially degraded under primarily anaerobic

    conditions with lime and nutrient addition, before being pumped to the

    primary clarifier. The clear overflow from the primary clarifier flows to

    the secondary pond, which operates as a conventional aerobic activated

    sludge process. Mixed liquor from this pond overflows to the secondary

    clarifier from which the final treated effluent overflows to lagoon Creek.

    Sludge is recycled from each clarifier to the pond from which it originated.

    Excess sludge from the primary treatment system is brought to an aerobic

    state over a period of two to four days in the sludge stabilisation pond prior

    to disposal by irrigation onto surrounding grazing land. Excess sludge from

    the secondary pond is irrigated directly in the form of secondary clarifier

    underflow. Under normal conditions approximately 10 hectares of land are

    used for irrigation.

    Treatment of wastes initially diverted to the weekend pond is discussed

    later.

    DESIGN CONCEPTS ND OPER TING PROCEDURES

    Series Versus Single ond System

    The results of early pilot plant trials in well mixed ponds indicated

    that for weekday wastes of initial BOD5 of up; to 4,000 mg/l, the average

    BOD, removal rate was greatest when the dissolved oxygen level in the

    mixed liquor was zero. At zero oxygen concentration in mixed liquor the

    rate of removal of BOD5 averaged 53 kg BOD5/kW/day, and was as high

    as 85 kg BOD5/kW/day on occasions. At these high rates the process was

    concluded to be substantially anaerobic, on the basis that the aerator oxygen

    input rate at 30°C and zero dissolved oxygen concentration was only

    33 6 kg/kW/day, as determined from both re-oxygenation and oxygen

    depletion tests. The former method measures the reaeration of clean water

    which has been chemically de-aerated and is usually termed the unsteady

    state reaeration method . The latter method involves stimulating bacterial

    growth so that the oxygen level falls to zero. As the oxygen level rises again

    the aerator is stopped at selected points and the depletion by bacterial

    activity measured. Residual BOD5 levels from the primarily anaerobic

    process were generally much higher than those that could be obtained,

    albeit at lower overall BOD5 removal rates, with an aerobic well mixed pond.

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    R . R . B AT H G AT E J . S . K E N IR Y A N D

    A W

    S TRO NG

    '7-

    Ba~ ass e nd Oil

    Primary

    Clarifier

    Secondary

    Pond

    Secondary

    Clarifier

    Primary

    F

    Final Discharge

    FIGURE 1

    Waste water treatment system Victoria

    Mill.

    .

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    R.R. BATHGATE J. S. KENIRY AND A.W. STRONG

    2513

    The superior

    BOD5

    removal rates obtained in a well mixed anaerobic

    pond offered a major potential advantage in terms of capital and operating

    cost of full scale treatment systems. However, a full anaerobic system suffered

    the disadvantages of objectionable odour and unsatisfactorily high

    BOD5

    in final effluent. The compromise solution was to adopt a two ponds n

    series ystem where the primary pond was operated in an anaerobic

    condition and the secondary pond was operated in an aerobic condition.

    Selection of Aeration Mixing Devices

    Floating surface aerators were selected in order to yield flexibility in

    operation at the pilot plant stage by permitting variation of liquor levels.

    The aerators were sized in order to supply complete mixing within the

    ponds. Complete mixing of pond contents was selected in an effort to

    maintain constant microbial activity at times of variable load. Aerators

    instead of sub-surface mixers were used in 't he primary pond to assist in

    odour and pH control.

    Control o f Oxygen and Liquid Levels in Ponds

    A problem frequently encountered in early trials was the formation

    in the ponds of poor-settling or bulking sludge. The bulking of sludge was

    associated primarily with the growth of filamentous organisms in aerobically

    treated liquors containing significant concentrations of carbohydrates.

    Observations indicated that the formation of bulking sludge was often

    associated with the transition from aerobic to anaerobic conditions or vice

    versa. Therefore a control system was installed to maintain aerobic condi-

    tions in the secondary pond, whilst a level controller in the primary pond

    maintains a minimum working volume by overriding the oxygen control

    system signal and reducing flow to the secondary pond when the minimum

    volume is approached. This minimum volume provides a buffer against

    shock loads on the primary pond. The control system is shown as Figure 2.

    It is assumed that facultative or anaerobic conditions are maintained

    in the primary pond by using aerators which supply only about 25 of the

    average oxygen demand in influent wastes. The large difference between

    oxygen demand and supply ensures continuous anaerobic conditions.

    The oxygen concentration in the secondary pond mixed liquor is

    continuously monitored and controlled at the desired set point of

    30

    sat-

    uration by regulating the flow from the primary to the secondary pond.

    As a general rule oxygen concentration varies inversely with waste strength

    and flow rate.

    The pH of the primary pond mixed liquor is regulated by automatically

    controlled dosing with milk of lime.

    A

    mixed liquor pH of 5.8 .0 gives

    good removal efficiency and satisfies odour control requirements. The pH

    of secondary pond mixed liquor requires no control and normally is in the

    range 6.8

    .3.

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    2514 PROCESSING

    Th e phosphate and nitrogen co ntents of mill waste waters are inadequate

    to satisfy microbial growth requirements.

    Current practice is to add commercial fertilizers such as high analysis

    superphosphate and aqua ammonia or di-ammonium phosphate to the

    primary pond. Nutrients excess to primary pond requirements pass to the

    secondary pond. The addition rate is regulated to maintain a concentration

    of nitrogen and phosphorous of

    1

    mg/l each in secondary pond mixed

    liquor.

    T he settling characteristics of s econd ary pond sludge are very sensitive

    I

    to nutrient levels and if n o excess nutrien t is available from t he prima ry

    pon d floc carryove r into final effluent is likely.

    Consequently nutrient addition must be carefully balanced between

    maintenance of adequate levels for bacterial growth and minimising the risk

    of eutrophication below the final discharge point.

    ,

    I

    Level Transmitter 4 Oxygen Recorder Controller

    2 Oxygen Meter 5 Automatic Control Valve

    3 Multiply~ng Unit 6 Oxygen Measuring Electrode

    FIGURE 2

    reatment plant control system

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    R.R. BATHGATE

    J . S .

    KENIRY

    AND A W

    STRON 25

    5

    Weekend Wastes

    Extremely strong wastes from washdowns and spillages are diverted

    to the weekend pond for pre-treatment, because of the longer retention time

    required to reduce the

    BOD5 load to a level acceptable for feeding to the

    secondary pond. After pre-treatment which includes pH control, nutrient

    addition, and some primary sludge re-cycle, these wastes are slowly bled

    back into the primary pond. The rate of bleed depends largely on the load

    on the primary pond; the time to empty the weekend pond each week varies

    between two and five days. Operating conditions in this pond are similar

    to those in the primary pond,

    aerators being used for mixing,

    OD

    reduction and for prevention of odours.

    The combination of primary and weekend ponds provides a buffer

    system which reduces the effects of variability in strengths of mill wastes

    and allows smoother control of flow to the secondary pond.

    Odour ontrol in Primary Pond

    Anaerobic or septic conditions are usually accompanied by offensive

    rotten egg type smells, but this is not the case for the primary pond. It is

    considered that hydrogen sulphide and other gases are oxidised to odourless

    compounds by introduction of oxygen, and that pH control prevents the

    formation of a strongly reducing environment which favours the production

    of sulphurous odours by sulphate reducing bacteria. Other smells caused

    by partially reduced volatile carbohydrates which are normally produced

    under anaerobic conditions, are minimised by maintaining pH

    5 5

    or greater

    in the primary and weekend pond mixed liquor.

    Pond Retention Times

    Trial work indicated that for continuous treatment,

    24

    hours retention

    in each pond of the series was sufficient to produce good quality effluent.

    In actual operation the retention time in the primary pond varies between

    19

    and

    32

    hours and in the secondary pond between

    26

    and

    40

    hours

    without noticeable effect on final effluent quality. We believe that shorter

    retention times are possible and trial work is being undertaken to test for

    the effect of shorter retention time.

    ontrol o f Suspended Solids in Mixed Liquor

    Suspended solids in both ponds are maintained between

    2000 000

    mg/l preferably close to

    2500

    mg/l. It has been found that a minimum

    suspended solids of

    1500 000

    mg/l is required to prevent the growth

    of single cell yeasts when loading is high. At suspended solids concentrations

    in or above the upper end of the operating range, clarifier overloading can

    occur if the flow rate is high. Higher concentrations also can cause poor

    quality effluent

    by

    producing large quantities of fine floc when the waste

    load decreases to a point where the population is starved for food; and can

    aggravate sludge disposal problems when strong wastes lead to high bacterial

    growth rates.

    \ I

    t

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    2516 PROCESSING

    Pre-Season Sludge Preparation

    Initially, sludge was formed by the addition of molasses to the sludge

    stabilisation pond, with adequate nutrients, at such a rate that aerobic

    conditions could be maintained by the 10 kW aerator. When bacterial growth

    increased the suspended solids level to about 2000 mg/l, the contents of

    this pond were pumped to a larger pond where growth continued with

    further molasses and nutrient addition. This continued until sludge concen-

    trations reached 2000 mg/l in both primary and secondary ponds, and

    thus were available to commence full treatment of mill wastes. About five

    weeks preparation time would normally be sufficient.

    For the start of 1975 season, sludge held over from 1974 was fed with

    molasses to generate further sludge. This reduced the preparation time from

    five weeks to three weeks and reduced molasses requirements from 27 tonnes

    to 16 tonnes.

    T BLE II Operational data Victoria mill treatment plant 1975 season

    Mill waste waters

    Average daily volume 3598 m3

    Average daily BOD5 content

    3 97 tonnes

    Treatment plant discharge

    Average daily BOD5 concentration

    daily results

    <

    20 mg /l BOD5 40

    Average daily suspended solids concentration 48 mg /l

    daily results

    <

    30 m g/l suspended solids 43

    Average daily oxygen concentration 61 saturation

    Average daily temperature 4 O

    Average daily oil grease concentration < mg/l

    Relevant operating data for the first 23 weeks of 1975 season are

    presented in Table 11

    The quality of waters discharged from the treatment plant during both

    the 1974 and 1975 seasons was adversely affected by the presence of clay

    eroded from the ponds walls. Measures taken during the 1975 slack season

    reduced the amount of erosion to the extent that the 61 mg/l BOD5 and

    213 mg/l suspended solids averages for 1974 were reduced considerably

    to the levels achieved during 1975. With the further knowledge gained during

    1975 season and further work during the 1976 slack season we expect the

    quality of the final effluent will improve further.

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    R . R . B A T HG A T E J . S . K E N I R Y A N D A W STRONG 2517

    A C K N O W L E D G E M E N T S

    The authors express their appreciation to the Management of CSR

    Limited for permission to publish this paper, and to the many CSR staff

    particularly the late Mr.

    J

    R . Miller, who, over a number of years, have

    contributed to the development and evaluation of the system described.

    Th e company s consultants for the development of th e process were

    Water and Trade Wastes Consultants Pty. Ltd. of 2 Barrack Street, Sydney,

    N.S.W. 2000.

    T R A T A M I E N T O D E L A S A G U A S D E D E S E C H O

    D E L

    C E N T R A L A Z U C A R E RO

    R . R . Bathgate ,

    J

    S. Keniry

    y

    A. W. Strong

    R SUM N

    Se describe el sistema instalado en el Central Victoria para el

    tratamiento de las aguas de desperdicio incluyendo en el trabajo

    10s conceptos del disefio y la operacion. Para tratar 10s desechos

    el sistema incluye dos etapas que se realizan en lagunas bajo plena

    mezcla cada una con re-cic lo del lodo. La primera etapa va equipada

    con dos pequefios aereadores de superficie

    y

    funciona principalmente

    bajo condiciones anaerobicas con control del pH y adicion de 10s

    nutrientes. La segunda etapa es un sistema aerobic0 activado de tra-

    tamiento de 10s cienos. Hay una tercera laguna para el pre-trata-

    miento de 10s desechos fuertes cuyo pre-tratamiento se realiza con

    anterioridad a la descarga a la primera laguna. El tiempo de retencion

    en la primera laguna es de

    4

    horas aproximadamente; y algo mas

    prolongado en la segunda laguna. La

    concentration

    de solidos en

    suspension en cada laguna se controla a unos 2500 mg/l; descar-

    gando el exceso de 10s lodos a las tierras circundantes dedicadas a

    pastos. Durante la campafia de 1975 el sistema trato un volumen

    promedio diario de 3 598 md de desechos conteniendo en promedio

    949 mg/l BOD y rindiendo un efluente final que contenia en pro-

    medio 26 mg/l BODs y 58 mg/l de solidos en suspension.