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Reliability Improvement for Turboexpander-Compressor System Marc S. LeDuc Atlas-Copco Mafi-Trench Co. Hassan A. Mazi Saudi Arabian Oil Company © Copyright 2012, Saudi Aramco. All rights reserved.

Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

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Page 1: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Reliability Improvement for Turboexpander-Compressor System

Marc S. LeDuc Atlas-Copco Mafi-Trench Co.

Hassan A. Mazi Saudi Arabian Oil Company

© Copyright 2012, Saudi Aramco. All rights reserved.

Page 2: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Outline

• Introduction

• Turboexpander-Compressor Challenges

1. Buffer Gas Excessive Flow

2. Expander Speed Limit

• Execution Optimization

• Lessons Learned

• Concluding Remarks

Reliability Improvement for Turboexpander-Compressor System

Page 3: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Hawiyah NGL Plant

• Plant was commissioned in 2009.

• Three trains to recover Ethane-rich NGL.

• Each train has two 50% turboexpander-compressors.

• Reliability of EC system directly impacts production and operating economics.

Inlet and

Gas Treating Sales Gas Compressors

Turbo Expanders

Support Systems NGL Pumps

Cold Boxes

De-Methanizers

Gas NGL Utilities

Reliability Improvement for Turboexpander-Compressor System

JT Valves

Page 4: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Turboexpander-Compressor System

Reliability Improvement for Turboexpander-Compressor System

Compressor Discharge

Expander Suction

Compressor Suction

Expander Discharge

Mechanical Center Section

Page 5: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Co

mp

Exp

Mechanical Center Section

Reliability Improvement for Turboexpander-Compressor System

Bearing Housing

Position Sensor Electromagnet Auxiliary Bearing IGV assembly

Page 6: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Performance Assessment Survey

C E

C E C E C E

C E C E

Healthy – No Concern

Performance Problem

Production Limitation

The turboexpander exhibited three problems: 1. Buffer gas excessive flow (Bearing Housing) 2. Wheel imbalance (Compressor) 3. High magnetic bearing current (Expander)

Reliability Improvement for Turboexpander-Compressor System

Page 7: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 1: Buffer Gas Performance

Buffer Gas Functions:

1. Rejects heat generated by magnetic bearings and shaft windage.

2. Protects auxiliary bearings from process gas.

Buffer Gas = Sealing Gas + Cooling Gas

1”

Reliability Improvement for Turboexpander-Compressor System

Page 8: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 1: Description

During Pre-Commissioning:

• Piping vibration at seal gas supply valves.

→ Increased valves and piping from 1” to 2” for stiffness.

Subsequent Performance Problems:

1. High dP across on-skid seal gas filters.

2. Potential machine trip due to low seal gas dP.

Original Design

Modification during Pre-Commissioning

1” 2”

Reliability Improvement for Turboexpander-Compressor System

Page 9: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

2”

Challenge 1: Analysis and Solution

Problem Analysis:

• Cooling gas flow could be reduced, such that bearings temperatures remain < 230 °F.

Implemented Solution:

• Reduced the size of internal orifices to 1/8” to restrict the cooling gas flow.

Reliability Improvement for Turboexpander-Compressor System

Previous Modification

Current System Operation

Page 10: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 1: Realized Enhancements

• Seal gas consumption was optimized by internally reducing orifice diameters.

• Filter cartridge life was increased due to reduced seal gas flow.

• Turboexpander trip due to low seal gas supply differential pressure was eliminated.

Reliability Improvement for Turboexpander-Compressor System

Page 11: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 2: Expander High Current

• Some machines could not be placed back online after planned shut down.

• Once started up, machines exhibited high magnetic bearing current on expander side.

• When the machine was shut down, high current still persisted.

• Lateral shaft translation by AMB control system was necessary to restore magnetic bearing parameters to acceptable levels.

Reliability Improvement for Turboexpander-Compressor System

Page 12: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 2: Internal Inspection

Reliability Improvement for Turboexpander-Compressor System

Failed Screw

Non-failed Screw

Expander Rub

Page 13: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Challenge 2: Analysis

Expander Side View IGV Front View

Exp. W

he

el

Bearing Current Abnormal

Reliability Improvement for Turboexpander-Compressor System

Guide vanes

Follower Follower Locator

Page 14: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

No failure on threads

Low-Stress High-Cycle Fatigue

Reliability Improvement for Turboexpander-Compressor System

Challenge 2: Screw Failure Analysis

Page 15: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Old vs. New Screws

Cap Screw Design

Socket-head Flanged-head

Fillet between head and Shank

Small radius Larger radius Beveled washer

Material

A320-L7 A286 ↑ 60% tensile ↑ 500% fatigue

Reliability Improvement for Turboexpander-Compressor System

Page 16: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Safely Removed Rotating Assembly

Reliability Improvement for Turboexpander-Compressor System

Page 17: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Readiness and Execution

2010 2011

Apr May Jun Jul Aug Sep Oct Nov Dec Jan Feb Mar Apr May

NGL-2

NGL-1

NGL-3

IGV Screws

Comp. Wheel

Exp. Wheel

Secure shutdown windows and resources – User Role

Expedite material manufacturing/delivery – Manufacturer Role

Reliability Improvement for Turboexpander-Compressor System

Page 18: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Findings Summary

Finding/Cause Corrective Action

Excessive seal gas flow Oversized cooling-gas orifice.

Parameter difficult to estimate a priori.

• Reduced

orifice size to 1/8”.

Rubbed expander wheel Failure of expander follower screws (IGV assembly).

Improper screws design and material selection.

• Replaced damaged wheels.

• Upgraded screw material and design.

Reliability Improvement for Turboexpander-Compressor System

Page 19: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Lessons Learned

User’s Perspective

• Conduct joint review of equipment/piping layout by manufacturer and user prior to construction approval.

• Implement Management of Change for modifications made at construction phase.

Manufacturer’s Perspective

• Develop analytical tools to more accurately determine pressures acting on IGV components.

• Redefine fastener selection process to provide a better safety margin.

Reliability Improvement for Turboexpander-Compressor System

Page 20: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Lessons Learned - Continued

Reliability Improvement for Turboexpander-Compressor System

Original Design Modified Design Manufacturer’s Perspective

• Modified expander follower design:

a) Adjusted component geometry to ensure mounting stability of IGV assembly members.

b) Improved mounting screw material and geometry.

Page 21: Reliability Improvement for Turboexpander-Compressor Systemturbolab.tamu.edu/wp-content/uploads/sites/2/2018/08/METS2CaseStudy15.pdf · Hawiyah NGL Plant • Plant was commissioned

Concluding Remarks

• Turboexpander availability was boosted from 65% to 98% • Active magnetic bearings have outstanding resistance to

major rotor imbalance events. • Corrective actions effectiveness was confirmed based on

inspection findings. • The key to success was outstanding coordination for

─ Shutdown windows ─ Spare parts and material manufacturing ─ Technical and field support

Reliability Improvement for Turboexpander-Compressor System