18

PROCESS LEVEL ENERGY

  • Upload
    others

  • View
    2

  • Download
    0

Embed Size (px)

Citation preview

Page 1: PROCESS LEVEL ENERGY
Page 2: PROCESS LEVEL ENERGY

PROCESS LEVEL ENERGY MANAGEMENT TEAM

ON ASH HANDLING PLANT

MEMBERS:

R K OJHA, LEADER

K V REDDI, MEMBER

ROMIT MOHAPATRA, MEMBER

DILIP DAS, MEMBER

Page 3: PROCESS LEVEL ENERGY

NALCO AT A GLANCE

CORPORATE OFFICE

BAUXITE MINES ALUMINA REFINERY ALUMINIUM SMELTER

CAPTIVE POWER PLANT

ROLLED PRODUCT UNIT PORT FACILITIES

WIND POWER PLANT SOLAR POWER PLANT

Page 4: PROCESS LEVEL ENERGY

SALIENT FEATURES

BAUXITE MINES: Area od deposit – 16Sq.KM Resource – 310 MT Capacity – 68.25 Lakh TPA Transport – 14.6KM long cable

belt conveyor

ALUMINA REFINERY: Capacity – 22.75 Lakh TPA Atmospheric pressure digestion Pre-desilication & inter-stage

cooling for higher productivity Co-generation –4X18.5MW power

ALUMINIUM SMELTER: Capacity – 4.60 Lakh TPA 180KW Cell technology Micro-processor based pot

regulation system Ingot, wire rod, billet, strip

casting

CAPTIVE POWER PLANT: Capacity – 1200 MW Micro-processor based burner

management system Automatic turbine run-up

system Specially designed barrel type

high pressure turbine

ROLLED PRODUCT UNIT: Capacity – 50000 MT/ annum Products – Cold rolled sheets, coils

from continuous caster route Technology – FATA Hunter of Italy

PORT FACILITIES: Location: Visakhapatnam Export - Alumina Import – Caustic Soda Mechanised storage and ship

handling facilities

WIND POWER PLANT: Capacity – 50.4 MW, A.P.,

commissioned in Dec’2012 Capacity – 47.6 MW, Rajastan,

commissioned in Jan’2014

SOLAR POWER PLANT: Capacity – 260 KW Commissioned roof top solar

power plant at Corporate Office

Page 5: PROCESS LEVEL ENERGY

ALUMINA REFINERY

ALUMINA MAKING PROCESS

STEAM GENERATION PROCESS

BOILERS: Make – M/s BHEL Capacity – 4 Boilers of 200TPH – 1 Boiler of 250TPH Type - VU40, Bi-drum, natural circulation, oil/ p.f. fired, fixed tangential corner fired

TURBOGENERATORS: Make – M/s BHEL Capacity – 4 TGs’ of 18.5MW Type - Extraction back pressure TG Higher cycle efficiency due to co-generation

Page 6: PROCESS LEVEL ENERGY

BOILER

AIR PRE-HEATER

ESP

AIR

FUEL

WET ASH SYSTEM

ASH POND

DM WATER

PROCESS FLOW DIAGRAM

STEAM

DRY ASH COLLECTION

FLY ASH SILO

CHIMNEY

FLUE GAS

PRAYASH QC

6

ECONOMISER

Page 7: PROCESS LEVEL ENERGY

WET ASH DISPOSAL SYSTEM

BLR #3

BLR #2

BLR #1

BLR #4

BLR #5

BOTTOM ASH HOPPER

LINE - 1 5 2 3 4 STAGE

1

STAGE 2

STAGE 3

STREAM#6

AIR

PREHEATER

ECONOMISER

BOILER BLOW DOWN

ESP

PRAYASH QC

7

STREAM#5

STREAM#4

STREAM#3

STREAM#2

STREAM#1

Page 8: PROCESS LEVEL ENERGY

ASH POND

ASH DISPOSAL PUMP HOUSE

ASH SLURRY PIT

ASH SLURRY PUMP

Page 9: PROCESS LEVEL ENERGY

UPGRADATION OF

ASH SLURRY PUMPS

Page 10: PROCESS LEVEL ENERGY

ASH DISPOSAL PUMP HOUSE

• NO. OF STREAMS : 03

• ASH SLURRY PUMPS: 09NOS

• SERIES PUMPING

• CAPACITY: 635M3/HR

• HEAD: 44MTRS

• MOTOR: 150KW

• NO. OF STREAMS : 03

• ASH SLURRY PUMPS: 09NOS

• SERIES PUMPING

• CAPACITY: 350M3/HR

• HEAD: 50MTRS

• MOTOR: 110KW

ADPH-I ADPH-II

Page 11: PROCESS LEVEL ENERGY

ADPH-I

• ORIGINAL PUMP

• EFFICIENCY : 67%

• POWER CONS : 120KW

• UPGRADED PUMP

• EFFICIENCY : 76%

• POWER CONS : 106KW

UPGRADATION OF ASH SLURRY PUMP IN

STREAM-1 OF OLD ADPH

Page 12: PROCESS LEVEL ENERGY

POWER SAVING

• INSTANTANEOUS POWER SAVING : 14KWH

• POWER SAVING PER DAY : 336KWH

• POWER SAVING PER ANNUM : 122640 KWH

• SAVING OF POWER @Rs 3.20/- : Rs 3,92,448/- (PER PUMP PER ANNUM)

• SAVING OF POWER FOR ONE STREAM:Rs 11,77,344 /- (PER ANNUM)

Page 13: PROCESS LEVEL ENERGY

CALCULATION OF PAY BACK PERIOD

• COST OF REPLACEMENT OF ONE PUMP : Rs 6,15,282/-

• COST OF REPLACEMENT OF ONE STREAM : Rs 18,45,846/-

• SAVING OF POWER FOR ONE STREAM:Rs 11,77,344 /- (PER ANNUM)

• PAY BACK PERIOD : 1.6 YEARS

THE PAY BACK PERIOD IS ABOUT ONE YEAR APART

FROM IMPROVED LIFE OF COMPONENTS

Page 14: PROCESS LEVEL ENERGY

EFFICIENCY OF PUMP = WATER HORSE POWER

SHAFT HORSE POWER

Page 15: PROCESS LEVEL ENERGY

REASON FOR INCREASE IN HYDRAULIC EFFICIENCY

• FLOW PATTERN CHANGED FROM RADIAL FLOW TO MIXED FLOW

• TWISTED VANE IMPELLER

• MODIFIED HYDRAULIC ASSEMBLY

Page 16: PROCESS LEVEL ENERGY

MIXED FLOW

TWISTED VANE IMPELLER

MODIFIED HYDRAULIC ASSEMBLY

Page 17: PROCESS LEVEL ENERGY

CONCLUSION

• EFFICIENCY INCREASED BY 9%

• POWER SAVING PER STREAM – 122.64 MW

• NET SAVING IN TERMS OF MONEY – Rs. 11,77,344 /-

Page 18: PROCESS LEVEL ENERGY