ppchem-05-2011-3

Embed Size (px)

Citation preview

  • 8/9/2019 ppchem-05-2011-3

    1/8

  • 8/9/2019 ppchem-05-2011-3

    2/8263PowerPlant Chemistry 2011, 13(5)

    PPCHEM

    chemistry. All drum units in the sys-

    tem have a mixed metallurgy feed-

    water heater system and no con-

    densate polishing. The cycle

    guidelines are listed in Table 1.

    These operating parameters have

    served the system well. The peri-

    ods between chemical cleanings of

    the boilers have averaged ten

    years or better over the last 20

    years. The cleaning solvents used

    are either diammonium or tetra-

    ammonium ethylenediaminetetra-

    acetic acid (EDTA) depending on

    whether the boiler is natural or

    forced circulation. No extensive

    layup techniques were used on theunits during scheduled or forced

    maintenance outages because

    outage and down time was kept to

    a minimum. Because of chronic

    reheater tube failures due to out-

    of-service corrosion suffered by all

    the units, dry air blower systems

    were installed on the reheater sec-

    tions on all units. Unit unavailability

    from boiler tube leaks averaged approximately 5 %, and a

    majority of these failures were from corrosion fatigue.

    CHANGING OPERATING CONDITIONS

    With the slowdown in the economy, electric generation

    needs reduced. In 2009 a majority of the drum units in the

    FirstEnergy system were placed on an economic reserve

    condition. That is, the units were shut down but needed to

    be available within a 72 h timeframe for operational dis-

    patch. 72 h were needed because many of the plant staff

    were assigned elsewhere in the company (normally to the

    Transmission and Distribution Departments) while the

    units were not operating. To assure that the units were

    ready for operation, boiler or feedwater systems were notdrained. In addition, boiler pressure checks were per-

    formed to assure that during the shutdown and subse-

    quent cool-down of the unit corrosion fatigue cracks did-

    n't occur or could be immediately repaired. After the first

    week of unit shutdown and subsequent leak checks, a

    nitrogen blanket was applied to the drum.

    The requirements of economic reserve along with the

    boiler leak checks made cycle protection very difficult to

    obtain. Corrosion in a unit cycle is most easily shown by

    the 'corrosion triangle' (Figure 1).

    Corrosion occurs when all three elements are allowed to

    come together, much in the same way as in the firefight-

    ers' fire prevention triangle. When any one of the con-

    tributing elements is removed from the situation, corrosion

    cannot occur. There are two basic ways this may be

    accomplished in an electric utility boiler. The first is to dry

    out all components. Once water, or moisture, is removed

    from the system, corrosion is stopped, hence the reason-

    ing for the installation of dry air blowers on the reheat sec-

    tions of the boiler. The second option is to remove all the

    air, or oxygen, in the system. This is accomplished by

    evacuating all the air from an area and replacing it with

    nitrogen.

    Boiler Parameters

    pH 9.1 to 9.6

    Specific conductivity [S cm1] 5 to 20

    Cation conductivity [S cm

    1

    ] < 10Silica [mg L1] < 0.2 (pressure dependent)

    Feedwater Parameters

    pH

    Specific conductivity [S cm1] 1.6 4.0

    Cation conductivity [S cm1] < 0.2

    Sodium [g L1] < 3

    Dissolved oxygen [g L1]< 20 at the condensate pump discharge

    < 5 at the economizer inlet

    ORP [mV] 200 350Hot Reheat Steam

    Sodium [g L1] < 3

    Cation conductivity [S cm1] < 0.2

    Table 1:

    Cycle chemistry guidelines.

    Water Oxygen

    Exposed metal

    Figure 1:

    Corrosion triangle.

    An Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles

  • 8/9/2019 ppchem-05-2011-3

    3/8

  • 8/9/2019 ppchem-05-2011-3

    4/8

    An Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles PPCHEM

    PowerPlant Chemistry 2011, 13(5) 265

    Case History I

    The Eastlake #2 unit is a 124 bar, 130 MW forced circula-

    tion Combustion Engineering boiler with a GE turbo-gen-

    erator located in Eastlake, Ohio, on the shore of Lake Erie.

    This unit had spent various amounts of time throughout

    2009 in an economic reserve condition ranging from one

    week to two months. During the off-line periods the unit

    was available at all times to restart. Analyses for iron were

    conducted by grab sampling in an effort to understand

    when the greatest amount of corrosion was occurring and

    if our current efforts in unit layup were satisfactory. This

    grab sampling and iron analysis was also conducted on

    the other units with similar results. Sampling was con-

    ducted at the condensate pump discharge, low-pressure

    (LP) heater outlet (deaerator inlet), economizer inlet, boiler,

    and hot reheat. Figures 68 show the typical iron results

    that were observed.

    EPRI best practice for iron corrosion transport [3] is

    2 g L1 maximum at the economizer inlet. At steady

    state loads, the Eastlake units were able to maintain below

    5 g L1 maintaining the guideline limits given in Table 1.

    Iron corrosion throughout the cycle was at its maximum

    during transient load and startup conditions. More trou-

    bling were the iron concentrations at the hot reheat point.

    Dry air had been used on this section for the last several

    years when the unit came off line. Although

    there were no large spikes in iron as seen on

    the feedwater section, it was obvious therewas corrosion in the hot reheat.

    Anodamine was injected into the conden-

    sate pump discharge of the Eastlake #2 unit

    on March 30, 2010. The injection rate was set

    for approximately 350 g L1 and as pre-

    dicted cycle cation conductivity increased.

    Within 24 hours the amine formulation was

    throughout the cycle and all chemistry control

    parameters were being met and maintained

    with the exception of the cycle cation conduc-

    tivity. The cycle cation conductivity had

    increased by 0.17 S cm1 from the back-

    ground normal 0.18 S cm1 to approximately

    H O2

    Cathode

    (O being the most common)2

    Anode (Fe)

    2H O + 2e2

    2OH + H2

    Fe 2+Fe + 2e Fe O2 3 Fe O3 4, (FeO Fe O ) 2 33+Hematite, Fe 2+Magnetite, Fe

    Figure 5:

    Protection triangle.

    350

    300

    250

    200

    150

    100

    50

    0

    1

    TotalIron

    [g

    kg

    ]

    Unit off line

    Sampled during

    load increase

    Startup

    Condensate pump discharge

    LP heater outlet

    Economizer inlet

    Sampled during

    load increase

    Time [d]

    1 2 3 4 5 6 7

    Figure 6:

    Feedwater iron analyses.

    140

    120

    100

    80

    60

    40

    20

    0

    1

    TotalIron

    [g

    kg

    ]

    Unit off line

    Time [d]

    1 2 3 4 5 6 7

    Figure 7:

    Boiler iron analyses.

    80

    60

    40

    20

    0

    1

    TotalIron

    [g

    kg

    ]

    Unit off line

    Time [d]

    1 2 3 4 5 6 7

    Figure 8:

    Hot reheat iron analyses.

  • 8/9/2019 ppchem-05-2011-3

    5/8266 PowerPlant Chemistry 2011, 13(5)

    PPCHEM An Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles

    0.35 S cm1. The unit was scheduled for a

    shutdown over the weekend two days later,

    which gave an excellent chance to determine if

    corrosion rates had been reduced during this

    short injection period. Sampling commenced

    immediately after the unit was placed back inservice with amine injection. The unit was

    again taken off line because of a tube failure.

    Amine injection continued at a rate of approxi-

    mately 350 g L1. The results of the grab

    sampling are shown in Figure 9.

    The addition of the proprietary amine formula-

    tion to Eastlake #2 continued until November

    30, 2010. Transient and startup iron corrosion

    analyses continued; long-term results are

    shown in Figure 10. Analyses of organics were

    also made during this period with the resultsgiven in Table 2. As expected, the organic acid

    levels throughout the cycle had increased,

    accounting for the increase in the cycle cation

    conductivities.

    All iron data was averaged to determine the

    numerical reduction in iron transport and is

    shown in Table 3. These averages are derived

    from grab sampling; the majority of the sam-

    ples were taken during transient loading con-

    ditions.

    Iron results given in the graphs and tables are

    total iron concentrations, that is, the combina-

    tion of Fe2+ and Fe3+ analyzed by way of the

    ferrozine method. While reductions in total

    iron are seen in the data, it is very interesting

    to note these reductions include significantly

    lower Fe2+ ( 2 g L1) and copper oxides

    (highest 1 g L1). A direct reaction occurs

    between iron and reducing water to form solu-

    ble species and hydroxides. When iron cor-

    rodes in an aqueous solution, both oxidation

    and reduction occur at the anode and cathode

    respectively. At the anode, an oxidationprocess occurs [6]:

    Fe Fe2+ + 2e (1)

    2H2O + 2e 2OH + H2 (2)

    Reduction of Fe2+ concentrations is seen as the metal sur-

    face (anode) is protected by the filming amine. Validation

    of this protection was also demonstrated on Eastlake #2

    when the amine feed was interrupted for a one-week

    period several months into the testing period, resulting in

    both corrosion product oxides once again increasing out

    of specification (iron increased to 15 g L1 and copper to

    11 g L1). Note that during the Anodamine chemical

    injection period and once again after reinstallation of

    dosage following the interruption in feed, during base load

    and during transient load situations both copper and iron

    were measured as equal to and/or lower than control lim-

    its (iron) or below detectable limits (copper).

    With any proposed change in operation, management

    needs to understand immediate pay back. Listing num-

    bers and showing graphs may not generate interest if real

    dollar savings are not shown. Unfortunately, reductions in

    corrosion transport may not correlate directly to reduc-

    tions in corrosion fatigue failures for quite some time.

    Pitting damage from past corrosive conditions remains

    within the tubes and residual stresses will continue to

    cause cracking [7]. Savings can be found elsewhere.

    200

    180

    160

    140

    120

    100

    80

    60

    40

    20

    0

    1

    TotalIron

    [g

    kg

    ]

    Date [mm/dd/yyyy]

    03/31/2010

    04/02/2010

    04/04/2010

    04/06/2010

    04/08/2010

    04/10/2010

    04/12/2010

    04/14/2010

    04/16/2010

    04/18/2010

    04/20/2010

    04/22/2010

    04/24/2010

    04/26/2010

    Off-reserve Off-FO

    LP heater discharge

    Hotwell pump discharge

    Economizer inlet

    Boiler

    Hot reheat

    Morning ramp-upRamp-up in load

    (startup)

    Figure 9:Subsequent startups and transient load sampling after addition of proprietary

    amine formulation.

    FO forced outage

    350

    300

    250

    200

    150

    100

    50

    0

    1

    T

    otalIron

    [g

    kg

    ]

    Condensate pump discharge

    LP heater outlet

    Economizer inlet

    Date [mm/dd/yyyy]

    02/17/2010

    02/24/2010

    03/03/2010

    03/10/2010

    03/17/2010

    03/24/2010

    03/31/2010

    04/07/2010

    04/14/2010

    04/21/2010

    04/28/2010

    05/05/2010

    05/12/2010

    05/19/2010

    05/26/2010

    06/02/2010

    06/09/2010

    06/16/2010

    06/23/2010

    06/30/2010

    Anodamine injection

    Normalchemistry

    parameters

    Figure 10:

    Results of iron sampling before and after addition of proprietary amine

    formulation.

  • 8/9/2019 ppchem-05-2011-3

    6/8267PowerPlant Chemistry 2011, 13(5)

    PPCHEMAn Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles

    Assuming that corrosion product oxide release and trans-

    port from the economizer inlet are responsible for all the

    deposit buildup within the boiler, the approximate

    34 g L1 iron calculates to 95 kg of iron being trans-

    ported to the boiler. A chemical cleaning on this particular

    unit occurs approximately every ten years with 950 kg of

    iron (Fe3O4) removed. Hence, the iron corrosion product

    oxide transport rate measured at the economizer is very

    closely verified by previous chemical cleaning history on

    the boiler. Using the averaged iron maximum corrosion

    product rate of 6.7 g L1 now measured, this equates to

    18 kg iron transported. Using the same cleaning criteria of

    approximately 950 kg removed, a chemical cleaning

    would be required every 50 years for this particular boiler.

    I leave it to the reader to calculate the money and

    improved availability/generation saved from reducing out-

    age, in addition to the time, costs and environmental limi-

    tations required to complete necessary boiler cleanings.

    Case History II

    Anodamine has been used on four other drum units as a

    preservation method when the unit is taken off line.

    Approximately 72 hours before a known unit shutdown,the amine is injected at a rate of approximately 300

    500 g L1 and applied until the

    unit is removed from service. As

    with the Eastlake #2 experience, all

    unit cycle cation conductivities

    increased from approximately 0.2

    to 0.4 S cm1. Initial injectionsvaried in success however. Several

    of the units' cycle cation conduc-

    tivity values increased dramatically

    to nearly 1.0 S cm1 even though

    amine injection rates were kept at

    300 g L1. Unfortunately no sam-

    ples were obtained during these

    high cation conductivity periods. In

    subsequent injections of the

    amine, however, the cation con-

    ductivity values did not increase to

    the originally seen high values(~ 1.0 S cm1). This phenomenon

    seems to depend upon the boiler cleanliness and last

    chemical cleaning. 'Clean' unit boilers do not see unusu-

    ally high cation conductivities (an approximately

    0.2 S cm1 increase over ambient values due to organic

    acid production). 'Dirty' boilers, or those with higher mag-

    netite deposition loading, seem to experience a higher

    cycle cation conductivity increase (an approximately 0.4

    to 1.0 S cm1 increase) for several days. After the initial

    amine injection and several days of operation with the

    chemical, the cycle cation conductivity values decrease to

    the approximate 0.2 S cm1increase over ambient val-

    ues. Acetate levels in all units are comparable to those

    listed in Table 2. Figures 11 and 12 show visual inspec-

    tions of the condenser and a superheater tube during a

    unit outage. Similar results were found after the unit was

    idle for two months. Notice the hydrophobic characteris-

    tics and that the water droplets do not touch the metal

    surfaces.

    Case History III

    FirstEnergy management was concerned about the

    increased cycle cation conductivities and acetate concen-

    tration levels. These measurements were clearly outsiderecommended turbine manufacturers guidelines [3,9,10].

    Before Anodamine Use Anodamine Injection

    Feedwater and steam BDL 40 60 g L1 acetate

    Boiler BDL 0.2 0.3 mg L1 acetate

    Table 2:Average boiler and cycle acetate concentrations. Detection limit = 0.03 mg L1.

    BDL below the detection limit

    Condensate LP Heater Econ Boiler Hot

    Pump Out Inlet Reheat

    Previous chemistry 21.8 47.9 34.4 23.8 17.5

    Anodamine use 8.5 7.9 6.7 9.9 7.4

    Table 3:

    Total average iron corrosion levels before and after amine use. All data is stated in g L1 Fe.

    Figure 11:

    Condenser

    door.

    Figure 12:

    Superheater

    tube.

  • 8/9/2019 ppchem-05-2011-3

    7/8268 PowerPlant Chemistry 2011, 13(5)

    PPCHEM An Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles

    The supplier R & D proposed a

    newly developed formulation,

    Anodamine HPFG, a fully water-

    soluble, non-toxic, cyclohexyl-

    amine-free thermally stable amine

    formulation designed to continueexisting levels of metal protection

    throughout the entire steam-water

    cycle but to effectively eliminate

    cation conductivity increases.

    On November 30, 2010 the

    Anodamine HPFG solution was

    introduced into the Eastlake #2

    and #3 condensate pump dis-

    charges. As discussed, unit #2 had

    been on a constant feed of the

    original formulation while the #3unit had been subjected to injec-

    tions only 72 hours before a

    scheduled unit shutdown. After an

    initial increase in the cycle cation

    conductivity on Eastlake #3, the

    cycle cation conductivity de-

    creased during steady amine injec-

    tion until the unit was taken off line

    for a scheduled economic reserve

    off (see Figure 13). Eastlake #2 has

    been injected continually with the

    new amine formulation to date at a

    rate of 300350 g L1. Econo-

    mizer inlet cation conductivity data

    for that unit is given in Figure 14.

    Increases in the economizer inlet

    cation conductivity are normally

    seen during a drop in unit load

    (feedwater flow) or during a unit

    startup. Analysis of the cycle

    waters revealed organic acids,

    acetate, etc. to be BDL (below

    detection limits). Inspections of the

    condenser have given the same

    positive visual evidence of metalhydrophobic characteristics and water beading as with

    the previous amine formulation as discussed and shown

    under case history II (see Figure 11).

    CONCLUSION AND FURTHER STUDY

    Apart from the ever important cycle treatment require-

    ments of ongoing system protection, stability of oxides,

    lowering of iron transport, preventing or limiting of FAC,

    and protection of both ferrous and admiralty alloys in

    mixed metallurgy systems, there is also a simultaneous

    occurrence of moisture and oxygen during unit off condi-

    tions causing corrosion within the cycle. Traditional miti-

    gation strategies include dry layup of the system, which

    requires the use of nitrogen. Capital investment of bulk

    storage and piping systems needs to be undertaken to

    adequately protect the cycle if this path is chosen [11,12].

    In addition, the safety aspects of using nitrogen should

    never be minimized and include asphyxiation (> 18 % oxy-

    gen is fatal), compressed gas dangers, and freeze poten-

    tial. The other traditional option is wet layup. This option

    includes increasing the feedwater ORP with a reducing

    chemical [11] (hydrazine) in mixed metallurgy feedwater

    heater systems, which can lead to FAC. Wet layup also

    requires capital investment of deoxygenation equipment

    or, at the very least, techniques to deoxygenate makeup

    water to the unit as the recommended guidance for dis-

    0.50

    0.45

    0.40

    0.35

    0.30

    0.25

    0.20

    0.15

    0.10

    1

    Conductivity[S

    cm

    ]

    11/30/2010,

    09:00

    11/30/2010,

    12:00

    11/30/2010,

    15:00

    11/30/2010,

    18:00

    11/30/2010,

    21:00

    12/01/2010,

    00:00

    12/01/2010,

    03:00

    12/01/2010,

    06:00

    12/01/2010,

    09:00

    12/01/2010,

    12:00

    12/01/2010,

    15:00

    12/01/2010,

    18:00

    12/01/2010,

    21:00

    Unit off line

    Injection of Anodamine HPFG

    Date [mm/dd/yyyy, h:min]

    Figure 13:

    Eastlake #3 economizer inlet cation conductivity during injection of the new amine

    formulation.

    1

    Cond

    uctivity[S

    cm

    ]

    11/30/2010

    12/02/2010

    12/05/2010

    12/12/2010

    12/19/2010

    12/26/2010

    01/02/2011

    01/09/2011

    01/16/2011

    01/23/2011

    01/30/2011

    02/02/2011

    02/04/2011

    02/06/2011

    02/13/2011

    02/20/2011

    Unit off line

    Injection of Anodamine HPFG

    Injection of Anodamine HPFG

    Unit off

    Unit off

    Date [mm/dd/yyyy]

    0.50

    0.45

    0.40

    0.35

    0.30

    0.25

    0.20

    0.15

    0.10

    Figure 14:

    Eastlake #2 economizer inlet cation conductivity during Anodamine HPFG injection.

  • 8/9/2019 ppchem-05-2011-3

    8/8269PowerPlant Chemistry 2011, 13(5)

    PPCHEMAn Alternative Chemistry for Both Operational and Layup Protection of High-Pressure Steam-Water Cycles

    solved oxygen in the boiler is < 100 g L1 before firing

    [11]. In addition, the feedwater system piping and other

    susceptible piping throughout the cycle is prone to FAC if

    all chemistry conditions are not at optimal levels. These

    non-optimal conditions also occur during normal unit

    operation.

    The use of filming amine technology to protect out-of-ser-

    vice metal surfaces would eliminate the use of nitrogen

    and other traditional deoxygenation techniques for metal

    protection along with the costs and safety concerns asso-

    ciated with it. Utility equipment would be ready for imme-

    diate operation while also being protected from corrosive

    conditions. An excellent balance of unit protection and

    unit availability would be achieved. A one-year monitoring

    period that included continuous operation with a film-

    forming amine, Anodamine, along with use for layup

    protection in multiple units has shown that this type ofchemical control program can protect both iron and cop-

    per systems even when exposed to oxidizing all-volatile

    treatment and ammonia cycle conditions. Testing of this

    program also indicates a significant reduction in Fe2+, an

    indication of protection against FAC. Introduction of the

    filming amine chemistry in all units did not cause corrosion

    product increases or any other unwanted side affects.

    Recent positive testing of the water-soluble Anodamine

    HPFG product showed thermal stability throughout the

    entire steam-water cycle. This grade was able to keep

    cycle cation conductivity values equal to previous condi-

    tions, below and in compliance with turbine manufacturer

    guidelines of 0.2 S cm1 (not degassed cation conduc-

    tivity) and showed no appreciable levels of organic degra-

    dation products like carbon dioxide, acetate/formate, etc.

    FirstEnergy has entered into a tailored collaboration (TC)

    project with EPRI and several other U.S. utilities to further

    test the use of this proprietary amine formulation and its

    effectiveness for cycle preservation.

    REFERENCES

    [1] Interim Consensus Guidelines on Fossil Plant Cycle

    Chemistry, 1986. Electric Power Research Institute,

    Palo Alto, CA, U.S.A., CS-4629.

    [2] Cycle Chemistry Guidelines for Fossil Plants: Phos-

    phate Treatment for Drum Units, 1994. Electric

    Power Research Institute, Palo Alto, CA, U.S.A., TR-

    103665.

    [3] Cycle Chemistry Guidelines for Fossil Plants: Phos-

    phate Continuum & Caustic Treatment, 2004. Electric

    Power Research Institute, Palo Alto, CA, U.S.A.,

    1004188.

    [4] Deoxygenation in Cycling Fossil Plants, 1992. Elec-

    tric Power Research Institute, Palo Alto, CA, U.S.A.,

    TR-100181.

    [5] Flow-Accelerated Corrosion in Power Plants, 1998.

    Electric Power Research Institute, Palo Alto, CA,

    U.S.A., TR-106611-R1.

    [6] Guidelines for Controlling Flow-Accelerated Corro-

    sion in Fossil and Combined Cycle Plants, 2005.

    Electric Power Research Institute, Palo Alto, CA,U.S.A., 1008082.

    [7] Verib, G. J., Conversion of a Drum Boiler from

    Phosphate to Caustic Treatment. Eighth International

    Conference on Cycle Chemistry, 2006, Calgary,

    Canada.

    [8] Dooley, B., McNaughton, W., Boiler Tube Failures:

    Theory and Practice Volume 2: Water-Touched

    Tubes, 2007. Electric Power Research Institute, Palo

    Alto, CA, U.S.A., 1012757.

    [9] Steam Purity Requirements for Turbine Operation,

    Alstom Power, HTGD 90 486 V0001F.

    [10] Steam Purity Recommendations for Utility Steam

    Turbines, 2004. General Electric Company, GEK

    72281c.

    [11] Cycling, Startup, Shutdown, and Layup Fossil Plant

    Cycle Chemistry Guidelines for Operators and

    Chemists, 2009. Electric Power Research Institute,

    Palo Alto, CA, U.S.A., 1015657.

    [12] Cycle Chemistry Guidelines for Startup, Shutdown,

    and Layup of Combined Cycle Units with Heat

    Recovery Steam Generators, 2009. Electric Power

    Research Institute, Palo Alto, CA, U.S.A., 1015657.

    THE AUTHOR

    George J. Verib (B.E., Chemical Engineering, Cleveland

    State University, Cleveland, OH, U.S.A.) is the cycle chem-

    istry consultant at the FirstEnergy Corp. He has held vari-

    ous positions in fossil-fired plant laboratories and corpo-

    rate laboratories for over 32 years and now serves as the

    company water quality consultant. George Verib has

    authored 15 papers on various aspects of makeup water

    production, condensate polishing, and boiler water treat-

    ment. He is a registered professional engineer in Ohio

    (U.S.A.) and a recipient of the EPRI Innovators Award for

    oxygenated water treatment in once-through boilers and

    of the Technical Transfer Award for caustic treatment

    chemistry in subcritical drum boilers.

    CONTACT

    George J. Verib

    76 South Main Street

    Akron, Ohio 44308

    U.S.A.

    E-mail: [email protected]