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1
Failure of Transformer Cable box
A case study
Presented by –
Janardan Choudhary, Executive Director (O&M)
2
INTRODUCTION
The 280 MW Dhauliganga Power Station, NHPC Ltd, situated at remote
place of Pithoragarh in Uttarakhand, India, was commissioned in 2005.
4 x 70 MW power is generated at 11 KV voltage level and stepped up to
220 KV level through twelve single phase bank of generator transformer
and the power evacuation is done through two 220 KV line.
Unit is connected to a bank of 3 nos. Single phase transformer, 29 MVA,
11 KV/220 KV/√3, OFWF. LV side of transformer bank is directly
connected to generator through isolated phase busduct and high
voltage terminal of the transformer is connected to 220 KV GIS by
220KV XLPE cable through High Voltage Cable Box (HVCB).
3
DESCRIPTION OF EVENT
On 22/08/2016 all four units were running on full load (280 MW).
At 13:29 hrs Unit#2 got tripped on XLPE cable differential protection of
R-phase.
The oil from the HVCB splashed & spilled all over the transformer
The XLPE cable connected to one side of HVCB got detached from the
bushing and fell apart.
The sprinkler fire protection system operated and fire got extinguished
promptly without much spreading of fire.
From the event list it was observed that PRV and Buchholz relay of
HVCB and Buchholz relay of main transformer were also operated
during the event.
4
DESCRIPTION OF EVENTS- Extent of damage
Cable box, insulated copper flexible cable (connecting XLPE cable and
HV bushing of transformer), HV bushing of transformer and XLPE cable
end termination were damaged beyond repair.
Transformer also got severly damaged
Radius of outer winding, i.e. HV winding, increased due to huge
tensile stress caused by electromechanical force.
Looseness of sector and support, deformation of lower & upper
winding end support and coil clamping rings were also observed
Complete Core assembly is decided to be replaced
5
Damaged and detached XLPE Cable
XLPE Cable
6
XLPE cable detached from Oil to Air
Bushing installed at HVCB
7
Damaged Flexible link inside the HVCB
8
RESTORATION OF UNIT
The oil of the R-phase transformer of Unit#2 got contaminated with the
HVCB oil which was subjected to high energy arc.
The transformer was subject to huge electromagnetic force.
All oil from the HVCB got drained out. Therefore, after fault DGA of
HVCB oil could not be done.
DGA of main transformer showed higher hydrocarbon gas content which
was due to mixing of HVCB oil.
Total down time was 21 days (including two weeks taken for arranging modified
flexible link).
Gases
(ppm)
After
fault
Before
fault
1. H₂ 53 0
2. H₂O 32 5
3. CO₂ 894 176
4. CO 153 3
5. C₂H₄ 104 5
6. C₂H₆ 21 0
7. CH₄ 40 1
8. C₂H₂ 5.5 0
DGA of Transformer Oil
o So faulty transformer along with bushing
and XLPE cables could not be used
immediately.
o To avoid further generation/capacity loss,
the faulty transformer along with all other
affected equipment were replaced with the
spare one available at site.
9
ANALYSIS & ROOT CAUSE
Detailed investigation on damaged HVCB and connection of flexible link was
checked in healthy transformer.
It was observed that the flexible copper link (connecting XLPE cable and HV
bushing of transformer) was not as per drawing.
As per drg., the end connection should form “L” shape to maintain proper
clearance to ground
10
ANALYSIS & ROOT CAUSE
Existing connection: The end connection of existing link was provided
with a socket bolted with connector of bushings horizontally.
Horizontal Connection
With time, the bend at both ends near socket joints loses rigidity (firmness)
resulting into increased sag near the midpoint of the flexible link..
11
ANALYSIS & ROOT CAUSE
The sag in the existing link led to the reduced clearance with ground
near halfway of the link (approx. 4 mm).
As a result, Partial discharge might have started, which got ultimately
converted into an arcing ground with HVCB bottom and failure.
HVCB bottom
side
12
PREVENTIVE ACTION
Following measures were carried out to ensure the overall insulation
level of flexible copper link within HVCB :
Extra insulation (craft paper & paper board) was applied on flexible copper link to
increase its rigidity.
Modification in connection of link with the connector of the bushings.
By above measures, appropriate clearnce of link to ground (HVCB bottom) was
maintained over entire the span.
Vertical
Connection
Modified rigid flexible link
having “L” shaped end connectors
was connected vertically with the
connector of the bushings.
13
PREVENTIVE ACTION
With modification in end connection and extra insulation, clearance
between flexible copper link and HVCB surface is made uniform
throughout its span
All flexible links for the balance transformers has been planned to be
replaced in phased manner. However, tightness of the flexible link at
end connection and proper clearance with HVCB bottom has been
ensured in all transformers.
The depletion of oil level over time in HVCB shall also adversely affect
the overall insulation level of flexible copper link. Therefore, regular
monitoring of oil level in HVCB and its top up as required has been
ensured.
14
RECOMMENDATIONS
The transformer having oil filled HVCB must be type tested and
installation/commissioning should be done as per approved drawing.
Suitable alternative solution should be explored to minimise the use of oil
filled High Voltage Cable Box for high voltage transformer to minimise
such type of faults.
15
THANK YOU