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Energy efficiency campaign
Tata Steel, Jamshedpur
National Workshop
Industrial Energy Efficiency
8th November‘2016
India Habitat Center, New Delhi
Energy Efficiency Improvement Journey (Gcal/tcs)
6.088 6.083
6.017 6.012
5.767 5.750
5.200
5.000
5.100
5.200
5.300
5.400
5.500
5.600
5.700
5.800
5.900
6.000
6.100
6.200
FY'12 FY'13 FY'14 FY'15 FY'16 ABP FY'17 FY'20
Good -4%
By-product gas
firing facility in
Boilers, New
Power plants
132 kV Power
transmission,
Energy efficient
motor / equpt
CDQ boiler,
BF TRT, VFD
Gas holders
Focused
Energy
efficiency
campaign
Journey – Power Generation
180 200
218
220 236
238 239
298
127
95 99
108
65 70
42
0
0
20
40
60
80
100
120
140
120
170
220
270
FY'10 FY'11 FY'12 FY'13 FY'14 FY'15 FY'16 FY'20
Co
al C
on
su
mp
tio
n (
To
ns
X 1
03 )
Po
we
r G
en
era
tio
n (
MW
)
By-product gas based In-House Generation
Power Generation (MW) Coal Consumption (Thousand Tons)
Long Term CAPEX Projects under implementation
Scope of project : Jamshedpur works
Overall lighting load is expected to come down by ~50%
3MW installed at Noamundi. 6 (six) more locations have been identified at Jamshedpur Works.
Site survey for Solar plant at Jamshedpur Completed
Increased usage of by-product gas
Revenue generation from sale of coal tar
Expected reduction in annual Liquid fuel consumption at few identified areas by ~ 4%
LED lighting
Duel fuel burner for Pellet plant
CO
GAS Duel fuel
burner
Solar Power
Magnetic resonator to improve fuel efficiency
Long Term CAPEX Projects being pursued
Low heat recovery using ORC technology
Ability to recover energy from low temperature source
Adaptive control system and sophisticated diagnostic
Plasma gasification to generate syngas from steel plant waste
Steel Plant
waste Syngas
generation
Plasma
Gasifier
Injection in Gas
Network
Conversion of waste into syngas
Improved waste management (Waste generation- 10 TPD)
Recovery of energy at low pressure
Compact design with higher efficiency
Shorter installation period
2,10,000 Nm3/hr 320-360◦ C
300 kg/Nm3
SP#3 SP#4 DUST 2 gm/Nm3
2 X 18.7 TPH 275◦C
165◦C
Bag Filter
ID Fan
Recovery of Waste Heat from SP3 & SP4 Sinter Cooler @ 4.5 MT production.
Package TRT
2.73 MW F-BF
Top gas
GCP
Gas
Network
Blower
Packaged TRT installation at F-BF Power generation
Sinter Cooler Heat recovery
Quick Gain – Low / No CAPEX Initiative
Reduction In
idle or speed
Loss
Optimization
of
Equipment
& Process
Efficient
Use or
Right
Selection
Arresting
Leakage loss
/ waste
minimization
Run time optimisation of coal circuit
conveyor at Coke plant
Installation of Closed type Goggle
valve at ‘H’ Blast Furnace TRT to
increase its availability
Use of hydraulic control valve with
auto control facility for fuel supply in
reheating furnace of HSM
Optimization of heating system for HP
CO injection through modification in
gas pipe network
Increase in COG utilization reducing
coal tar consumption at Pellet plant
through modified COG network
Reduction on Oxygen venting loss at
LD1
Reduction in compressed air loss at
CRM by sizing and connecting to
compressed air network
Reducing power consumption at LD1
Vessel ID Fan by running at 1000 rpm
instead of 1550 rpm
Quick Gain – Low / No CAPEX Initiative
Reduction In
idle or speed
Loss
Optimization
of
Equipment
& Process
Efficient
Use or
Right
Selection
Arresting
Leakage loss
/ waste
minimization
Reduction in idle running of auxiliaries
of D&G machine at Pellet Plant
Reducing waiting time at LF1 by
shifting LC grade from CC1 to CC3 at
LD1
Modification of Blowing strategy to
optimize coal blast supply at F- BF
Compressed air network pressure
optimization
LP steam line network repairing /
modification to reduce steam loss
Use of waste wash oil in place of LDO
for Boiler operation
Supply of MP oxygen in place of HP
oxygen to Blast Furnaces
Speed reduction of ID Fan of LD1
Vessel from 1550 to 1000 rpm
11/15/2016 TATA INNOVISTA 2016
Spent wash oil: an alternative source
of energy
11/15/2016 TATA INNOVISTA 2016
Energy efficiency improvement
program launched in April 15
Genesis of idea
Steel Plant
Energy use
Coal
Fuel oil
Power
Industrial
Gases
Raw
Material
Coke
oven Coal Coke
Coke oven gas
Blast
furnace
Concerns in Current practices Generation of spent wash oil
Current practice in Industry
Direct selling as low value waste
for disposal
Distillation inside plant to recover
by products
Current practice in Tata Steel
Direct selling as low value waste
for disposal as distillation require
capital investment
Considerable amount
Environmental concern: Storage,
handling & disposal
Social obligation Accountability for the
entire life cycle from cradle to grave:
Dependency on external agencies, might
affect the brand image.
Gas
cleaning
Wash Oil Spent Wash Oil
Clean Coke oven gas for process use
11/15/2016 TATA INNOVISTA 2016
Current process & Process innovation
Major concern to reuse the Spent wash oil – It contains impurities
Objective : To identify the process by which Spent wash oil can be reutilised efficiently without
any Capital investment
Naphthalene is
absorbed in wash oil
Wash oil
Storage
Spent wash oil
Ric
h O
il
Na
ph
ta. S
cru
bb
er
Coke oven gas
Clean Coke oven Gas
Storage tank
for spent
wash oil
Le
an
Oil
Makeup wash oil
Temperature
is maintained
at 160 0C
(range 150-
180 0C)
Rich oil is
preheated
up to 140 0C
Naphthalene
and wash oil is
separated
Polymerized oil
Preheater
Na
ph
tha
len
e S
till
Regenerator Cooler
Rich Oil
30-350C
11/15/2016 TATA INNOVISTA 2016
Current process & Process innovation
Temperature is
maintained at
160 0C (range
150-180 0C)
Rich oil is
preheated
up to 140 0C
Rich oil is
preheated up to
150 0C
Naphthalene
and wash oil is
separated
Increased
up to 170
- 175 0C
Polymerized oil
Preheater
Na
ph
tha
len
e S
till
Regenerator Cooler
Rich Oil
30-350C
Process Approach Lab Scale Study
Literature confirms that appreciable
difference in boiling point temperature
between impurities and wash oil
Lab scale distillation with temperature
elevation of 100C
In the range of 150-1800C distillation
gives impurities < 0.001%
Plant trial
Plant trial conducted initially 4 hours
with two modifications
Spent wash oil quality improved with
impurities < 0.003%
Modification
11/15/2016 TATA INNOVISTA 2016
Exploration for utilizations - How
Development of idea
Sampling and analysis done by
Internal team – R&D
National test house , Kolkata
Average Properties LDO Spent wash oil
Gross Calorific Value,
kcal/kg 10200-10800 10872
Flash Point (P.M.C.C.). oC 66 50
Water Content (by Xylene
distillation), % (v/v) 0.25 < 0.01
Total Sulphur as S, %, max 1.8 0.45
Pore point, oC 12-21 (-) 6
Kinematic Viscosity at 40oC,
Cst 2.5-15.7 3.6027
Ash Content, % 0.02 0.019
Sediment, % 0.1 0.017
Carbon Residue, % 1.5 0.0010
Copper strip corrosion No. 2 No. 1A
Analysis has given startling result: all
parameters are very close to LDO except the
density.
This has triggered us to use spent wash oil as a replacement of LDO
11/15/2016 TATA INNOVISTA 2016
Exploration for utilizations - Where
Potential area of utiliasation
Area of Utilization Remarks Status
Heavy vehicles / Earth
moving machineries
Insufficient requirement
× Pre-heating Furnaces Quality issue in finished product
× Diesel Generator Intermittent use and OEM declined
× Boiler After lots of technical deliberation with subject
experts and statistical analysis it has been
concluded that boiler would be the best possible
utilization safely and in an effective manner
√
11/15/2016 TATA INNOVISTA 2016
Exploration for utilizations – Trial phase
PDCA 1
PDCA 2
Experiment in boiler Result
Use of spent wash oil in boiler
as support fuel
( Not connected to the network)
Failed
Improper oil atomization and
dripping of fuel
Use of spent wash oil as support fuel after
tuning/ readjustment of atomization
pressure ( Not connected to the network)
Successful.
Stable operation as a support fuel.
11/15/2016 TATA INNOVISTA 2016
PDCA 3
Experiment in boiler Result
Use of spent wash oil in boiler with
modified logic and reaction plan
(connected to the network)
Successful.
Stable generation as a load carrying fuel
No deviation in Chimney emission
No deposits on pressure part
Challenges Risk mitigation
Combustion failure due to higher viscosity
Tuning of steam atomizer control system with redefined logic
Inspection of deposits on pressure parts
Online monitoring of flue gas temperature
Interruption in process steam supply to
Tata steel network might lead to
catastrophic failure
Revised operational control procedure and reaction plan
Alternate support fuel firing during the trial period
Kept all the stakeholders informed and alert
Higher emission beyond the permissible
Statutory limit
Online monitoring of stack emission
Kept environment management department informed
Exploration for utilizations – Implementation phase
11/15/2016 TATA INNOVISTA 2016
Results and benefits
After successful trial, boiler operation with spent wash oil has been deployed in all in-house power generating stations
Energy saving 3712 Gcal/Yr
Reduction in CO2 emission1570 Ton/Yr
11/15/2016 TATA INNOVISTA 2016