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8/3/2019 DH -- Environmental Improvements in an&NA Production
1/30
IFDC NW 2011
CASE STUDY:
ENVIRONMENTAL IMPROVEMENTS IN NA&AN PRODUCTION
Nitrogen Fertilizer Production
Technology Workshop 2011, Seville
Puertollano Factory: Ammonia Plant, NA Plants and Ammonia Storage
David Herrero Fuentes
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IFDC NW 2011
Fertiberia
N
Puertollano
Location of the Factory
Introduction AN mistNH3 slip in NA-2
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Birds eye view of the facilities
1. Ammonia Plant2. Nitric Acid Plants
3. Ammonia Storage Tank
4. Ammonia Loading Station
5. Ammonium Nitrate Plant
6. Nitrate Storage Area
7. Urea Plant
8. Urea Storage Area
9. Bagging plant
10. Water tank C. I.
11. Central Offices
12. General Workshop
13. Warehouse
Introduction AN mistNH3 slip in NA-2
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Configuration and main figures
AMMONIA
PLANT
600 tpd
NITRIC
ACID
PLANTS
440 tpd
UREA
PLANT
400 tpd
AMMONIUMNITRATES
PLANT
700 tpd
NH3
CO2
LOADING
NH3
HNO3
NH3 TANKS
10.000 t
HNO3 TANKS
1.800 t
BULK STORAGE
25.000 t
Urea prill
UAN PLANT
600 tpd
ANS TANK
100 t
LOADINGA
REA
BULK STORAGE
55.000 t
AN prill
ANS
olution
Urea
Sol.
N.GAS
ELECT.
N2
Sale
WATER
AIR
NAT2.000 t
Dolomite&
Additives
Introduction AN mistNH3 slip in NA-2
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IPPC Permit
Plant Description Dust(mg/Nm3)
NH3(ppm)
Nox(mg/Nm3)
N2O(ppm)
NH3 Reforming, Aux.Boiler, Desulphuration,
Methanation, Synthesis
5 200 (C)
HNO3-1 Flue-gas 5 5(C) 200(C) 800(C)
HNO3-2 Flue-gas 5 5(C) 150(C) 300(C)
AN Prilling Tower
Dolomite grinding&transport
40
10
40
Urea Prilling Tower
Synthesis
35 20
50
Loading Bulk loading
Bagging
15/30
5
Emissions: Maximum values, main parameters
(C) : Continuous measurement. For non-continuous measurements, monthly.
* Immission in the perimeter of the factory to be lower than 75 g/m3
Waste water disposal to water body: Maximum values, main parameters, continuous measurement
Description Volume Total Nitrogen (mg N/l) pH T(C)
Centralized waste water
treatment system
2.880 m3/d < 25 6-9 < 25
Introduction AN mistNH3 slip in NA-2
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NOx SCR (Shell-CRI)
Nitric Acid Production and De-NOx system
Introduction NH3 slip in NA-2
Catalytic
Combustion
Air
NH3
NO oxidation&
NO2 absorptionNOx
NH3
NOx:
2000-4000 ppmv
V2O5
Energy
NA-2 basic diagram (M/M plant)Puertollano FactoryTost
ack
NOx:
< 150 mg/Nm3
H2
O
HNO3
380-400 tpd
Air
6NO + 4NH3 5N2 + 6H2O
6NO2 + 8NH3 7N2 + 12H2O
NO + NO2 + 2NH3 2N2 + 3H2O
4NO`+ O2 + 4NH3 4N2 + 6H2OReactions
NOx SCR transforms NOx and added NH3 into nitrogen and
water .
NH3 slip from the reactor depends on inlet NOx level, desired
outlet NOx level and on the efficiency of the system.
BAT references in Europe define a maximum emission of 5
ppmv with a NOx emission lower than 150 mg/Nm3.
AN mist
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Follow-up of Ammonia slip in NA plantsPuertollano Factory. 5s measure, daily average
0
5
10
15
20
25
30
35
40
45
50
55
60
65
70
75
18/06/2010 09/07/2010 30/07/2010 20/08/2010 10/09/2010 01/10/2010 22/10/2010 12/11/2010 03/12/2010
Date
NH3slip(ppmv)
NA-2 NA-1
NH3 slip in NA-2 was 7 times higher than best references
BAT: 5 ppmv
Average: 34 ppmv
Introduction NH3 slip in NA-2 AN mist
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Potential causes for increasing ammonia slip
Excess ammonia (only temporal)
Poor mixing of flue-gas and ammonia before the De-
NOx reactor
Deviated-from-design operating conditions (pressure,
temperature)
End of catalyst life cycle.
Bypass of the catalytic bed.
Introduction NH3 slip in NA-2 AN mist
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Preliminary Analysis
The De-NOx system was totally replaced in 2000 by CRI, worldwide reference. CRI came
several times to the plant and analyzed the causes together with Fertiberia:
Cause Analysis Decision
Poor mixing NH3 injection&mixing system was also replaced in 2000 under CRI
specification and supervision, using well-proven SULZER static mixers.
To be checked in
next turnaround
Deviations
from the
design
conditions
Parameter
Flow (Nm
3
/h)Inlet temperature (C)
Pressure (bar.a)
Inlet NOx concentration (ppm)
Design
< 50.000>220
>3,5
< 4.000
Current
< 50.000220
3,7
< 4.000
OK
Catalyst life
cycle
Catalyst is 10 years old. Estimated life cycle by the vendor is 20 years. In
2009 catalyst was checked and 25 kg (2,1%) were added due to
settlement. Samples were taken and analyzed by the vendor, showing
good activity levels.
OK
Bypass of the
catalytic bed
The internal module (squared) is placed on a plate. The plate is
supported on a ring and sealed with manganese-containing fiberglass
joints. Theses joints are fixed in place just by gravity forces and pressure
differential.
Calculation showed that only a 0,9% of gas bypass will produce an 40
ppmv increase of the ammonia slip!
To be checked in
next turnaround
Introduction NH3 slip in NA-2 AN mist
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Lateral flow reactor description
Detail of the lateral-flow module:
Installation of upper
sealing plates:
Introduction NH3 slip in NA-2 AN mist
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Reactor
wall
Supporting
ring
Supporting
plate
Original
joint
Detail of the union between
supporting plate and reactor wall:
In 2009 turnaround, actions were taken to avoid gas bypasses
Added in
2009
Mdule
(catalyst)
NOx+NH3
Perforated
plate
After 2009 turnaround, ammonia slip decreased from
40 to 20 ppmv. At the end of the next gauze
campaign emission reached 40 ppmv again.
Introduction NH3 slip in NA-2 AN mist
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If you can not beat them
500 lts of catalyst were purchased
previously to 2010 turnaround.
It was planned to cover all the lateral
areas outside the module and exposed
to rich NOx gas with a catalyst layer.
Thus, if any bypass, NH3 and NOx would
react in the presence of catalyst,cleaning the bypass gas and avoiding
tail gas contamination with NH3/NOx
Replace
ImproveCatalyst
Introduction NH3 slip in NA-2 AN mist
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December 2010 turnaround: Inspection of the NH3 injection&mixing
Ammonia injections:
Checked, OK
Static mixers:
Checked, OK
Introduction NH3 slip in NA-2 AN mist
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Inspection of the catalyst module
Height and distribution of the catalyst:
Module is opened. Catalyst in good
condition. Maximum settlement of 3 cm in
some areas without gas bypass. Somecatalyst is added. Joints are replaced. Upper
sealing plates reinstalled.
Checked, OK
Channels sealing:
After visual inspection, no leaks.
Checked, OK
Introduction NH3 slip in NA-2 AN mist
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Through the end of the cover plate
visual inspection shows no joint at all.
Joint is replaced and additional jointas planned is added, with special
care.
A new cover plate is installed, thistime with some overlapping.
Gas bypass is confirmed
Introduction NH3 slip in NA-2 AN mist
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and catalyst is added in the lateral areas between reactor and module
Introduction NH3 slip in NA-2 AN mist
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Follow-up of ammonia slip in NA-2
Puertollano Factory. 5s measure, daily average
0
5
10
15
20
25
30
35
40
45
50
55
60
65
70
75
18/06 09/07 30/07 20/08 10/09 01/10 22/10 12/11 03/12 24/12 14/01 04/02 25/02 18/03 08/04 29/04 20/05 10/06
Date
NH3slip(ppmv)
Results: better than expected, permanent almost zero emission
Average: 34 ppmv
Average: 0,4 ppmv
2010 2011
BAT: 5 ppmv
Introduction NH3 slip in NA-2 AN mist
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IFDC NW 2011
New challenges
To reduce the number and intensity of ammonia slip or
NOx excursions: Optimization of the control system.
To reduce ammonia consumption in the De-NOx based
on plant condition and legal limit (operate the plant
closer to the limit).
Installation of an advanced process control systemin the De-NOX unit of NA-2
Introduction NH3 slip in NA-2 AN mist
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The challenge: reduction of AN mist from the AN prilling tower
February 9th, 2011 16:00 hrs - Soluble AN34,5% fabrication However, when producing
LDAN this problem does not exist. The only difference: prilling temperature
Introduction NH3 slip in NA-2 AN mist
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All-purpose prilling tower
ANS consumption by product%. Year 2010. Total=166.028 t AN 100%
Soluble
AN34,5
CAN27AN33,5
LDAN
UAN32
ANS20
Hot ANS
33%
21%
3%
19%
15%
6%
2%
Prilling time distribution%. Year 2010. Total= 6.516 hours
Soluble
AN34,5
40%
25%
CAN27
AN33,5
4%
LDAN
31%
During more than 65% of the yearly operating time of the prilling tower, corresponding to 187days, mist generation is observed (AN34,5/CAN27/AN33,5). More than 55% of the ANS is
transformed into these prilled fertilizers.
Introduction NH3 slip in NA-2 AN mist
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Simplified diagram of the prilling unit
Final concentration Additives mixing Prilling&Gas Treatment
Falling-film evaporator
by hot air&steam
Inlet: 90-94% AN
(with/without additives)
Outlet: 96-99,8% AN
Mixing tank for:
- Dolomite
- Dust from screens&mill
- Additives
8 single-stage scrubbers, 2 of them
treating both prill ing tower exhaust and
air from the final evaporator.
Introduction NH3 slip in NA-2 AN mist
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Mist effect does not imply failure to comply with environmental permit
Though complying with legal limits, Fertiberia has the concern to solve out this mist
problem. Mist is generated in descending order in the following products: Soluble AN,
AN33,5 and CAN27. When prilling LDAN no mist is observed.
Emission measures are consistent with visual observation of the mist generation.
Dolomite is well washed out by the scrubbers
Ammonia emission also depends on an adequate control of ph and flow in the washing liquor.
Emission Legal Limit
(mg/Nm3)
Number of
measures (06-10)
Average
(mg/Nm3)
% over
the limit
Ammonia 40 67 28 4,5
Dust 40 300 14 1,0
Ammonia Dust
Measures
(Number)
Average
(mg/Nm3)
% Over
the Limit
Measures
(Number)
Average
(mg/Nm3)
% Over
the Limit
Sol.AN 20 29 10,0 79 25 2,5
CAN27 15 32 6,7 83 17 1,2
LDAN 32 21 0,0 138 6 0,0
Product
Emission
Introduction NH3 slip in NA-2 AN mist
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Mist generation mechanism: liquid AN vapor pressure
1. Ammonia and nitrous fumes evolve from the
liquid surface of the prill in the vicinity of the
prilling bucket. Gas release depends on the vapor
pressure of the AN at the surface of the prill.
Vapor pressure depends on the state and
temperature of the AN.
2. As gases cool down when finding cooler air, they
combine and crystallize to form AN sub-micron
crystals.
3. These crystals, due to low weight, are sucked up
by the fans. The mesh of the scrubbers is not
design to retain sub-micron particles, so crystals
are emitted, being the origin of the mist
(persistent blue-grey typical emission).
4. Gas stream from final evaporator is combined
with exhaust gases from the prilling tower before
entering the scrubbers, worsening the problem
(same mechanism)
State T(C) VP(mmHg)
Solid
38 0,015
111 0,037
129 0,126
143 0,289
160 0,958
Liquid
170 1,400
180 2,510
190 3,690
200 6,310
210 9,050
AN Vapour Pressure
Introduction NH3 slip in NA-2 AN mist
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Public references
Mist size
Ref.
Size distribution, % weigth
(particle diameter, m)
12
CAN27
(no gas
treatment)
83% 8% 1% 8%
Ref.
Size distribution, % weigth
(particle diameter, m)3
TAN 10% 40% 25% 25%
Mist: 86,2%
Mist: 68,8%
When searching for references, it was confirmed
that mist is generated by sub-micron emission.
Scrubbing system at Puertollano is not designed to
deal with those particle sizes.
Scrubbers designed for mist elimination are not an
option in the case of Puertollano, due to CAN27
operation.
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Size distribution investigation at Puertollano (in course)
0%
25%
50%
75%
100%
0 5 10 15 20
%Weigt
h
m
Introduction NH3 slip in NA-2 AN mist
Total emission by product*
* Measured in 1 out of 8 scrubbers, 4 periods of 1 hour per port, 2
ports per scrubber. Total measuring time: 8 hours per product.
Average values.
Estimated size distribution curves
Mist
Soluble AN34,5 (prilling+final concentration)
LDAN (priling + final concentration)
LDAN (only prilling)
Mist in LDAN < 25% of emission
Mist in Sol.AN34,5 > 90% of emission
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Actions in study/course/implemented
When preparing the ANS to prill:
Replace AS reactor by AS crystal after the final evaporation.
Add a desiccant (eg.magnesium sulphate) to ANS for reducing
prilling&concentration temperature while not modifying quality properties.
When prilling:
Test water sprays in the vicinity of the prilling bucket to reduce vapor pressure byfreezing prill surface.
When treating the exhaust gases:
Increase air flow (and thus the cooling rate), by refurbishing fan scrubbers.
Segregate final concentration and prilling exhaust gases. Install a dedicated
treatment system for final concentration gases.
Launch study with main engineering companies to modify/refurbish/replace the
scrubbing system by other to tackle with sub-micron emissions, taking into
consideration the presence of dolomite when prilling CAN27.
Priority
1
Introduction NH3 slip in NA-2 AN mist
Installatio
n&
OperationCosts
Prio
rity
2
Prio
rity
3
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Public references: water sprays
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Public references: desiccant addition
Prilling tower for CAN27 (no treatment). Addition of magnesium sulphate reduced mist generation, by
reducing operation temperature (final concentration outlet) from 175-180C to 155-160C
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Public references: scrubber modification
TAN prilling tower. Vertical filters for sub-micron particles were added to the scrubber.
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Is it possible to solve mist emission in a multipurpouse prilling tower?
WHY NOT?
THANK YOU!, ANY IDEAS?
Introduction NH3 slip in NA-2 AN mist