41
Well Name: Date: 4/27/15 Field: Safety Mtg: Yes AFE No: AFE Amount: WI % Purpose: Rig Contractor: Operator: Jose Pusher: Present Operation: Comp Days: Workover Days: Testing Days: Original PBTD: New PBTD: BOPD: Orig. Open Perfs: BWPD: New Perfs: MCFPD: Daily Costs: Prior Cum Cost: 3,537,230.00 $ Cum Cost: 3,544,630.00 $ Bits BOP/Rentals Cementing Coil Unit Flowback Forklift Hot Oilier Kill Truck PKR Service Pumps Reverse unit Rig 1,500.00 $ Rods Roustabout Stimulation Supervision 1,800.00 $ Downhole Tools Tech. Super. Trucking 1,800.00 $ Tbg Rentals Vacuum Trucks Well Equip. Wellhead Wireline Service/TCP WO Fluids Csg/TieBack 2,300.00 $ DAILY TOTAL 7,400.00 $ Total Load (bbls): Swab (hrs): Load to Recover: Daily Recovery (bbls Rig Supervisor: Total Recover (bbls): BO: 7,400.00 $ Daily Completion - Workover Report University 31 #1H - Greystone Oil & Gas Triple N - Devonian CB-1408 Original Completion of Well Basic Energy Clean out well 15,490' Art Linthicum Activity: Expense Breakdown: 7:00am – Crew AOL. Took delivery of 3 ½” production string and loaded out 4 ½” tie-back string (took to Deep Well for inspection). Well has 0 psi. SWI SDFN. ESP cancelled missing part of motor. Forecast: Will run 3 ½” on 4/28/2015 in the AM.

Daily Completion - Workover Report

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Page 1: Daily Completion - Workover Report

Well Name: Date: 4/27/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,537,230.00$ Cum Cost: 3,544,630.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 1,500.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools

Tech. Super.

Trucking 1,800.00$

Tbg Rentals

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Csg/TieBack 2,300.00$

DAILY TOTAL 7,400.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

7,400.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Took delivery of 3 ½” production string and loaded

out 4 ½” tie-back string (took to Deep Well for inspection). Well has 0

psi. SWI SDFN. ESP cancelled missing part of motor. Forecast: Will run

3 ½” on 4/28/2015 in the AM.

Page 2: Daily Completion - Workover Report

Well Name: Date: 4/25/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,523,930.00$ Cum Cost: 3,537,230.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools

Tech. Super. 1,200.00$

Trucking 1,500.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Csg/TieBack 2,300.00$

DAILY TOTAL 13,300.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL, well has 0 psi. ND 4 ½”, Nu BOP. RU laydown

machine and casing crew. Load and haul off workstring. PU on casing,

come out of PBR at 140K, LD 229 joints of 4 ½”. RD casing crew. SWI

SDFN.

13,300.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 3: Daily Completion - Workover Report

Well Name: Date: 4/24/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,513,830.00$ Cum Cost: 3,523,930.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools

Tech. Super. 1,200.00$

Trucking 600.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 10,100.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. POOH w/ workstring, laying down w/ bit. SWI

SDFN 5:30pm. Forecast: Will ND liner and pull.

10,100.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 4: Daily Completion - Workover Report

Well Name: Date: 4/23/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,480,730.00$ Cum Cost: 3,513,830.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 10,000.00$

Reverse unit

Rig 8,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 9,000.00$

Tech. Super. 1,200.00$

Trucking 600.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 33,100.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

33,100.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

6:00am – PU 3 ¾” milltooth.

RIH to 8000’, break circulation.

RIH to 10,990’, break circulation.

RIH to 12,000’, break circulation.

RIH, tag 13,436’, wash 60’ at a time. Circulate bottoms up, fell out at

13,600’. RIH, 10 joints at a time and circulate for 30 minutes. Well

staying at 400 psi. Tagged bottom at 15,495’, circulate for 4 hours. Lost

returns; would get them back for 20 minutes at a time. Hang kill tbg, LD

swivel. POOH, laying down workstring. Forecast: LD workstring.

Page 5: Daily Completion - Workover Report

Well Name: Date: 4/22/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,447,630.00$ Cum Cost: 3,480,730.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 10,000.00$

Reverse unit

Rig 8,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 9,000.00$

Tech. Super. 1,200.00$

Trucking 600.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 33,100.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

33,100.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

6:00am – Crew change. Wash down to 13,405’, circulate for 3 hours,

could not make more hole. Circulation pressure – 460 psi on wellhead.

Kill tbg, POOH w/ bit. Bit had marks on inside of cones. Put on 3 ¾”

overshot w/ bumper sub and oil jars. TIH to 13,405’, caught fish, came

free at 4K over. Went down 30’ past where fish was, TOH. Got out at

08:30hrs w/ mill and bit box from coil. Forecast: RIH, wash to 15,490’,

circulate clean.

Page 6: Daily Completion - Workover Report

Well Name: Date: 4/21/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,418,530.00$ Cum Cost: 3,447,630.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 10,000.00$

Reverse unit

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 9,000.00$

Tech. Super. 1,200.00$

Trucking 600.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 29,100.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

29,100.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Well has 800 psi (it was shut in w/ 450 psi);

circulate for 1 hour. RIH, picking up 20 jts at a time and breaking

circulation. Tagged @ 12,711’, washed to 12,797’, lost wellhead returns

– very little circulation. Cut soap back, blew on it for 1 ½ hours. Kill tbg,

POOH, LD motor. RIH w/ 3 7/8” mill tooth and bumper sub, oil jars and

2 3/8” workstring. Got to 10,990’, started jamming; air took 5 hours to

break circulation. Go in to 11,100’ tag high; PU swivel and wash

through. Lost circulation, blow on well for 2 ½ hours, hang swivel back.

Crew change @ 0600hrs. Forecast: Wash to bottom, 15,490’.

Page 7: Daily Completion - Workover Report

Well Name: Date: 4/20/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,387,930.00$ Cum Cost: 3,418,530.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 10,000.00$

Reverse unit

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 9,000.00$

Tech. Super. 1,200.00$

Trucking 2,100.00$

Tbg Rentals 2,500.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 30,600.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Open well – 0 psi. Move in (2) – 1350 foam air

units and a frac tank w/ gas buster. Plumb in w/ hardline; PU 3 7/8”

sealed bearing tri-cone bit w/ motor, bumper sub, oil jars. RIH w/ 2

3/8” PH6 P110 workstring to 5000’. Unload well, no fluid. RIH to

10,026’, unload 60 bbls fluid; took 3 hours to get circulation. SWI,

SDFN.

Took delivery of 4500’ of 2 3/8” P110 workstring, now have 15,500’.

Load out 2 7/8” Hydrill and release. Forecast for tomorrow: Clean well

to 15,490’.

30,600.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 8: Daily Completion - Workover Report

Well Name: Date: 4/18/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,378,830.00$ Cum Cost: 3,387,930.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 1,500.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools

Tech. Super. 1,200.00$

Trucking

Tbg Rentals 2,100.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 9,100.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

9,100.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Open well – 0 psi. Cut and LD 892' coil (made 24

cuts), LD motor (left 3 7/8” mill and motor shaft, about 3’). Shut well in,

SD. Will resume operations 4/20/2015 w/ clean-out run. Will push bit

to bottom and leave.

Page 9: Daily Completion - Workover Report

Well Name: Date: 4/17/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,361,930.00$ Cum Cost: 3,378,830.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 4,800.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 4,500.00$

Tech. Super. 1,200.00$

Trucking

Tbg Rentals 2,100.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 16,900.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

16,900.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL, well on vacuum; finish POOH. Put on overshot and

jars, RIH, latch on to fish @ 10,365’. Jar for 3 hours, making 4’; jarring

up to 140K. Fish came loose; pull out fish, dragging out. Pull up, verify

fish has 6K of weight when we got to surface. Shut well in, SD.

Prepping to cut and LD coil.

Page 10: Daily Completion - Workover Report

Well Name: Date: 4/16/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,345,630.00$ Cum Cost: 3,361,930.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 4,800.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 2,700.00$

Tech. Super. 1,200.00$

Trucking 1,200.00$

Tbg Rentals 2,100.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 16,300.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Open well – 0 psi. Unload 1000’ of 2 7/8” Hydrill.

PU 3 ¾” shoe, 992’ of 2 7/8” Hydrill. RIH, slide over fish, wash down to

11,262’. Circulation pressure at 1200 psi at 3 bpm. Wash sand and

circulate clean. Pull up 1500’, SWI and SDFN. Forecast: Will POOH to

look at shoe to see if bottomed out – if so, will RIH w/ jars and overshot

to jar fish out.

16,300.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 11: Daily Completion - Workover Report

Well Name: Date: 4/15/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,326,430.00$ Cum Cost: 3,345,630.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 6,000.00$

Tech. Super. 1,200.00$

Trucking

Tbg Rentals 1,200.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 19,200.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

19,200.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

8:00am – Crew AOL. Open well – 0 psi. TIH w/ overshot and

workstring. Latch onto fish, jar on coil for 4 hours, jarring up to 140K.

Got off of fish, POOH, no damage done to grapple. SWI, SDFN. Forecast

for tomorrow: Will PU 2 7/8” CS Hydril and wash over coil.

Page 12: Daily Completion - Workover Report

Well Name: Date: 4/14/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,307,230.00$ Cum Cost: 3,326,430.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 6,000.00$

Tech. Super. 1,200.00$

Trucking

Tbg Rentals 1,200.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 19,200.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

19,200.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Open well – 0 psi. PU 3 ¾” shoe and 3 jts of wash

pipe. RIH, tag up at 10,365’. Wash 60’ of sand and plug parts, circulate

clean. Hang swivel back, POOH. Pick up: overshot w/ new grapple, 4’

extension, jars, collars w/ bumper sub, 6 collars w/ accelerator. SWI,

SDFN. Forecast for tomorrow: RIH and latch on and attempt to jar free.

Page 13: Daily Completion - Workover Report

Well Name: Date: 4/13/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,288,030.00$ Cum Cost: 3,307,230.00$

Bits

BOP/Rentals

Cementing

Coil Unit

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit 2,500.00$

Rig 4,000.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 6,000.00$

Tech. Super. 1,200.00$

Trucking

Tbg Rentals 1,200.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 19,200.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Open well, no pressure. Finish RIH, got down to

fish, PU swivel. Wash down 6’, full circulation. Latch onto fish, hang

back swivel, started jarring at 100K working up to 120K. Fish pulled off

after jarring for 2 ½ hours. Made 12’, coil still stuck. POOH w/ grapple.

Shut well in, SDFN. Forecast for tomorrow: PU 100’ wash pipe, make

wash run before latching back on.

19,200.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 14: Daily Completion - Workover Report

Well Name: Date: 4/12/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,267,280.00$ Cum Cost: 3,288,030.00$

Bits

BOP/Rentals 600.00$

Cementing

Coil Unit

Flowback 2,500.00$

Forklift 700.00$

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 3,800.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 9,150.00$

Tech. Super.

Trucking 1,000.00$

Tbg Rentals 1,200.00$

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane

Frac Tanks

DAILY TOTAL 20,750.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

7:00am – Pipe on location. Unload and tally 2 3/8” P110 (351 jts). NU

BOP, PU fishing tools: 3 7/8” overshot w/ 2” grapple, 3 1/8” bumper

sub, 3 1/8” hydro jars, 6 – 3 1/8” DCs, 3 1/8” energizer sub, 268 jts 2

3/8” P110. Got in w/ 8559’, shut well in at 6:30pm. Forecast for

tomorrow: Tag up, break circulation, wash down to fish, latch on and

jar free.

20,750.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 15: Daily Completion - Workover Report

Well Name: Date: 4/11/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,200,330.00$ Cum Cost: 3,267,280.00$

Bits

BOP/Rentals

Cementing

Coil Unit 30,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 2,500.00$

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 2,500.00$

Tech. Super. 3,500.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip. 650.00$

Wellhead

Wireline Service/TCP 18,000.00$

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 66,950.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

66,950.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

7:00am – Pick up on coil w/ crane to 40K. Went to NU injector head

and coil dropped out of chains. Top of fish at ground level; get overshot

and 10’ x 2 3/8” sub. Fished coil out w/ crane. Held fish w/ BOP slips,

put on coil connector w/ TIW valve. Made gauge ring run to 10,400’,

POOH. Put on cutter 1.35. RIH, pumped 25 bbls down coil, cut coil.

POOH, RD wireline, latch onto coil w/ crank, only pull 40K and no

movement. Call out rig and rig mats; RU well service unit, latch on, pull

up to 80K and coil pulling free. Sand packed off around cut, LD 30’ coil.

Pulling free at 65K. NU injector head, tie-back to release. Pull out 130’,

pulled free. POOH w/ 10,375’ of coil. Inspected cut on fish – CLEAN.

RD coil unit. Shut well in, shut down 2:30am. Forecast for tomorrow:

PU work string w/ overshot and jars to work fish free.

Page 16: Daily Completion - Workover Report

Well Name: Date: 4/10/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,121,530.00$ Cum Cost: 3,200,330.00$

Bits

BOP/Rentals

Cementing

Coil Unit 61,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 8,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 78,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

78,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

6:00am – Pumping N2 at 2800 mcf, no pressure build up on casing.

Working coil up to 87K and snubbing down to 40K. Coil parted at

surface; ND coil, PU on coil. Clamped off, broke BOP down and NU over

part. Secure well and line up wireline service to cut coil, put on coil

connector, NU TIW. Shut well in, SDFN. Forecast for tomorrow: Cut

coil at 10,375’.

Page 17: Daily Completion - Workover Report

Well Name: Date: 4/9/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 3,048,730.00$ Cum Cost: 3,121,530.00$

Bits

BOP/Rentals

Cementing

Coil Unit 48,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 72,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

72,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

6:00am – Well shut in. N2 unit down. Parts are being flown in from

Houston. 6:30pm – N2 came back online. Pumping 2800 mcf;

circulation pressure 3350 psi, wellhead built up to 93 psi. 12:30am –

Started working coil down -30K to max pull of 87K – no movement.

Circulation pressure 3350 psi, no change and wellhead 0 psi. Well not

charging. Undress pack-off, work coil several more times, no

movement. (Greystone) to prep an AFE for cutting coil and fishing tools

and coil out from depth of 11,498’.

Page 18: Daily Completion - Workover Report

Well Name: Date: 4/8/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,958,430.00$ Cum Cost: 3,048,730.00$

Bits

BOP/Rentals

Cementing

Coil Unit 65,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,500.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 90,300.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

6:00am – Pumping N2 at 2800 mcf and fluid at rollover w/ foamer down

coil. 4:00pm – Started to circulate around 1 bbl out while pumping 4.5

bbls in. Moved coil to 11,498’, lost circulation again, shut casing in.

Continue to pump and work coil through the night, no movement, no

circulation. N2 pump went down at 5:45am. Well shut in. Waiting on

change out of pump. Prep to continue to try and work free. Circulation

pressure has been running around 5300 on coil

90,300.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 19: Daily Completion - Workover Report

Well Name: Date: 4/7/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,871,630.00$ Cum Cost: 2,958,430.00$

Bits

BOP/Rentals

Cementing

Coil Unit 62,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 86,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

6:00am – Charging on well, worked free. 2:30pm – Come up from

12,770’ to 11,505’; lost wellhead pressure again, went back to charging

well w/ 2400 psi on casing. Pumping down coil w/ 0.75 bpm fluid and

1200 mcf N2. Worked pipe several times, well still not charging. Have

not made any more hole. At midnight, dropped ball going straight

through circulation. Sub fluid w/ straight N2, 2200 mcf. Pumped 520

bbls fluid while stuck at 11,505’. Was pumping 0.25 gallons foamer per

10 bbls fluid. At 6:00am, still charging well. Prep to work coil free, then

POOH.

86,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 20: Daily Completion - Workover Report

Well Name: Date: 4/6/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,788,830.00$ Cum Cost: 2,871,630.00$

Bits

BOP/Rentals

Cementing

Coil Unit 58,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 82,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

6:00am – RIH w/ coil. Well has 100 psi, wellhead pumping 600 mcf N2

and ¾ bpm fluid. Got to curve, picked up N2 rate to 1000 mcf. Tag sand

at 13,211’; wash 100’ at a time. Pull 100, got through, went down,

tagged plug #4 @ 14,571’, short trip. Got sticky at 11,300’, lost

wellhead; recharge well to 2100 psi. POOH to 9700’. RIH, holding 500

psi on wellhead, tag plug #4 @ 14,571’, plug #3 @ 14,097’, plug #2 @

15,042’ and plug #1 @ 15,277’. Wellhead 480 psi, pumping 5 bbls

sweeps 100 vis. Tag bottom @ 15,490’, well drilled out. POOH, got to

13,200’, wellhead went to 0 psi, lost circulation. Pulled to 12,220’, got

tight. Stopped and started recharging well from 2:00am. At 6:00am still

charging. Pulled to 10K over and stacked down trying to snub, no

progress. Still charging. Prep to get coil free, POOH, then RDMO.

82,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 21: Daily Completion - Workover Report

Well Name: Date: 4/2/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,713,030.00$ Cum Cost: 2,788,830.00$

Bits

BOP/Rentals

Cementing

Coil Unit 51,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 75,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

75,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Art Linthicum

Activity: Expense Breakdown:

5:00am – Moved coil 200’, lock down again. Charge up 2500 psi on

casing. Pump-down coil until well charged up. Open casing through gut

line, pull up 80K and coil pulled free. POOH w/ coil, change bit nipple,

clean out plug catcher. Ready to run back in and finish last 4 plugs first

thing in the AM on 04/06/15. Shut well in shut down 7:30pm.

Page 22: Daily Completion - Workover Report

Well Name: Date: 4/1/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,639,730.00$ Cum Cost: 2,713,030.00$

Bits

BOP/Rentals

Cementing

Coil Unit 51,000.00$

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 73,300.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Art Linthicum

Activity: Expense Breakdown:

5:00am – Finish POOH; no cutting in basket. Put on bit, RIH, tag plug #8

@ 13,604’, plug #7 @ 13,838’ and plug #6 @ 14,084’. Circulation

pressure on wellhead 245 psi. Pumping 1 bbl, 1000 N2. Tag plug #5 @

14,328’. Pumping 5 bbls sweeps; drill out plug #5 and well goes on

vacuum. POOH to short trip to 13,337’, still no circulation. Started

getting sticky; shut down, start to charge well. On casing pumping 1200

N2 @ 2000 psi; back on coil, pumping 0.75 fluid 1000 N2. Drag up hole

to 13,100’ pulling 65K to 80K. Recharge well, start trying to work free.

Moved a couple of feet, let coil set. Pumping down coil to charge up

well. Will continue to try and work free and drill out remaining 4 plugs

in the AM. Well shut in to charge.

73,300.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Clean out well

15,490'

Page 23: Daily Completion - Workover Report

Well Name: Date: 3/31/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,563,930.00$ Cum Cost: 2,639,730.00$

Bits

BOP/Rentals

Cementing

Coil Unit 51,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 75,800.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

75,800.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RD Frac Equipment / Move off location

15,490'

Art Linthicum

Activity: Expense Breakdown:

5:00am – Charging well up, 30 psi on casing. Switch off coil, pump

down casing w/ N2. Pressure up to 2400 psi, book back to coil, started

pumping 0.75 fluid and 1200 N2. Work coil at negative 20K and pull to

85K. Rip casing open to pit while working coil; continue same steps.

7:30pm – Coil came free, circulate @ 280 psi, send 2 sweeps at 5 bbls

each and 110 vis. POOH, change out motor, put on Venturi basket. First

run, tag @ 13,365’. Come out w/ 0.25 full basket. RIH again, set down

mill down 4’ of basket cavity. POOH. Prep to drill out remaining 9

plugs.

Page 24: Daily Completion - Workover Report

Well Name: Date: 3/30/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,482,630.00$ Cum Cost: 2,563,930.00$

Bits

BOP/Rentals 3,500.00$

Cementing

Coil Unit 51,000.00$

Flowback 2,500.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Downhole Tools 15,000.00$

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks 2,000.00$

Well Equip.

Wellhead

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks

DAILY TOTAL 81,300.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

81,300.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RD Frac Equipment / Move off location

15,490'

Art Linthicum

Activity: Expense Breakdown:

5:00am – Open well, RIH w/ coil tbg @ 5000’. Start N2 @ 1.5 fluid and

600 N2. Tag plug #1 @ 11,261, plug #2 @ 11,497’, plug #3 @ 11,728’.

Short trip to wellhead, 70 psi sweeps. Pumped 5 bbls w/ 5 bbls spacer,

110 visc. Plug #4 @ 11,966’, #5 @ 12,174’, 6 @ 12,296’. Short trip, tag

plug #7 @ 12,451’, plug #8 @ 12,690’, plug #9 @ 12,927, plug #10 @

13,178’. Tag #11 @ 13,400’, do not drill, short trip. Wellhead 45 to 75

psi, pumping 1 bbls fluid, 1000 N2. Pulled to 12,305’, well goes on

vacuum. 10:00pm – Coil stuck. Work coil until 1:00am. Max pulled,

used 75K snub down, max 20K. Made 10’. No circulation. 5:00am –

Start at 1200 and fluid 0.75. Still charging wellbore. Wellhead 30 psi,

casing still shut. Prep to continue charging well to work coil free.

Page 25: Daily Completion - Workover Report

Well Name: Date: 3/29/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,467,580.00$ Cum Cost: 2,482,630.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,800.00$

Tbg Testing

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

DAILY TOTAL 15,050.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

15,050.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RD Frac Equipment / Move off location

15,490'

Bob Dimit

Activity: Expense Breakdown:

MIRU coiled tbg and clean-out tools.

Page 26: Daily Completion - Workover Report

Well Name: Date: 3/28/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 2,452,830.00$ Cum Cost: 2,467,580.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

DAILY TOTAL 14,750.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

14,750.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RD Frac Equipment / Move off location

15,490'

Bob Dimit

Activity: Expense Breakdown:

Move frac equipment off location.

Page 27: Daily Completion - Workover Report

Well Name: Date: 3/27/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 1,920,140.00$ Cum Cost: 2,452,830.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 1,950.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP 18,600.00$

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

Pressure Control 15,860.00$

Frac Pumping (4 Stages) 406,955.00$

Frac Plugs 6,945.00$

Water (12,546 bbls) 8,785.00$

Acid/Chems 54,845.00$

DAILY TOTAL 532,690.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

532,690.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Pump Stages 15 - 18

15,490'

Perf Stage #16 11,851', 11,771', 11,691, Stage #17 11,611',

11,531', 11,458', Stage #18 11,373', 11,291', 11,211'

Bob Dimit

Activity: Expense Breakdown:

Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500

psi.

Pumped Stage #15 with 4,200 gal 15% HCl, 122,262 gal linear & cross-

linked gel, 151,538# of 20/40 RC sand @ 60 BPM. Set Magnum Snub

Nose flow-thru plug at 11,891'. Perforated Devonian @ 11,851',

11,771', 11,691' with 19 shots (.35" holes). Pressure tested lines. Drop

frac plug ball ahead of acid.

Pumped Stage #16 with 3,990 gal 15% HCl, 120,162 gal linear & cross-

linked gel, 148,225# of 20/40 RC sand @ 60 BPM. Set frac plug at

11,651'. Perforated @ 11,611', 11,531', 11,458'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #17 with 3,822 gal 15% HCl, 118,860 gal linear & cross-

linked gel, 145,413# of 20/40 RC sand @ 60 BPM. Set frac plug at

11,417'. Perforated @ 11,373', 11,291', 11,211'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #18 with 3,990 gal 15% HCl, 125,390 gal linear & cross-

linked gel, 144,215# of 20/40 RC sand @ 60 BPM. Job Complete

Page 28: Daily Completion - Workover Report

Well Name: Date: 3/26/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 1,543,535.00$ Cum Cost: 1,920,140.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 1,950.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP 18,600.00$

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

Pressure Control 18,860.00$

Frac Pumping (3 Stages) 305,220.00$

Frac Plugs 6,945.00$

Water (12,546 bbls) 6,280.00$

DAILY TOTAL 376,605.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

376,605.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Pump Stages 12 - 14

15,490'

Perf Stage #13 12,569', 12,495', 12,411, Stage #14 12,331',

12,251', 12,171', Stage #15 12,091', 12,008', 11,934'

Bob Dimit

Activity: Expense Breakdown:

Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500

psi.

Pumped Stage #12 with 5,208 gal 15% HCl, 117,684 gal linear & cross-

linked gel, 141,088# of 20/40 RC sand @ 60 BPM. Set Magnum Snub

Nose flow-thru plug at 12,611'. Perforated Devonian @ 12,569',

12,495', 12,411' with 19 shots (.35" holes). Pressure tested lines. Drop

frac plug ball ahead of acid.

Pumped Stage #13 with 3,822 gal 15% HCl, 119,826 gal linear & cross-

linked gel, 141,201# of 20/40 RC sand @ 60 BPM. Set frac plug at

12,371'. Perforated @ 12,331', 12,251', 12,171'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #14 with 4,074 gal 15% HCl, 116,886 gal linear & cross-

linked gel, 149,321# of 20/40 RC sand @ 60 BPM. Set frac plug at

12,131'. Perforated @ 12,091', 12,008', 11,934'. SDFN.

Page 29: Daily Completion - Workover Report

Well Name: Date: 3/25/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 1,056,978.00$ Cum Cost: 1,543,535.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 1,950.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP 24,800.00$

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

Pressure Control 16,060.00$

Frac Pumping (4 Stages) 406,952.00$

Frac Plugs 9,260.00$

Water (12,546 bbls) 8,785.00$

DAILY TOTAL 486,557.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

486,557.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Pump Stages 8 - 11

15,490'

Perf Stage #9 13,531', 13,451', 13,371, Stage #10 13,291',

13,211', 13,137', Stage #11 13,053', 12,971', 12,891', Stage # 12

12,811', 12,731, 12,651

Bob Dimit

Activity: Expense Breakdown:

Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500

psi.

Pumped Stage #8 with 3,780 gal 15% HCl, 111,342 gal linear & cross-

linked gel, 92,200# of 20/40 RC sand @ 60 BPM. Set Magnum Snub

Nose flow-thru plug at 13,571'. Perforated Devonian @ 13,531',

13,451', 13,371' with 19 shots (.35" holes). Pressure tested lines. Drop

frac plug ball ahead of acid.

Pumped Stage #9 with 4,620 gal 15% HCl, 125,370 gal linear & cross-

linked gel, 141,576# of 20/40 RC sand @ 60 BPM. Set frac plug at

13,331'. Perforated @ 13,291', 13,211', 13,137'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #10 with 4,536 gal 15% HCl, 126,252 gal linear & cross-

linked gel, 148,889# of 20/40 RC sand @ 60 BPM. Set frac plug at

13,098'. Perforated @ 13,053', 12,971', 12,891'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #11 with 4,200 gal 15% HCl, 119,994 gal linear & cross-

linked gel, 141,499# of 20/40 RC sand @ 60 BPM. Set frac plug at

12,851'. Perforated @ 12,811', 12,731', 12,651' SDFN.

Page 30: Daily Completion - Workover Report

Well Name: Date: 3/24/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 562,724.00$ Cum Cost: 1,056,978.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 9,547.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP 24,800.00$

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

Pressure Control 16,140.00$

Frac Pumping (4 Stages) 406,952.00$

Frac Plugs 9,260.00$

Water (12,575 bbls) 8,805.00$

DAILY TOTAL 494,254.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

494,254.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Pump Stages 5 - 7

15,490'

Perf Stage #5 14,491', 14,411', 14,325, Stage #6

14,251',14,171',14,091', Stage #7 14,011', 13,931', 13,851',

Stage # 8 13,766', 13,691, 13,611

Bob Dimit

Activity: Expense Breakdown:

Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500

psi.

Pumped Stage #4 with 3,990 gal 15% HCl, 120,876 gal linear & cross-

linked gel, 143,638# of 20/40 RC sand @ 60 BPM. Set Magnum Snub

Nose flow-thru plug at 14,531'. Perforated Devonian @ 14,491',

14,411', 14,325' with 19 shots (.35" holes). Pressure tested lines. Drop

frac plug ball ahead of acid.

Pumped Stage #5 with 4,116 gal 15% HCl, 142,800 gal linear & cross-

linked gel, 141,987# of 20/40 RC sand @ 60 BPM. Set frac plug at

14,295'. Perforated @ 14,971', 14,896', 14,811'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #6 with 4,242 gal 15% HCl, 130,116 gal linear & cross-

linked gel, 140,403# of 20/40 RC sand @ 60 BPM. Set frac plug at

14,051'. Perforated @ 14,011', 13,931', 13,851'. Pressure tested lines.

Drop frac plug ball ahead of acid.

Pumped Stage #7 with 4,116 gal 15% HCl, 120,078 gal linear & cross-

linked gel, 139,726# of 20/40 RC sand @ 60 BPM. Set frac plug at

13,806'. Perforated @ 13,766', 13,691', 13,611' SDFN.

Page 31: Daily Completion - Workover Report

Well Name: Date: 3/23/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 187,674.00$ Cum Cost: 562,724.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 1,950.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP 18,600.00$

WO Fluids

Crane 5,500.00$

Frac Tanks 450.00$

Pressure Control 15,800.00$

Frac Pumping (3 Stages) 305,220.00$

Frac Plugs 6,945.00$

Water (11,119 bbls) 7,785.00$

DAILY TOTAL 375,050.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

375,050.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Pump Stages 1 - 3

15,490'

Stage #2 15,211',15,131',15,051', Stage #3 14,971', 14,896',

14,811', Stage # 4 14,731', 14,651', 14,571'

Bob Dimit

Activity: Expense Breakdown:

Pressure tested lines to 9483 psi. Pressured 4 ½” – 7” annulus to 2500

psi.

Pumped Stage #1: 630 gal 15% HCl, 153,888 gal linear & cross-linked

gel, 183,966# of 20/40 RC sand @ 60 BPM. Set Magnum Snub Nose

flow-thru plug at 15,251'. Perforated Devonian @ 15,211', 15,131',

15,051' with 19 shots (.35" holes). Pressure tested lines. Drop frac plug

ball ahead of acid.

Pumped Stage #2: 6,720 gal 15% HCl, 142,800 gal linear & cross-linked

gel, 141,987# of 20/40 RC sand @ 64BPM. Set frac plug at 15,011'.

Perforated @ 14,971', 14,896', 14,811'. Pressure tested lines. Drop frac

plug ball ahead of acid.

Pumped Stage #3: 5,460 gal 15% HCl, 161,379 gal linear & cross-linked

gel, 131,712# of 20/40 RC sand @ 64 BPM. Set frac plug at 14,771'.

Perforated @ 14,731', 14,651', 14,571'. Pressure tested lines. SDFN

Page 32: Daily Completion - Workover Report

Well Name: Date: 3/22/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 148,474.00$ Cum Cost: 187,674.00$

Bits

BOP/Rentals 2,500.00$

Cementing

Coil Unit

Flowback 1,800.00$

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumps 4,000.00$

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super. 1,950.00$

Trucking

Tbg 3 Days

Vacuum Trucks

Well Equip.

Wellhead 3,000.00$

Wireline Service/TCP

WO Fluids

Pick Up Machine

Sfc Rentals 5,500.00$

Frac Tanks 2,700.00$

Pressure Control 16,250.00$

DAILY TOTAL 39,200.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Jody Linthicum

Activity: Expense Breakdown:

Move in frac stack, crane, wireline, pump-down, flowback, lights/lifts

and sanitation. RU and ready for frac.

39,200.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Prep for Frac

15,490'

15,441' , 15,366', 15,291'

Page 33: Daily Completion - Workover Report

Well Name: Date: 3/12/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 137,304.00$ Cum Cost: 148,474.00$

Bits

BOP/Rentals 1,500.00$

Cementing

Coil Unit

Flowback

Forklift 750.00$

Hot Oilier

Kill Truck

PKR Service

Pumps

Reverse unit

Rig 3,000.00$

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking 1,500.00$

Tbg 3 Days 1,920.00$

Vacuum Trucks

Well Equip.

Wellhead 1,000.00$

Wireline Service/TCP

WO Fluids

Pick Up Machine

DAILY TOTAL 11,170.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

11,170.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RU coil tubing unit / Toe Prep

15,490'

15,441' , 15,366', 15,291'

Jody Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. Well on slight vacuum. Release hanger and POOH,

laying down tbg. POOH w/ gauges and contact Precision Pressure Data

to pick up. ND BOP, NU master valve, RD and release rentals and move

off. Will have remainder of frac stack NU and move in support rentals

on 3/21/2015.

-------Standby for Frac Date---------------

Page 34: Daily Completion - Workover Report

Well Name: Date: 3/9/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 121,940.00$ Cum Cost: 137,304.00$

Bits

BOP/Rentals 500.00$

Cementing

Coil Unit

Flowback

Forklift 750.00$

Hot Oilier

Kill Truck

PKR Service

Pumps 4,064.00$

Reverse unit

Rig 3,000.00$

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking 1,000.00$

Tbg Rental/Day 640.00$

Vacuum Trucks

Well Equip.

Wellhead 1,000.00$

Wireline Service/TCP

WO FluidsPick Up/Lay Down

Machine 2,910.00$

DAILY TOTAL 15,364.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Jody Linthicum

Activity: Expense Breakdown:

7:00am – Crew AOL. RU, rack 335 jts 2 3/8” L80 rental. ND master valve

and NU BOP. PU SN w/ 2 3/8” x 6’ perforated gauge carrier and tally in.

TIH w/ 331 jts, PU hanger and land tbg @ 10,593'. RU pump, load w/ 37

bbls, shut in tbg and establish rate of 8 bpm @ 3630 psi.

25 bbls in, 8 bpm @ 3650 psi

50 bbls in, 7.75 bpm @ 3800 psi

71 bbls in, 7.6 bpm @ 3900 psi and SD

ISIP – 1300 psi / 5 minutes – 475 psi / 8 minutes – 0 psi

Shut in and RD pump. Will POOH w/ gauges on 3/12/2015. Basic

elected to leave rig over hole w/ no standby charges. SISDFTD 5:30pm.

15,364.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RU coil tubing unit / Toe Prep

15,490'

15,441' , 15,366', 15,291'

Page 35: Daily Completion - Workover Report

Well Name: Date: 3/8/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 42,365.00$ Cum Cost: 121,940.00$

Bits

BOP/Rentals

CementingCoil Unit w/ Chemical

& Mixing Plant 40,000.00$

Flowback

Forklift

Hot Oilier

Kill Truck

PKR Service

Pumping Unit

Reverse unit

Rig

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking

Tubing

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service/TCP 11,942.00$

WO Fluids

Acid/Chems 12,085.00$

Motor w/ Mill 14,048.00$

DAILY TOTAL 79,575.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Jody Linthicum

Activity: Expense Breakdown:

5:00am – Move in coil tubing unit/mixing plant, RU. PU motor w/ 3 7/8”

mill; test motor, NU, test stack to 10K and casing to 6K, RIH. Baker TCP

and acid on location. Tag 15,490' w/ mill, send sweep, drop ball and lay

71 bbls of 15% Acetic acid in lateral. POOH to 9500', pump soda ash

through coil and chase sweep out of hole. LD motor/mill, PU guns and

RIH to 15,490'. Perforate:

7 shots/6spf/60deg/.35 entry hole diameter (ehd) @ 15,441'

6 shots/6spf/.35ehd @ 15,366'

6 shots/6spf/.35ehd @ 15,291'

POOH to 9500’. Establish rate through coil of 5 bpm @ 3600 psi, pump

29 bbls, SD. Pressure @ 0 psi and resume POOH. POOH w/ guns, all

shots fired. Start RDMO at 10:00pm. Will move in rig, tbg and gauges

for DFIT in the AM.

79,575.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

RU coil tubing unit / Toe Prep

Page 36: Daily Completion - Workover Report

Well Name: Date: 3/7/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: 6,250.00$ Cum Cost: 42,365.00$

Bits

BOP/Rentals 1,000.00$

Cementing

Coil Unit

Flowback

Forklift

Hot Oilier

Kill Truck 500.00$

PKR Service

Pumping Unit

Reverse unit

Rig 4,200.00$

Rods

Roustabout 500.00$

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking 500.00$

Tubing

Vacuum Trucks 1,600.00$

Well Equip.

Wellhead 7,500.00$

Wireline Service

WO Fluids

Csg/TieBack 6,015.00$

Torque Turn 5,750.00$

Casing Crew 7,050.00$

DAILY TOTAL 36,115.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Jody Linthicum

Activity: Expense Breakdown:

7:00am – Crews AOL. RU casing equipment, PU seal assembly, set

torque turn and tally in w/ csg. Seat seals, test to 2000 psi. Pull seal,

sub out and land hanger w/ 90K compression. ND BOP, NU tbg head

and master valve. Test annulus to 2000 psi, RD casing crews and

release. RD pulling unit, move off and ready for CTU toe prep in the

AM. SISDFTD 10:00pm

36,115.00$

Daily Completion - Workover Report

University 31 #1H - Greystone Oil & Gas

Triple N - Devonian

CB-1408

Original Completion of Well

Basic Energy

Rig to run Casing

Page 37: Daily Completion - Workover Report

Well Name: Date: 3/6/15

Field: Safety Mtg: Yes

AFE No: AFE Amount: WI %

Purpose:

Rig Contractor: Operator: Jose Pusher:

Present Operation:

Comp Days: Workover Days: Testing Days:

Original PBTD: New PBTD: BOPD:

Orig. Open Perfs: BWPD:

New Perfs: MCFPD:

Daily Costs: Prior Cum Cost: -$ Cum Cost: 6,250.00$

Bits

BOP/Rentals 1,000.00$

Cementing

Coil Unit

Flowback

Forklift 750.00$

Hot Oilier

Kill Truck

PKR Service

Pumping Unit

Reverse unit

Rig 1,000.00$

Rods

Roustabout

Stimulation

Supervision 1,500.00$

Tbg Testing

Tech. Super.

Trucking 2,000.00$

Tubing

Vacuum Trucks

Well Equip.

Wellhead

Wireline Service

WO Fluids

Workstring

Rentals Surface

Safety Anchors

DAILY TOTAL 6,250.00$

Total Load (bbls): Swab (hrs):

Load to Recover: Daily Recovery (bbls):

Rig Supervisor: Total Recover (bbls):

BO:

Daily Completion - Workover Report

Original Completion of Well

Basic Energy

6,250.00$

Expense Breakdown:Activity:

University 31 #1H - Greystone Oil & Gas

CB-1408

Triple N - Devonian

10:00am – Move in rig, racks/mats, BOP and RU. Also, set light plants

and rack 231 jts 4 ½” 11.6# P110 LTC. Will move in Baker seal assembly,

subs, casing crew and pick-up machine in the AM. SDFTD 2:00pm

MIRU

Jody Linthicum

Page 38: Daily Completion - Workover Report

Fail Date AFE #: CB-1408

Start Date 3/6/2015 AFE $:

End Date Foreman: Jody Linthicum

Service Co. Basic Energy Bob Dimit

Use Drop Down: Art Linthicum

WS Reason

Type of Failure

Cause of Failure 1

Cause of Failure 2

Failed Item

Failed Part

Type In Data:

Size/Grade

Brand

Coating

Area Failed

Failure Depth

Description

Well Service Report

Original Completion of Well

Orig Completion

Page 39: Daily Completion - Workover Report

fluid type fluid type fluid type fluid type Proppant Name Proppant Name

Show amount

used in barrels

Gallons -

Autocalculated

Show amount

used in barrels

Gallons -

Autocalculated

Show amount

used in lbs

Show amount

used in lbs

1 0 0 0 - 676

2 0 0 0 - 608

3 0 0 0 - 582

4 0 0 0 - 523

5 0 0 0 - 320

6 0 0 0 -

7 0 0 0 -

8 0 0 0 -

9 0 0 0 -

10 0 0 0 -

11 0 0 0 -

12 0 0 0 -

13 0 0 0 -

14 0 0 0 -

Avg.

Rate

(bpm)

Stage # Formation NamePerfs - Each Interval /

Display in feet

Plug Set

depth /

Display

depth in

feet

Openin

g WHP

(psi)

Break

Down

(psi)

ISIP

(psi)

15 Min.

SIP

(psi)

Max

Press

(psi)

Avg.

Press

(psi)

Max

Rate

(bpm)

Break

Rate

(bpm)

FG

psi/ft

Total Acid

(bbls)

Total Acid

(gallons -

autocalc)

Propp

.

Concn

. Min

(ppg)

Propp

.

Concn

. Max

(ppg)

TOTAL Load to

Recover (bbls)10# Linear 10# Linear 20# Xlinked 20# Xlinked

20/40

Ottowa

20/40 Super

LCTotal Proppant

(lbs - autocalc)

Page 40: Daily Completion - Workover Report

15 0 0 0 -

16 0 0 0 -

17 0 0 0 -

18 0 0 0 -

19 0 0 0 -

20 0 0 0 -

21 0 0 0 -

22 0 0 0 -

0 0 0 2,709

Page 41: Daily Completion - Workover Report

Tally Length Depth

Tally Length Depth

Tally Length DepthCasing Tally

Rod Description

Tubing Description