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Booster Cogging:Synchronization with the Main Injector
for NuMI & Slip-Stacking
Robert Zwaska
University of Texas at Austin
Budker SeminarJuly 27, 2004
July 27, 2004 Robert ZwaskaBooster Cogging
2
IntroductionMyself
• Graduate Student at the University of Texas Sine 1999
• NuMI/MINOS Since 2000
• Booster Group Since 2003
• Fermi Ph.D. program Since 2003 or 2004
People Involved• Sacha Kopp
Advisor in Texas
• Eric Prebys Supervisor at FNAL
• Bill Pellico Cogger at FNAL
• Bob Webber Earlier Cogger
• Rich Meadowcraft, Todd Sullivan, Andrew Feld, Jim Lackey, Alberto Marchionni, Alex Waller, Craig Drennan Have helped out
July 27, 2004 Robert ZwaskaBooster Cogging
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OutlineI. Motivation
i. Multi-Batch Operation
ii. Booster Losses
II. Notching the Booster BeamI. Extracting with the Notch
III. Sources of Slippage
IV. Cogging Method
V. Examples of Issues Encountered
July 27, 2004 Robert ZwaskaBooster Cogging
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The Fermilab Booster• Multiple-turn injection of H- ions
Carbon stripping foil Typically 12-14 turns
• Accelerates 400 MeV 8 GeV• Fast cycling synchrotron
Resonant magnet ramp Frequency of 15 Hz locked with wall-
socket• Circumference of 474 m• Beam bunched at 37 MHz
Harmonic number = 84 53 MHz at extraction
• 18 RF Stations 0.9 MV• Accelerates in 33 ms
T = 5.45• 5-6 x 1012 protons/pulse
80 – 90 % efficient• Single turn extraction
Two extraction regions
Injection
Extraction to Main Injector /
MiniBooNE
Extraction to Beam Dump
The Main Injector• Accepts 8 GeV protons from the Booster• Accelerates to 120 GeV
Uses 53 MHz from the Booster 4 MV of RF power
• Circumference of 3319 M 7 x the length of the Booster
July 27, 2004 Robert ZwaskaBooster Cogging
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NuMI/MINOS
• Long-Baseline experiment Neutrino oscillations measurements 735 km
• Uses 120 GeV protons from the Main Injector
• Designed for 400 kW ave. power Will be closer to 250 kW as start
• Seriously statistics limited Initially needs 8 x 1020 protons
• Will start December 2004
Neutrinos at the Main InjectorMain Injector Neutrino Oscillation SearchN
eutrino beam
July 27, 2004 Robert ZwaskaBooster Cogging
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Slip-Stacking• Combines two Booster
batches longitudinally In the Main Injector
• To be used, initially, for antiproton production Part of Run II Upgrades
Tim
e
Longitudinal Position
July 27, 2004 Robert ZwaskaBooster Cogging
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Multi-Batch Operation
Batch 1 (PBar)
Batch 2
Batch 3
Batch 4
Batch 5
Batch 6
Booster
Main Injector
½ Batch(empty) ½ Batch
(empty)
• Two beams must be accelerated together in the Main Injector Extracted to PBar & NuMI
• Requires “multi-batch” operation 6 batches from the Booster
NuMI
July 27, 2004 Robert ZwaskaBooster Cogging
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Radiation Issues
• Radiation is the operational limit on Booster operation Limits integrated number of protons
• Residual activation in the tunnel Radioisotopes created by showers Long lived isotopes limit how much
maintenance can be done in the tunnel
• Damage of beam components• Prompt radiation from the
showering of lost protons Radiation scales with energy and
number of protons lost Very small amount penetrates the
shielding
July 27, 2004 Robert ZwaskaBooster Cogging
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Extraction Need for a Notch• Extraction kicker magnet has a
risetime of ~ 40 ns Only ~ 10 ns between bunches
• Beam lost at 8 GeV Lost on septum magnet at extraction Intolerable for extended operation
• Instead, beam is removed at 400 MeV Create a “notch” in the beam Activation scales, roughly, with beam
energy lost• Loss reduced by 95% (from this
source) Position of losses can be chosen as a
non-critical area• Extraction kicker firing must be
synchronized with the notch Easy with one batch…
84 RF bucketsaround circumference
Notch
Booster
July 27, 2004 Robert ZwaskaBooster Cogging
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Notching• Induce a large vertical betatron
oscillation• Uses a kicker magnet• Displacement goes as:
y ~ 90o / period• Most of the beam is deposited in
the third magnet• Kick must be large enough to
scrape off beam Beam is stiffer at higher energy
Notcher
Pinger
)sin( Vy
py
July 27, 2004 Robert ZwaskaBooster Cogging
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Notching for Multibatch- Cogging -
84 RF bucketsaround circumference
NotchBooster
Main Injector
Previous injectedPrevious injectedBooster batchBooster batch
• Booster extraction to MI must be synchronized with the notch• Extraction must also be synchronized to the beam already
circulating in the Main Injector• Problem: The Booster and Main Injector are not necessarily
synchronized Booster beam “slips” relative to the Main Injector Amount of slippage is not consistent cycle-to-cycle
• “Cogging” is forced synchronization of beams No Booster flattop available to fix at the end Active feedback is necessary during acceleration
July 27, 2004 Robert ZwaskaBooster Cogging
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Raw position
Following the Notch
• RF buckets slip at a rate fMI – fB
Initially 15 MHz Notch wraps around the Booster
many times
• Extraction with one batch Count RF buckets to make a marker Extract on marker
• Tunable delay
Reset Main Injector
• With several batches Possible if total slippage is exactly
the same Requires 1 in 100,000 consistency
6/7 resonance
July 27, 2004 Robert ZwaskaBooster Cogging
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Measuring Slippage• Monitor Notch position throughout
the cycle• Use Main Injector RF as a standard
clock• Booster RF frequency varies with
energy 38 53 MHz
• Start counting on Main Injector revolution marker
• Stop Counting on Booster revolution marker
• Makes a table of positions (tripplan)
588 buckets @ 52.8114 MHzMain Injector
Revolution Marker
84 buckets @38 – 53 MHz
Booster Revolution Marker (Notch)
Booster RF 38 – 53 MHz
in 1in 2in
July 27, 2004 Robert ZwaskaBooster Cogging
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Raw position Relative to baseline
~ 3 turns
Relative Slippage• Slippage in a cycle varies by > 200 buckets
About 3 circumferences• Notch is essentially at a random position w.r.t the beam
circulating in the Main Injector
July 27, 2004 Robert ZwaskaBooster Cogging
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Sources of Slippage
• Any change in the difference of frequencies (fMI, fB) will cause slippage
• Some errors in the Booster can be parameterized as a change in p(t)
• Slip rate: (buckets/ time) 15 MHZ 0
• (inj. ext.)
• Variations in wall socket frequency has long been suspected as a source of error Booster 15 Hz is line f ÷ 4
2
2
2
)(MI
MIBMI1
11
p
mcfff
t
tdttS0
'' )()(
)2cos()( 10 ftpptp
GeV/c 9223.4)( ie21
0 ppp
GeV/c 9666.3)( ie21
1 ppp
July 27, 2004 Robert ZwaskaBooster Cogging
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Error Characterization• Any perturbation to (t) will resulting
slippage• Some errors can be parameterized as a
change in p(t) Each has a particularly shaped S(t) curve
MaximumMagnet Current
Magnet Frequency
Timing
MinimumMagnet Current
Time (ms)
S(t
) (
norm
aliz
ed)
t
tdx
ddtxtS
0
'' )()(
• Several possible errors shown below: Timing: 1 s 15 bucket slip Magnet Frequency: 1 mHz 6 bucket slip Minimum Magnet current (pi): 1/10,000
10 bucket slip Maximum Magnet current (pe): 1/10,000
7 bucket slip
July 27, 2004 Robert ZwaskaBooster Cogging
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sample
Notchradial feedback
Cogging Method• Use the early part of the cycle to
predict net slippage before extraction Place the notch anticipating further
slippage (few ms into cycle)
• After transition slippage can be induced by changing the radial position of the beam Changes the feedback of the Low
Level RF systems Changes the circumference, and thus
period, of a revolution Active feedback can correct to zero
error
r
~ 3 turns
July 27, 2004 Robert ZwaskaBooster Cogging
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Intelligent Notching• Depends on consistent slippages signature
i.e. source of slippage
• Application of the notch 5 ms later can reduce range
~ 3 turns
~ 20 buckets
July 27, 2004 Robert ZwaskaBooster Cogging
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First Tests of Cogging• Notch using prediction• Radial Feedback late in the cycle• r = k ∙ S
Exponential damping k 0.2 mm / bucket e-folding time 10 ms
NotchRadial
Feedback
Notch
RadialFeedback
Doesn’t get to zero
Recent Cogging in the Booster• Shown are the second batches of a slip-stacking cycle
All slippage is to one side Radial feedback is significant
• Radial offset goes to a constant value to get closer to zero 90% with 0 error Other 10% with ± 1 (out of ~ 70)
Notch
RadialFeedback 0 ms 33 ms
0e12-5 mm
2.4e12+5 mm
15 ms 35 ms
Intensity
Radial PositionsOf multiple cycles
July 27, 2004 Robert ZwaskaBooster Cogging
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Beam in the Main Injector
• These are Booster Batches lined up in the Main Injector Two different beam tests
• Kicker extraction is synchronized with beam in Main Injector Not to the notch in Booster
• Upper set is uncogged Notch appears randomly within
the batches
• Second batch is cogged Notch appears at a consistent
position with each batch Only the timing of the notcher
need be adjusted• Wouldn’t be visible otherwise
Tim
e
Tim
e
Notches
July 27, 2004 Robert ZwaskaBooster Cogging
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Ping Notching
• Current notch knocks out the beam with one kick Works less well at slightly higher momenta Activates one region with the loss
• This loss is irreducible and scales with the number of protons
• Alternative: Apply a series of smaller kicks (pings) Similar, in concept, to anti-damping
• But, no feedback Takes a few hundred turns Uses a solid-state driver Losses go into collimators
• Need to account for tune spreads and shifts
July 27, 2004 Robert ZwaskaBooster Cogging
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Broadband Pinging Simulation
Applying a broadband sequence of pings allows a
range of tunes to be kicked out
July 27, 2004 Robert ZwaskaBooster Cogging
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Intensity in the Main Injector
• Since commissioning, MI has run with only 5 x 1012 protons in it 1/7 of the ring
• With NuMI, there will be at least 3 x 1013
5+1 x 1012
Booster per-batch intensity may be higher Stacking schemes might allow another 50%
• Numerous problems need to be addressed Foremost are instabilities due to beam-loading and other collective effects
• This is just to get to our planned intensities, higher will require significant upgrades
July 27, 2004 Robert ZwaskaBooster Cogging
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Time
Phase
A View of Slip-Stacking
July 27, 2004 Robert ZwaskaBooster Cogging
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GMPS• Booster magnets are part of a resonant circuit
DC & AC componentsAC is part of a LRC circuit with choke & caps in
tunnel
• Circuit controlled by “GMPS” (Gim-pis)Gradient Magnet Power Supply
July 27, 2004 Robert ZwaskaBooster Cogging
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Settings
Read-backs
Feedback
July 27, 2004 Robert ZwaskaBooster Cogging
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GMPS Regulation• Observed Oscillation of minimum
current Occurs over a train of cycles
• Suggestive of line draw, and compensation Feedback with t 400 ms
• Hypthesized cause: Pulsed devices drag line current down Lower line current reduces power
input to GMPS Particularly, RF & bias supplies
GMPS regulation
-1.5
-1
-0.5
0
0.5
1
1.5
2
-10 -8 -6 -4 -2 0 2 4 6 8 10
Time (s)
Bias power to 1 Station (kW)
Error in minimum Current
July 27, 2004 Robert ZwaskaBooster Cogging
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GMPS Over a Cycle Train
GMPS regulation
-1.5
-1
-0.5
0
0.5
1
1.5
2
-8.5 -8.3 -8.1 -7.9 -7.7 -7.5 -7.3 -7.1 -6.9 -6.7 -6.5Time (s)
Bias power to 1 Station (kW)
Error in minimum Current
12 12 14 14 1D 1D 1D 1D 1D 1D 1D
July 27, 2004 Robert ZwaskaBooster Cogging
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GMPS Effects• These are all the second $14
w.r.t. a first $14• All display an initial slippage
Starts after ~1 msRate of ~ 7 buckets/msTurns around after notch
• Difference depends on position on trainWorse for NuMI cyclesDepends on the rest of the timelineDifferent signature than other slips
• Hurts PredictionCan’t be fixed by frequent tripplans
• What’s Happening:Beam is bunched into 38 MHZ buckets
• Set externally• No initial Slippage
Phase feedback turns on quickly• Lower magnet current• Beam is pushed toward outside• Slippage begins
Radial feedback turns on after few ms• Gain ramps up• Beam moved to correct position• Slippage lessons quickly
July 27, 2004 Robert ZwaskaBooster Cogging
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What to do with GMPS?• Compensate with cogging:
Cogging “works” with this variation• However, beam is pushed more than we would like
Adequate for moderate intensities
• Fix GMPS:EE Support is looking into feedback
• Feedback should be able to be faster
More stable GMPS might be good all around
• Isolate GMPSMove GMPS to a different feeder than pulsed devicesUnder investigation
July 27, 2004 Robert ZwaskaBooster Cogging
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Half a Notch
• Notcher power supply is old and decrepit
• Notch is marginal on batch trains
• Notch is partial with cogging 5-10% remains in two
buckets Only two buckets wide
• Makes cogging hard We could always go with a
wider notch, but we don’t want to
July 27, 2004 Robert ZwaskaBooster Cogging
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Summary• Proton demand at FNAL has been growing, and will continue to
Current experiments need more protons NuMI is about to start using protons Potential experiments need even more protons
• FNAL has an ongoing process of upgrade and improvement to its proton source Focuses on the Booster and Main Injector accelerators
• Improvement is expected in the Booster
• Main Injector will start high-intensity operations
Improvements have been made with outside collaboration:• Universities, involved in experiments and otherwise
• Other labs (KEK, BNL, LANL, RAL, etc.)
• Until a Proton Driver materializes, improvements in proton intensity will require investments throughout the accelerator complex