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ASHRAE JOURNAL ashrae.org JANUARY 2014 36 A new 1.1 million ft 2 (102 193 m 2 ) research insti- tute building at Houston Methodist Hospital (HMH) prompted an expansion of its existing central utility plant (CUP). The steam demand on the CUP required operation of the two existing natural gas 60,000 lb/h (7560 g/s) high-pressure steam boilers, leaving the plant without a standby unit. Although the CUP had sufficient chiller capacity, it was deficient in the necessary cooling tower capacity to support opera- tion of all seven of the installed centrifugal chillers simultaneously. Auxiliary equipment for the one existing steam-driven chiller and/or ancillary equipment of any of the electric drive chillers (cooling towers, condenser/chiller water pumps) were not connected to standby power. BY BRUCE L. FLANIKEN, P.E., MEMBER ASHRAE Texas Hospital Central Plant Redesign 2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES SECOND PLACE HEALTH CARE FACILITIES, EXISTING A new research institute at Houston Methodist Hospital prompted an expansion of the central utility plant. New high efficiency equipment included a gas turbine-driven electrical generator with duct burner and high pressure heat recovery steam generator with aqueous ammonia selective catalytic reduction. ABOUT THE AUTHOR Bruce L. Flaniken, P.E., is design & construction manager of engineering at the Houston Methodist Hospital. Central Utility Plant Cogeneration CHP Upgrade Location: Houston Owner: Houston Methodist Hospital Principal Use: Existing Hospital CUP Includes: Two natural gas-fired, high pres- sure steam boilers; five electric drive water-cooled centrifugal chillers; two steam-driven, water-cooled centrifugal chillers including ancillary equipment (cooling towers, condenser/chiller water pumps) and electrical switchgear; gas turbine-driven electrical generator with duct burner and high-pressure heat recovery steam generator with aqueous ammonia selective catalytic reduction (SCR). The CUP now serves existing 1,000-bed hospital and 1.1 million ft 2 research facility. Employees/Occupants: 450 Gross Square Footage: 1.2 Million Conditioned Space Square Footage: 1.1 Million Substantial Completion/Occupancy: January 2011 Occupancy: 100% BUILDING AT A GLANCE This article was published in ASHRAE Journal, January 2014. Copyright 2014 ASHRAE. Posted at www. ashrae.org. This article may not be copied and/or distributed electronically or in paper form without permission of ASHRAE. For more information about ASHRAE Journal, visit www.ashrae.org.

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  • A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 43 6

    A new 1.1 million ft2 (102 193 m2) research insti-tute building at Houston Methodist Hospital (HMH) prompted an expansion of its existing central utility plant (CUP). The steam demand on the CUP required operation of the two existing natural gas 60,000 lb/h (7560 g/s) high-pressure steam boilers, leaving the plant without a standby unit. Although the CUP had sufficient chiller capacity, it was deficient in the necessary cooling tower capacity to support opera-tion of all seven of the installed centrifugal chillers simultaneously.

    Auxiliary equipment for the one existing steam-driven chiller and/or ancillary equipment of any of the electric drive chillers (cooling towers, condenser/chiller water pumps) were not connected to standby power.

    BY BRUCE L. FLANIKEN, P.E., MEMBER ASHRAE

    Texas HospitalCentral Plant Redesign

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    SECOND PLACEHEALTH CARE FACILITIES, EXISTING

    A new research institute at

    Houston Methodist Hospital

    prompted an expansion of the

    central utility plant. New high

    efficiency equipment included

    a gas turbine-driven electrical

    generator with duct burner and

    high pressure heat recovery

    steam generator with aqueous

    ammonia selective catalytic

    reduction.

    ABOUT THE AUTHOR Bruce L. Flaniken, P.E., is design & construction manager of engineering at the Houston Methodist Hospital.

    Central Utility PlantCogeneration CHP Upgrade

    Location: Houston

    Owner: Houston Methodist Hospital

    Principal Use: Existing Hospital CUP

    Includes: Two natural gas-fired, high pres-sure steam boilers; five electric drive water-cooled centrifugal chillers; two steam-driven, water-cooled centrifugal chillers including ancillary equipment (cooling towers, condenser/chiller water pumps) and electrical switchgear; gas turbine-driven electrical generator with duct burner and high-pressure heat recovery steam generator with aqueous ammonia selective catalytic reduction (SCR). The CUP now serves existing 1,000-bed hospital and 1.1 million ft2 research facility.

    Employees/Occupants: 450

    Gross Square Footage: 1.2 Million

    Conditioned Space Square Footage: 1.1 Million

    Substantial Completion/Occupancy: January 2011

    Occupancy: 100%

    BUILDING AT A GLANCE

    This article was published in ASHRAE Journal, January 2014. Copyright 2014 ASHRAE. Posted at www.ashrae.org. This article may not be copied and/or distributed electronically or in paper form without permission of ASHRAE. For more information about ASHRAE Journal, visit www.ashrae.org.

  • J A N U A R Y 2 0 1 4 a s h r a e . o r g A S H R A E J O U R N A L 3 7

    Therefore, they could not provide emergency cool-

    ing, which was required by the new research building

    as well as being necessary to care for patients during

    major storms and hurricanes that cause utility outages

    in Texas.

    The installation of the cogeneration turbine with

    duct burner and high-pressure steam thermal energy

    recovery unit makes HMH the only hospital in the

    Texas Gulf Coast area that can operate during hurri-

    cane-type power grid outages. The system incremental

    cost and estimated energy savings using simple pay-

    back had been projected to pay back in 3.5 years or less.

    The CUP upgrade project directly addressed the

    cooling tower deficiency by installing an additional

    6,800 tons (23,915 kW) of cooling tower capacity in the

    form of seven additional cells. The standby steam and

    power concerns were addressed by the installation of a

    200 psig (1379 kPa) natural gas turbine-generator com-

    bined heat and power (CHP) unit to increase overall

    thermal efficiency and produce steam via a combination

    heat recovery steam generator and natural gas-fired

    duct burner of standby power at 4,160 V via a natural

    gas-turbine generator. (Note: the actual capacity of

    the 4.3 MW cogeneration unit varies depending upon

    outside air temperature and percent relative humidity.

    Initial capacity rating is given at ISO inlet air conditions

    of 60F [15.5C] DB/60% RH. Ambient inlet air becomes

    de-rated to approximately 3.8 MW at 100F [38C]

    DB/60% RH.)

    The CHP unit was installed to address standby power

    and emergency cooling capability concerns. This unit

    allows HMH to generate its own electrical power and

    take advantage of reduced energy mix cost, and increase

    CHP thermal efficiency while in the CHP mode.

    The installation of the higher cost low NOX output

    CHP turbine with aqueous ammonia selective catalytic

    reduction (SCR) significantly decreased NOX emissions.

    It also reduced the overall permit application time in an

    EPA non-attainment zone (by submitting it to EPA using

    best available control technologies, which reduced over-

    all NOX output substantially).

    Existing chilled water emergency cooling concerns were

    addressed through the addition of a 2,800 ton (9847 kW)

    steam turbine-driven chiller and by revising the existing

    electrical power distribution, feeding standby power to

    other electric chillers and their auxiliary equipment. This

    provides for 6,800 tons (23 915 kW) of emergency cool-

    ing capability in cogeneration island mode (stand-alone

    mode) when all power is lost to the facility.

    Additional pump piping cross connections and man-

    ual bypass/isolation valves also were installed to allow

    dedicated chilled and condenser water pumps to cross

    connect to other nearby chillers to the greatest extent

    possible. Variable frequency drives (VFDs) were added to

    all cooling tower fans and chilled water and condenser

    water pumps to improve system response and wire-to-

    water efficiency.

    The installation of a 2,000 ton (7034 kW) steam turbine

    chiller in 2004 was undertaken as part of an energy ini-

    tiative rebate available from the local utility company.

    Another separate chilled water distribution upgrade

    project involved adding differential pressure sensors

    to control secondary chilled water distribution pumps

    driven by VFDs.

    This was done primarily to improve system DT that was 2F to 3F (4C to 5C) lower than designed for in

    the original chiller selections. It is an ongoing goal to

    achieve a standardized DT of 12F (22C) throughout all buildings on site served by our district CHP. The CUP

    now produces up to a total of 12,800 tons of chilled water

    through five 2,000 ton (7034 kW) electric chillers, one

    2,000 ton (7034 kW) steam-driven centrifugal chiller

    and the new 2,800 ton (9847 kW) steam-driven centrifu-

    gal chiller in an N+1 configuration throughout.

    ABOVE Cogeneration system with new and existing cooling tower and power house.

    LEFT Cogeneration system looking north.

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

  • A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 43 8

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    The CUP can produce up to a total demand of

    99,500 lb/h (12 537 g/s), 210 psig (1448 kPa) steam

    through a 24,500 lb/h (3087 g/s) heat recovery steam

    generator, a 25,000 lb/h (3150 g/s) natural gas-fired

    duct burner and two high-pressure steam boilers

    rated at 50,000 lb/h (6300 g/s) in a N+1 configuration

    and with a boiler operated in standby low-fire mode

    for quick steam demand response to CHP systems

    shutdown, reducing energy consumption and emis-

    sions of NOX.

    A new 200 psig (1379 kPa) natural gas main from the

    local utility company that included a high-pressure natu-

    ral gas pressure regulating station was installed to serve

    CHP and boiler loads while improving system perfor-

    mance and reliability. A rooftop ammonia storage tank and

    an at-grade fill station were installed to support the aque-

    ous ammonia SCR emission controls system. A CHP con-

    tinuous emissions monitoring system had to be installed

    and operational at the time of start-up, which required

    HMH to update all facilities overall air quality compliance

    forms to meet state and federal emission requirements.

    The BAS originally installed in the CUP was upgraded

    to increase the degree of automation and optimization

    that could be achieved to reduce staffing requirements

    while improving systems reliability, record keeping and

    maintenance. This will allow optimization of all CUP

    chillers, pumps, cooling towers, CHP electrical genera-

    tion, CHP thermal energy recovery (heat recovery steam

    generator) and high-pressure steam boilers integration

    in our efforts to maximize wire-to-water efficiencies.

    Energy EfficiencyInstalling a new 2,800 ton (9847 kW) high efficiency

    R-134a steam-driven centrifugal chiller to replace

    the existing 2,000 ton (7034 kW) asynchronous elec-

    tric motor-driven centrifugal R-22 chiller rated for

    0.758 kW/ton reduced electrical demand by 1,600 kW.

    Also, a modeled offset of nearly 1.5 million kWh of elec-

    trical consumption was realized. The optimized opera-

    tion of the primary chilled water supply loop and the

    secondary chilled water loops systems has been greatly

    enhanced by the building automation system, which

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  • A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 0

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    research demands while reducing dependence on the

    local power grid.

    The hospitals steam demand profile requires pro-

    ducing approximately 20,700 lb/h (2608 g/s) of steam

    to meet heating, sterilizing, humidification, domestic

    hot water steam loads, along with the steam demand

    of a 2,800 ton (9847 kW) steam-driven centrifugal

    chiller (requiring 25,300 lb/h [3188 g/s] of high-pres-

    sure steam). This allows us to base load the CHP for

    electrical power generation and recovered thermal

    energy while rarely having to fire the high NOX steam

    boilers.

    Operation & MaintenanceExisting reliability, redundancy and other O&M issues

    addressed during the project design and construction

    phase included adding cooling tower capacity, along with

    system piping and electrical system modifications that

    provided a higher degree of overall functionality and reli-

    ability. We have achieved cold weather operation of the

    CUP using one 2,800 ton (9847 kW) steam-driven chiller

    where previously it took a minimum of two 2,000 ton

    (7034 kW) chillers.

    This was achieved by improving AHU coil design DT to match the original design of 12F (22C) DT and adding UVC lights to keep cooling coils clean when replacing old

    low DT air-handling units, by adding UVC lamps to exist-ing cleaned and refurbished AHU coils, and by better

    secondary and primary chilled water systems differential

    pressure and VFD control. The addition of the CHP and

    associated protective switchgear has made the overall

    system much more complex, but the added BAS automa-

    tion and increased O&M training required by the system

    have resulted in a more reliable and easier to troubleshoot

    overall central utility plant, and one that certainly can

    operate during extended power grid outages.

    Cost EffectivenessThe natural gas-fired CHP cogeneration/heat recov-

    ery steam generator/duct burner units were installed

    to address both power capacity and emergency cool-

    ing capability concerns. This gives HMH the ability to

    allows improved wire-to-water

    transfer of energy, reducing overall

    energy consumption considerably.

    InnovationThe use of a natural gas turbine-

    driven CHP/heat recovery steam

    generator/duct burner to provide

    for the base steam demand, and that

    required to run the steam-driven

    chiller, has resulted in a substantial

    shift in demand from the existing

    utility power grid to the natural gas

    utility and allowed us to produce up

    to 2,800 tons (9847 kW) of chilled

    water from free steam for only the

    cost associated with running the

    condenser-chilled water pumps and

    cooling tower fans.

    HMH can produce up to 6,800 tons

    (23 915 kW) of emergency cooling

    in the cogeneration (CHP) island

    mode if all power is lost due to roll-

    ing brownouts or storm damage.

    This upgrades the ability to operate

    a significant portion of the campus

    while maintaining patient care and

    Electricity MMBtu Gas MMBtu

    2010 2011 Energy Mix 2011 2012 Energy Mix

    FIGURE 1 Cogeneration decreased the dependency on electricity, reducing electric consumption and avoiding $1.85 mil-lion in net expense over 12 months. This cogeneration project is expected to return investment in fewer than two years.

    12

    10

    8

    6

    4

    2

    0

    Blend

    ed $/

    MMBt

    u

    Feb. Mar. Apr. May Jun. Jul. Aug. Sep. Oct. Nov. Dec. Jan.

    FIGURE 2 Year-over-year change. Due to the reduction in electricity use (a higher expense energy source) the overall $MMBtu was reduced significantly and savings are higher than modeled.

    2010 11 Blended $/MMBtu

    2011 12 Blended $/MMBtu

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  • A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 2

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    (CHP) and used the free steam to run a steam-driven

    chiller 8,456 hours during this period, making maximum

    use of the free thermal energy recovered by the heat

    recovery steam generator. While we found it difficult to

    compute the exact savings derived from cogeneration due

    to dramatic utility cost fluctuations that occurred during

    the project, we were able to calculate energy cost savings

    of approximately $1.85 million mainly due to the added

    thermal energy recovery (Figure 1).

    We averaged electrical and natural gas use and cost

    via a blended $/MMBtu (Figure 2). This translates to a

    total annual gross savings of $2.2 million from Feb. 2011

    FIGURE 3 Shift of energy expense due to cogeneration (from 20112012). While installation of the cogeneration operation increased maintenance and standby gas expense, the benefit of avoided util-ity expense of more than $1.3 million and more than $800,000 of free steam generation established this project as a best practice standard for reducing expense and lowering carbon footprint.

    $2 Million

    $1.5 Million

    $1 Million

    $500,000

    $0

    $(500,000)Feb. Mar. Apr. May Jun. Jul Aug. Sep. Oct. Nov. Dec. Jan.

    self-generate electrical power and achieve sav-

    ings in energy costs while in the cogeneration

    mode. The $1 million annual estimated energy

    savings resulting from the overall increased

    thermal efficiency of the CHP (from 30% to

    approximately 88%) came from base load-

    ing of the CHP unit for both power and steam

    consumption (24/7/365). This completely off-

    set the added cost of the upgrade from a new

    high-pressure steam boiler and a new 2.5 MW

    emergency diesel generator to the 4.3 MW gas-

    fired cogeneration turbine/heat recovery steam

    generator/duct burner unit with a modeled

    payback between three and four years.

    The project achieved a 92.2%+ annual operating

    hours (8,079 hours of operation) for cogeneration

    Actual Net Savings: $1.85 Million Avoided UtilityFree Stream Increased Standby GasIncreased Maintenance

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  • J A N U A R Y 2 0 1 4 a s h r a e . o r g A S H R A E J O U R N A L 4 3

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    through Jan. 2012 with a net annual avoided cost of $1 mil-

    lion. One additional cost that had to be included was the

    cost of running one of the high-pressure steam boilers at

    low fire during cogeneration (CHP) mode so that in the

    event of cogeneration shutdown we could get the high-

    pressure steam system operational in under an hour.

    That additional annual operation cost was $73,726.

    Also, we have added the calculated cost of chilled water

    demand load and power consumption savings on the

    CUP chilled water production by recovering 24,500 lb/h

    (3087 g/s) of high-pressure steam from the cogenera-

    tion heat recovery steam generator for an annual total

    of 294,000 lb/h (37043 g/s) of high-pressure steam

    (165,541.6 MMBtu). That steam is used to produce 21

    million ton hours of cooling via the steam-driven cen-

    trifugal chillers at an estimated savings of $817,523 for a

    combined annual net savings of $1.8 million from Feb.

    2011 through Jan. 2012. This puts the simple payback at

    2.16 years versus four years as initially modeled.

    Systems overall heat transfer efficiency for the cogen-

    eration (CHP) unit increased from around 30% for gen-

    eration of electric power to slightly above 88% by using

    the heat recovery steam generator unit to capture

    the free waste heat and use it effectively to generate

    domestic hot water, heating hot water, sterilizer steam

    and/or chilled water in the manifolded high-pressure

    steam distribution system.

    The environmental impact from NOX emissions has

    been reduced by selecting a gas turbine-generator CHP

    unit using aqueous ammonia SCR with best available

    control technology rated to produce maximum 15 ppm

    NOX in lieu of high-pressure steam boilers. Using the

    EPA CHP emissions calculator, the CHP system will

    reduce NOX by a net reduction of 71% or 20.79 tons/year

    (56.9 kg/year), SO2 by a net reduction of 100% or

    56.10 tons/year (154 kg/year) and will reduce CO2 by

    10,511 tons/year (28,797 kg/year) or 28%.

    Expensive hurdles included site adaptation of the exist-

    ing 50-year-old CUP roof structural support to install

    the equipment on the roof and getting a crane to set up

    the equipment without closing the hospital main patient

    drop-off. Others were limited working space access adja-

    cent to the emergency entrance/ambulance drive and the

    ongoing construction of the new research building.

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  • A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 4

    2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES

    Integrating the xisting plant BAS and CHP system con-

    trols, installing the chiller, cooling tower and piping cross

    connections without shutting down the existing CUP

    utilities had to be carefully planned and mitigated.

    The heat recovery steam generator can recover

    24,500 lb/h (3087 g/s) of free high-pressure 210 psig

    (1448 kPa) steam from the turbine engine discharge gases.

    The duct burner was selected to generate an additional

    25,000 lb/h (3150 g/s) of high-pressure 210 psig (1448 kPa)

    steam by injecting fuel to the closed gas turbine discharge

    where there was sufficient oxygen to get an extremely

    efficient burn with minimal heat loss. This allowed us to

    base load the heat recovery steam generator and recover

    high-pressure steam while running only one high-pres-

    sure steam boiler November through February.

    The recovery and use of this lower cost steam is what

    improved payback and pushed overall thermal effi-

    ciency to 88.1% while keeping loss of thermal efficiency

    to the flue stack to 11.9% of input gas ratings. HMH also

    base loaded the CHP electrical generation capacity so it

    would not have to negotiate interconnectivity fees with

    the local utility. HMH received a local utility rebate of

    approximately $450,000 for the kW demand displaced

    by the steam centrifugal chiller.

    A lesson learned was that we should have included the

    turbine inlet chilled water cooling coil to reduce entering

    air temperature to 57F (14C) ISO year-round to allow the

    turbine to operate at maximum efficiency due to denser,

    cooler air intake and produce the full 4.5 MW of power at

    all outside air temperatures. The cost to add that now as

    a separate project is about $1.2 million, while including

    it initially would have cost about $750,000, reducing the

    simple payback from nearly five years to about three years

    or less. In Houston, there are approximately 7,080 hours

    where the outside air temperature is above the 57F (14C)

    ISO temperature that allows the CHP turbine to produce

    4.5 MW of power, in lieu of the de-rating to approximately

    3.8 MW at 100F (38C) DB/60% RH of standby power at

    4,160 V via a natural gas-turbine generator.

    Another lesson learned is that we should have set up

    the electrical systems protection relays to shut down the

    cogeneration unit, rather than the main power feed from

    the utility company as this is less disruptive of our side and

    still protects the utility and hospital systems as required.

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