Upload
magdyeng
View
4
Download
0
Embed Size (px)
DESCRIPTION
ASHRAE Journal for Jan 2014
Citation preview
A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 43 6
A new 1.1 million ft2 (102 193 m2) research insti-tute building at Houston Methodist Hospital (HMH) prompted an expansion of its existing central utility plant (CUP). The steam demand on the CUP required operation of the two existing natural gas 60,000 lb/h (7560 g/s) high-pressure steam boilers, leaving the plant without a standby unit. Although the CUP had sufficient chiller capacity, it was deficient in the necessary cooling tower capacity to support opera-tion of all seven of the installed centrifugal chillers simultaneously.
Auxiliary equipment for the one existing steam-driven chiller and/or ancillary equipment of any of the electric drive chillers (cooling towers, condenser/chiller water pumps) were not connected to standby power.
BY BRUCE L. FLANIKEN, P.E., MEMBER ASHRAE
Texas HospitalCentral Plant Redesign
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
SECOND PLACEHEALTH CARE FACILITIES, EXISTING
A new research institute at
Houston Methodist Hospital
prompted an expansion of the
central utility plant. New high
efficiency equipment included
a gas turbine-driven electrical
generator with duct burner and
high pressure heat recovery
steam generator with aqueous
ammonia selective catalytic
reduction.
ABOUT THE AUTHOR Bruce L. Flaniken, P.E., is design & construction manager of engineering at the Houston Methodist Hospital.
Central Utility PlantCogeneration CHP Upgrade
Location: Houston
Owner: Houston Methodist Hospital
Principal Use: Existing Hospital CUP
Includes: Two natural gas-fired, high pres-sure steam boilers; five electric drive water-cooled centrifugal chillers; two steam-driven, water-cooled centrifugal chillers including ancillary equipment (cooling towers, condenser/chiller water pumps) and electrical switchgear; gas turbine-driven electrical generator with duct burner and high-pressure heat recovery steam generator with aqueous ammonia selective catalytic reduction (SCR). The CUP now serves existing 1,000-bed hospital and 1.1 million ft2 research facility.
Employees/Occupants: 450
Gross Square Footage: 1.2 Million
Conditioned Space Square Footage: 1.1 Million
Substantial Completion/Occupancy: January 2011
Occupancy: 100%
BUILDING AT A GLANCE
This article was published in ASHRAE Journal, January 2014. Copyright 2014 ASHRAE. Posted at www.ashrae.org. This article may not be copied and/or distributed electronically or in paper form without permission of ASHRAE. For more information about ASHRAE Journal, visit www.ashrae.org.
J A N U A R Y 2 0 1 4 a s h r a e . o r g A S H R A E J O U R N A L 3 7
Therefore, they could not provide emergency cool-
ing, which was required by the new research building
as well as being necessary to care for patients during
major storms and hurricanes that cause utility outages
in Texas.
The installation of the cogeneration turbine with
duct burner and high-pressure steam thermal energy
recovery unit makes HMH the only hospital in the
Texas Gulf Coast area that can operate during hurri-
cane-type power grid outages. The system incremental
cost and estimated energy savings using simple pay-
back had been projected to pay back in 3.5 years or less.
The CUP upgrade project directly addressed the
cooling tower deficiency by installing an additional
6,800 tons (23,915 kW) of cooling tower capacity in the
form of seven additional cells. The standby steam and
power concerns were addressed by the installation of a
200 psig (1379 kPa) natural gas turbine-generator com-
bined heat and power (CHP) unit to increase overall
thermal efficiency and produce steam via a combination
heat recovery steam generator and natural gas-fired
duct burner of standby power at 4,160 V via a natural
gas-turbine generator. (Note: the actual capacity of
the 4.3 MW cogeneration unit varies depending upon
outside air temperature and percent relative humidity.
Initial capacity rating is given at ISO inlet air conditions
of 60F [15.5C] DB/60% RH. Ambient inlet air becomes
de-rated to approximately 3.8 MW at 100F [38C]
DB/60% RH.)
The CHP unit was installed to address standby power
and emergency cooling capability concerns. This unit
allows HMH to generate its own electrical power and
take advantage of reduced energy mix cost, and increase
CHP thermal efficiency while in the CHP mode.
The installation of the higher cost low NOX output
CHP turbine with aqueous ammonia selective catalytic
reduction (SCR) significantly decreased NOX emissions.
It also reduced the overall permit application time in an
EPA non-attainment zone (by submitting it to EPA using
best available control technologies, which reduced over-
all NOX output substantially).
Existing chilled water emergency cooling concerns were
addressed through the addition of a 2,800 ton (9847 kW)
steam turbine-driven chiller and by revising the existing
electrical power distribution, feeding standby power to
other electric chillers and their auxiliary equipment. This
provides for 6,800 tons (23 915 kW) of emergency cool-
ing capability in cogeneration island mode (stand-alone
mode) when all power is lost to the facility.
Additional pump piping cross connections and man-
ual bypass/isolation valves also were installed to allow
dedicated chilled and condenser water pumps to cross
connect to other nearby chillers to the greatest extent
possible. Variable frequency drives (VFDs) were added to
all cooling tower fans and chilled water and condenser
water pumps to improve system response and wire-to-
water efficiency.
The installation of a 2,000 ton (7034 kW) steam turbine
chiller in 2004 was undertaken as part of an energy ini-
tiative rebate available from the local utility company.
Another separate chilled water distribution upgrade
project involved adding differential pressure sensors
to control secondary chilled water distribution pumps
driven by VFDs.
This was done primarily to improve system DT that was 2F to 3F (4C to 5C) lower than designed for in
the original chiller selections. It is an ongoing goal to
achieve a standardized DT of 12F (22C) throughout all buildings on site served by our district CHP. The CUP
now produces up to a total of 12,800 tons of chilled water
through five 2,000 ton (7034 kW) electric chillers, one
2,000 ton (7034 kW) steam-driven centrifugal chiller
and the new 2,800 ton (9847 kW) steam-driven centrifu-
gal chiller in an N+1 configuration throughout.
ABOVE Cogeneration system with new and existing cooling tower and power house.
LEFT Cogeneration system looking north.
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 43 8
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
The CUP can produce up to a total demand of
99,500 lb/h (12 537 g/s), 210 psig (1448 kPa) steam
through a 24,500 lb/h (3087 g/s) heat recovery steam
generator, a 25,000 lb/h (3150 g/s) natural gas-fired
duct burner and two high-pressure steam boilers
rated at 50,000 lb/h (6300 g/s) in a N+1 configuration
and with a boiler operated in standby low-fire mode
for quick steam demand response to CHP systems
shutdown, reducing energy consumption and emis-
sions of NOX.
A new 200 psig (1379 kPa) natural gas main from the
local utility company that included a high-pressure natu-
ral gas pressure regulating station was installed to serve
CHP and boiler loads while improving system perfor-
mance and reliability. A rooftop ammonia storage tank and
an at-grade fill station were installed to support the aque-
ous ammonia SCR emission controls system. A CHP con-
tinuous emissions monitoring system had to be installed
and operational at the time of start-up, which required
HMH to update all facilities overall air quality compliance
forms to meet state and federal emission requirements.
The BAS originally installed in the CUP was upgraded
to increase the degree of automation and optimization
that could be achieved to reduce staffing requirements
while improving systems reliability, record keeping and
maintenance. This will allow optimization of all CUP
chillers, pumps, cooling towers, CHP electrical genera-
tion, CHP thermal energy recovery (heat recovery steam
generator) and high-pressure steam boilers integration
in our efforts to maximize wire-to-water efficiencies.
Energy EfficiencyInstalling a new 2,800 ton (9847 kW) high efficiency
R-134a steam-driven centrifugal chiller to replace
the existing 2,000 ton (7034 kW) asynchronous elec-
tric motor-driven centrifugal R-22 chiller rated for
0.758 kW/ton reduced electrical demand by 1,600 kW.
Also, a modeled offset of nearly 1.5 million kWh of elec-
trical consumption was realized. The optimized opera-
tion of the primary chilled water supply loop and the
secondary chilled water loops systems has been greatly
enhanced by the building automation system, which
Advertisement formerly in this space. Advertisement formerly in this space.
Advertisement formerly in this space.
A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 0
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
research demands while reducing dependence on the
local power grid.
The hospitals steam demand profile requires pro-
ducing approximately 20,700 lb/h (2608 g/s) of steam
to meet heating, sterilizing, humidification, domestic
hot water steam loads, along with the steam demand
of a 2,800 ton (9847 kW) steam-driven centrifugal
chiller (requiring 25,300 lb/h [3188 g/s] of high-pres-
sure steam). This allows us to base load the CHP for
electrical power generation and recovered thermal
energy while rarely having to fire the high NOX steam
boilers.
Operation & MaintenanceExisting reliability, redundancy and other O&M issues
addressed during the project design and construction
phase included adding cooling tower capacity, along with
system piping and electrical system modifications that
provided a higher degree of overall functionality and reli-
ability. We have achieved cold weather operation of the
CUP using one 2,800 ton (9847 kW) steam-driven chiller
where previously it took a minimum of two 2,000 ton
(7034 kW) chillers.
This was achieved by improving AHU coil design DT to match the original design of 12F (22C) DT and adding UVC lights to keep cooling coils clean when replacing old
low DT air-handling units, by adding UVC lamps to exist-ing cleaned and refurbished AHU coils, and by better
secondary and primary chilled water systems differential
pressure and VFD control. The addition of the CHP and
associated protective switchgear has made the overall
system much more complex, but the added BAS automa-
tion and increased O&M training required by the system
have resulted in a more reliable and easier to troubleshoot
overall central utility plant, and one that certainly can
operate during extended power grid outages.
Cost EffectivenessThe natural gas-fired CHP cogeneration/heat recov-
ery steam generator/duct burner units were installed
to address both power capacity and emergency cool-
ing capability concerns. This gives HMH the ability to
allows improved wire-to-water
transfer of energy, reducing overall
energy consumption considerably.
InnovationThe use of a natural gas turbine-
driven CHP/heat recovery steam
generator/duct burner to provide
for the base steam demand, and that
required to run the steam-driven
chiller, has resulted in a substantial
shift in demand from the existing
utility power grid to the natural gas
utility and allowed us to produce up
to 2,800 tons (9847 kW) of chilled
water from free steam for only the
cost associated with running the
condenser-chilled water pumps and
cooling tower fans.
HMH can produce up to 6,800 tons
(23 915 kW) of emergency cooling
in the cogeneration (CHP) island
mode if all power is lost due to roll-
ing brownouts or storm damage.
This upgrades the ability to operate
a significant portion of the campus
while maintaining patient care and
Electricity MMBtu Gas MMBtu
2010 2011 Energy Mix 2011 2012 Energy Mix
FIGURE 1 Cogeneration decreased the dependency on electricity, reducing electric consumption and avoiding $1.85 mil-lion in net expense over 12 months. This cogeneration project is expected to return investment in fewer than two years.
12
10
8
6
4
2
0
Blend
ed $/
MMBt
u
Feb. Mar. Apr. May Jun. Jul. Aug. Sep. Oct. Nov. Dec. Jan.
FIGURE 2 Year-over-year change. Due to the reduction in electricity use (a higher expense energy source) the overall $MMBtu was reduced significantly and savings are higher than modeled.
2010 11 Blended $/MMBtu
2011 12 Blended $/MMBtu
Advertisement formerly in this space.
A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 2
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
(CHP) and used the free steam to run a steam-driven
chiller 8,456 hours during this period, making maximum
use of the free thermal energy recovered by the heat
recovery steam generator. While we found it difficult to
compute the exact savings derived from cogeneration due
to dramatic utility cost fluctuations that occurred during
the project, we were able to calculate energy cost savings
of approximately $1.85 million mainly due to the added
thermal energy recovery (Figure 1).
We averaged electrical and natural gas use and cost
via a blended $/MMBtu (Figure 2). This translates to a
total annual gross savings of $2.2 million from Feb. 2011
FIGURE 3 Shift of energy expense due to cogeneration (from 20112012). While installation of the cogeneration operation increased maintenance and standby gas expense, the benefit of avoided util-ity expense of more than $1.3 million and more than $800,000 of free steam generation established this project as a best practice standard for reducing expense and lowering carbon footprint.
$2 Million
$1.5 Million
$1 Million
$500,000
$0
$(500,000)Feb. Mar. Apr. May Jun. Jul Aug. Sep. Oct. Nov. Dec. Jan.
self-generate electrical power and achieve sav-
ings in energy costs while in the cogeneration
mode. The $1 million annual estimated energy
savings resulting from the overall increased
thermal efficiency of the CHP (from 30% to
approximately 88%) came from base load-
ing of the CHP unit for both power and steam
consumption (24/7/365). This completely off-
set the added cost of the upgrade from a new
high-pressure steam boiler and a new 2.5 MW
emergency diesel generator to the 4.3 MW gas-
fired cogeneration turbine/heat recovery steam
generator/duct burner unit with a modeled
payback between three and four years.
The project achieved a 92.2%+ annual operating
hours (8,079 hours of operation) for cogeneration
Actual Net Savings: $1.85 Million Avoided UtilityFree Stream Increased Standby GasIncreased Maintenance
Advertisement formerly in this space.
J A N U A R Y 2 0 1 4 a s h r a e . o r g A S H R A E J O U R N A L 4 3
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
through Jan. 2012 with a net annual avoided cost of $1 mil-
lion. One additional cost that had to be included was the
cost of running one of the high-pressure steam boilers at
low fire during cogeneration (CHP) mode so that in the
event of cogeneration shutdown we could get the high-
pressure steam system operational in under an hour.
That additional annual operation cost was $73,726.
Also, we have added the calculated cost of chilled water
demand load and power consumption savings on the
CUP chilled water production by recovering 24,500 lb/h
(3087 g/s) of high-pressure steam from the cogenera-
tion heat recovery steam generator for an annual total
of 294,000 lb/h (37043 g/s) of high-pressure steam
(165,541.6 MMBtu). That steam is used to produce 21
million ton hours of cooling via the steam-driven cen-
trifugal chillers at an estimated savings of $817,523 for a
combined annual net savings of $1.8 million from Feb.
2011 through Jan. 2012. This puts the simple payback at
2.16 years versus four years as initially modeled.
Systems overall heat transfer efficiency for the cogen-
eration (CHP) unit increased from around 30% for gen-
eration of electric power to slightly above 88% by using
the heat recovery steam generator unit to capture
the free waste heat and use it effectively to generate
domestic hot water, heating hot water, sterilizer steam
and/or chilled water in the manifolded high-pressure
steam distribution system.
The environmental impact from NOX emissions has
been reduced by selecting a gas turbine-generator CHP
unit using aqueous ammonia SCR with best available
control technology rated to produce maximum 15 ppm
NOX in lieu of high-pressure steam boilers. Using the
EPA CHP emissions calculator, the CHP system will
reduce NOX by a net reduction of 71% or 20.79 tons/year
(56.9 kg/year), SO2 by a net reduction of 100% or
56.10 tons/year (154 kg/year) and will reduce CO2 by
10,511 tons/year (28,797 kg/year) or 28%.
Expensive hurdles included site adaptation of the exist-
ing 50-year-old CUP roof structural support to install
the equipment on the roof and getting a crane to set up
the equipment without closing the hospital main patient
drop-off. Others were limited working space access adja-
cent to the emergency entrance/ambulance drive and the
ongoing construction of the new research building.
Advertisement formerly in this space.
A S H R A E J O U R N A L a s h r a e . o r g J A N U A R Y 2 0 1 44 4
2013 ASHRAE TECHNOLOGY AWARD CASE STUDIES
Integrating the xisting plant BAS and CHP system con-
trols, installing the chiller, cooling tower and piping cross
connections without shutting down the existing CUP
utilities had to be carefully planned and mitigated.
The heat recovery steam generator can recover
24,500 lb/h (3087 g/s) of free high-pressure 210 psig
(1448 kPa) steam from the turbine engine discharge gases.
The duct burner was selected to generate an additional
25,000 lb/h (3150 g/s) of high-pressure 210 psig (1448 kPa)
steam by injecting fuel to the closed gas turbine discharge
where there was sufficient oxygen to get an extremely
efficient burn with minimal heat loss. This allowed us to
base load the heat recovery steam generator and recover
high-pressure steam while running only one high-pres-
sure steam boiler November through February.
The recovery and use of this lower cost steam is what
improved payback and pushed overall thermal effi-
ciency to 88.1% while keeping loss of thermal efficiency
to the flue stack to 11.9% of input gas ratings. HMH also
base loaded the CHP electrical generation capacity so it
would not have to negotiate interconnectivity fees with
the local utility. HMH received a local utility rebate of
approximately $450,000 for the kW demand displaced
by the steam centrifugal chiller.
A lesson learned was that we should have included the
turbine inlet chilled water cooling coil to reduce entering
air temperature to 57F (14C) ISO year-round to allow the
turbine to operate at maximum efficiency due to denser,
cooler air intake and produce the full 4.5 MW of power at
all outside air temperatures. The cost to add that now as
a separate project is about $1.2 million, while including
it initially would have cost about $750,000, reducing the
simple payback from nearly five years to about three years
or less. In Houston, there are approximately 7,080 hours
where the outside air temperature is above the 57F (14C)
ISO temperature that allows the CHP turbine to produce
4.5 MW of power, in lieu of the de-rating to approximately
3.8 MW at 100F (38C) DB/60% RH of standby power at
4,160 V via a natural gas-turbine generator.
Another lesson learned is that we should have set up
the electrical systems protection relays to shut down the
cogeneration unit, rather than the main power feed from
the utility company as this is less disruptive of our side and
still protects the utility and hospital systems as required.
Advertisement formerly in this space.