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Consultancy. Project Delivery. Innovation. Case Study: Natural Gas Letdown Reliability Dynamic Simulation to ensures unit reliability and saves £3m/year Client: Refinery run by Multinational Oil & Gas Corporation

Case Study: Natural Gas Letdown Reliability

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Page 1: Case Study: Natural Gas Letdown Reliability

Consultancy.

Project Delivery.

Innovation.

Case Study: Natural Gas Letdown Reliability

Dynamic Simulation to ensures unit reliability and saves £3m/year

Client: Refinery run by Multinational Oil & Gas Corporation

Page 2: Case Study: Natural Gas Letdown Reliability

Who are we?

Process engineering consultancy

Specialising in advanced modelling techniques, to give answers that

are more accurate, reliable and robust

Expertise in HYSYS Dynamics and Dynsim

Decades of process and mechanical engineering experience

Combine cutting edge simulation with real world understanding, to

provide you with solutions that are effective and practical.

Core team of eight engineers, supported by a wide network of

associates.

Extensive simulation experience across a range of industries

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Page 3: Case Study: Natural Gas Letdown Reliability

Project Background

Refinery needed to convert to natural gas as primary fuel source to

replace LPG / Gas Oil to reduce energy costs (£3m/year), manage

sulphur emissions and operate a new CHP plant

Decision taken to import natural gas from national grid

Initial third party installation of let-down systems had major safety and

reliability issues

Decision to completely redesign with new knowledge and check out

design using dynamic simulation to validate reliability

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Page 4: Case Study: Natural Gas Letdown Reliability

Our Responsibilities

Concept Design, avoiding pitfalls of original design. Issue report and

help client to make best decision

FEED, including detailed design basis document, HAZOP study and

control & trip analysis

Detailed Process Design, specification of new equipment, hydraulic

network models and relief and venting study

Dynamic Simulation to validate reliability and test operability

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Page 5: Case Study: Natural Gas Letdown Reliability

Old Let-Down Configuration

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Page 6: Case Study: Natural Gas Letdown Reliability

Old Reliability Issues

All critical consumers dependent on a single let down

Single trip takes down the whole site

Second stage let down station unstable, inlet pressure too high and often

trips from a disturbance in downstream fuel gas pressure. This then

causes an upstream trip at first let down station, taking down the site

Natural gas make up into fuel gas critical to keeping process

heaters/steam boilers running. Fuel gas pressure depletes very quickly

if natural gas is lost

Backup LPG vaporiser too slow to act and has to keep flowing at low

rates to ensure availability at short notice

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Page 7: Case Study: Natural Gas Letdown Reliability

First Let Down Station

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Page 8: Case Study: Natural Gas Letdown Reliability

New Let-down Configuration

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Page 9: Case Study: Natural Gas Letdown Reliability

Hardware Improvements

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Separate Let Down

Systems create

diversification

Reduced inlet pressure to

second let down station &

improved margin between

operating and trip settings

Second let down station

provides diversification

Electric heater provides online

back up to steam preheater

Page 10: Case Study: Natural Gas Letdown Reliability

Dynamic Simulation to Check Reliability

Build high fidelity dynamic simulation of gas network from 94 barg supply

to 3.5 barg fuel gas system

Include all mechanical features of system, valve closing times, detailed

valve trim characteristics, preliminary controller settings, heat transfer

from heaters and heat loss from pipes.

Set up multiple initial conditions, to represent minimum and maximum

operating conditions to examine valve positions, turndown on heaters,

stability to system noise.

Look at single disturbance scenarios such as heater trip, valve trip and

assess affects on pressure and temperature.

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Page 11: Case Study: Natural Gas Letdown Reliability

Example Scenario – Back up Preheater Changeover

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Verify that electric heater picks

up the temperature on loss of

steam before low temperature

trip activates

Page 12: Case Study: Natural Gas Letdown Reliability

Example Scenario - Disturbance on Turbine Stream

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Pressure recovers on parallel control valve

for fuel gas stream after initial drop

Turbine stream peaks but does not trip on

flow disturbance

Page 13: Case Study: Natural Gas Letdown Reliability

Summary

Complete redesign of natural gas let down and distribution system

including a full concept study, design basis and detailed process design

Developed a dynamic model that demonstrated high reliability for a

variety of plant disturbances under different modes of operation without

the need to perform actual plant trials

Dynamic model informs the commissioning team of controller settings,

and operating conditions

Costly LPG backup system was removed saving £3M/year

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Page 14: Case Study: Natural Gas Letdown Reliability

Summary

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Consultancy.

Project Delivery.

Innovation.

Please get in touch to find out how we can help your

business today.

E: [email protected] W: flexprocess.co.uk

T: +44 1454 629 689