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AKSHAY S KRISHNA
VNIT Nagpur
Sewa Hydroelectric Project (120 MW) is
located in Kathua district of Jammu and
Kashmir
J&K region is situated in foot-hills of
Himalayas where igneous rocks are abundant
Sewa river istributary to mighty Ravi River
The 53m high concrete gravity dam near
village Gatti aims at generating 120MW
electricityA 298 m long 6 m horse shoe
shaped concrete lined tunnel was
constructed for this HYDEL project
10.02km m long Head Race tunnel of 3.30m
Horse shoe including under ground pressure
tunnel-3nos with 2.4m in dia, 380m long and
vertical pressure shaft 622m with surface
penstock length of 175m and…
A diversion tunnel 6m dia and 298mm long
was constructed on right bank to facilitate
construction of Diversion Dam. Diversion
tunnel was designed to take even the flood
discharge
This tunnel though not very long in length
had typical design having two horizontal
bends.
Tunnel was passing through granite stone and
having seepage at various locations.
The tunnel was bored by conventional
drilling and blasting method by using full
face method.
SEWA PROJECT LAYOUT
Drilling activity was the most critical activity
since the rock encountered was very hard
and only one face was available for boring.
Consumption of drill rods was bit high
Drilling and blasting pattern asadopted is
shown in Fig
Blast hole drilling was initially planned by
drilling jumbo but later changed to high
speed jack hammers Atlas Copco make.
Actual penetration achieved on this rock was
0.25m/min.
Maximum pull in hard rock strata was
achieved 2.8m. It was decided not to drill
holes more than 10’ depth to avoid wastage
of time and money
Assumed average life of drill rod in tender
was 200m but actually achieved at site was
only 180m.
Grinding of drill rod was very important in
this type of rock.
Electric cup type grinder was used and
performance of this grinder found very
satisfactory.
To minimize the cost, rebitting of drill rod
was done locally and this experiment proved
very successful
Charging pattern was in accordance with the
wedge cut, drilling and blasting pattern
Modification in charging was that two
numbers primers were used in cut holes.
Due to hard rock, power factor was also
high. It was varying from 1 to 2 kg/m3.
Power gel 901 explosive with long delay
detonators were used
1. Survey and profile marking - 0.50 hours
2. Drilling - 2.00 hours
3. Charging & blasting - 1.00 hours
4. Defuming - 0.5 hours
5. Scaling/Mucking and
bottom cleaning - 4.5 hours
Rock support/Shotcreting - 2.5 hours
Total cycle time - 11.00 hours
Add for unforeseen - 1.00 hour
- 12.00 hours
Defuming system at this site was working all
right.
Sucking system ventilation was adopted and
proved to be effective.
Two units of 45kWx02, having dia .750mm
fans were installed at portal with 1000 mm
dia flexible duct