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Well Control DW Step Up Steffen S Kristiansen / Thomas Nilsen, October 2017 2 oktober 20 Classification: Open © Statoil ASA

Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

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Page 1: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

Well Control – DW Step UpSteffen S Kristiansen / Thomas Nilsen, October 2017

2 oktober 2017Classification: Open

© Statoil ASA

Page 2: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

Long term competitiveness Organisational capabilitiesSafety and security

2 oktober 20172 Classification: Open © Statoil ASA

Page 3: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

Understand trends

2 oktober 20173 Classification: Open © Statoil ASA

Page 4: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

2 oktober 20174 Classification: Open © Statoil ASA

Page 5: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

TUBING CUT

1

4

5

6

7

3

2

Well control incident

Operation with course of events:

• When connecting Pulling Tool to TH: TH was unlocked and string jumped 5 - 6 m due to HC gas trapped below.

• Seawater in marine riser evacuated to the rig floor.

• Closed Annular Preventer (AP) (6) and Blind Shear Ram (BSR). BSR closed on TH and did not shear string.

• Well filled with gas from reservoir to AP.

• Well killed by bull heading

Reason for events:

• It is assumed that FCV’s (1) unintentionally opened during BOP connector pressure test (4).

• Poppet valves on top of the TH were exposed during connector test, and pressure was transmitted down the control lines, potentially cycling FCV’s to 100% open position.

• Gas from the reservoir migrated into the well and was trapped below TH and shallow set plug in the tubing until the incident occurred.

Location: Block 31/2

Rig type: Semi Submersible

Well type: P&A – Multi lateral well

Date: 15.10.2016

Level 1

TUBING CUT

1

4

5

6

7

3

2

Learn from details

2 oktober 20175 Classification: Open © Statoil ASA

Page 6: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and

Risk assessment in planning phase

Handling of risks in execution phase

Indication of well control incident

Handling of influx/kick situation

Competence and training

• WCR - identified and measures addressed *• WCR - awareness among all relevant personnel• QC of swab calculations

• WCR – Morning meetings , DOP arenas, Tool Box talks• WCR - always to be reviewed as part of MOC**• Be open to weak signals

• Volume control• Circulate bottoms up if doubt about downhole situation• Listen to other’s opinions• Worst case approach until else is proven

• Updated Kill sheet • Onshore support available on short notice – Emergency team • Clarify Roles and responsibilities

• Well control certification (IWCF) & Well integrity seminars• Periodic exercises (Drills)• Table tops and simulator training • Experience sharing and learning (One pagers/Safety flash)

Stepping up Well Control DW

2 oktober 20176 Classification: Open © Statoil ASA

Page 7: Well Control DW Step Up - Petroleumstilsynet - Forside 2017/Ptil... · Well Control –DW Step Up ... •Gas from the reservoir migrated into the well and was trapped below TH and