50
Vol. VII. No.2 Editor : B.S. Tomar April 2008 Editorial Nuclear reactor is a complex system with variety of materials (fuel, clad, coolant, moderator, etc.) under different conditions of pressure, temperature and concentration. Chemical behaviour of nuclear materials, particularly those which come in contact with water under hostile conditions, has a profound effect on the health of the reactor. It determines the extent of wear/ corrosion of the reactor components as well as the radiation levels on out of core system (PHT, moderator pipelines). It is, therefore, of prime importance to understand the water chemistry related to operating nuclear reactors. The present bulletin is aimed at putting together the knowledge and experience on water chemistry in one place. This will enable the budding young reactor chemists understand complex issues related to water chemistry and at the same time the radiochemistry fraternity might focus their efforts towards some of the challenges being faced by the station chemists, like the 124 Sb problem. I thank Dr. S. Velmurugan to have agreed to be the guest editor of this bulletin. I am grateful to Dr. S.V. Narasimhan, who was the main source of strength behind this bulletin, to write the FOCUS. CONTENTS From the Secretary’s Desk 94 Focus 97 Guest Editorial 98 Chemistry in the Operation 99 of Nuclear Reactors S.V. Narasimhan Chemical Decontamination Strategies 104 Dr. S. Velmurugan Removal of Turbidity from Coolant 114 Systems using Electrochemical Filtration G.Venkateswaran and A.G. Kumbhar Corrosion of Primary Heat 125 Transport System Carbon Steel Material in PHWR Hariharan Subramanian Role and Responsibilities of a 132 Station Chemist in a Nuclear Power Station – A Perspective K.S. Krishna Rao Gamma spectrometric measurements 136 on PHT and Moderator systems of PHWRs B.S. Tomar, Sumit Kumar, T.P. Chaturvedi and V.K. Manchanda Roundup 142

Vol. VII. No.2 Editor : B.S. Tomar April 2008 CONTENTS · the corrosion products. Activation of the transported corrosion products by the neutron flux in the core generates the radioactive

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Page 1: Vol. VII. No.2 Editor : B.S. Tomar April 2008 CONTENTS · the corrosion products. Activation of the transported corrosion products by the neutron flux in the core generates the radioactive

Vol. VII. No.2 Editor : B.S. Tomar April 2008

Editorial

Nuclear reactor is a complex system with

variety of materials (fuel, clad, coolant,

moderator, etc.) under different conditions of

pressure, temperature and concentration.

Chemical behaviour of nuclear materials,

particularly those which come in contact with

water under hostile conditions, has a profound

effect on the health of the reactor. It determines

the extent of wear/ corrosion of the reactor

components as well as the radiation levels on out

of core system (PHT, moderator pipelines). It is,

therefore, of prime importance to understand the

water chemistry related to operating nuclear

reactors. The present bulletin is aimed at putting

together the knowledge and experience on water

chemistry in one place. This will enable the

budding young reactor chemists understand

complex issues related to water chemistry and at

the same time the radiochemistry fraternity

might focus their efforts towards some of the

challenges being faced by the station chemists,

like the 124Sb problem.

I thank Dr. S. Velmurugan to have agreed

to be the guest editor of this bulletin. I am

grateful to Dr. S.V. Narasimhan, who was the

main source of strength behind this bulletin, to

write the FOCUS.

CONTENTS

From the Secretary’s Desk 94

Focus 97

Guest Editorial 98

Chemistry in the Operation 99of Nuclear Reactors

S.V. Narasimhan

Chemical Decontamination Strategies 104

Dr. S. Velmurugan

Removal of Turbidity from Coolant 114Systems using Electrochemical Filtration

G.Venkateswaran and A.G. Kumbhar

Corrosion of Primary Heat 125Transport System Carbon Steel Material in PHWR

Hariharan Subramanian

Role and Responsibilities of a 132Station Chemist in a Nuclear Power Station – A Perspective

K.S. Krishna Rao

Gamma spectrometric measurements 136on PHT and Moderator systems of PHWRs

B.S. Tomar, Sumit Kumar, T.P. Chaturvedi and V.K. Manchanda

Roundup 142

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Dear Members

Your association has initiated the process to elect the 10th Executive Committee for the period 2009-11. In view of the enthusiasm shown by members to be a part of the association to render their expertise and services,there is a contest for the membership in the Executive Committee.

The Chapter at Tarapur has become a reality on September 27, 2008. Our members at the centre havealready drawn a programme to attend to the requests from various institutes in the vicinity of Tarapur byconducting a one-day workshops and help in meeting the objectives of the association in spreading theawareness about the subject of Radiochemistry and Applications of Radioisotopes for societal benefits. It isheartening to note that members from NPCIL at Tarapur have evinced keenness to support the activities of theassociation.

The Indo-US agreement has brought a bizarre of buoyancy in many premier academic institutes in Indiathat impelled to launch new courses allied to Nuclear Technology while seeking support from the Departmentof Atomic Energy. Thanks to various reports that appeared in a section of newspapers on the entire gamut ofthe deal, many schools and colleges have written to IANCAS to conduct Workshops in and around Mumbai.Our Southern Chapter has broadened its base to cater to many such requests in the Southern Regionparticularly in Andhra Pradesh and Karnataka. This sudden surge in the requests from the academia makesthe activities of our association more meaningful and responsible.

I must admit that the Editorial team of the association is working hard to bring out the bulletins on timeand also to fill the accumulated delay. So far IANCAS has brought out 40 thematic bulletins on topics ofcontemporary relevance to the subject of Nuclear Technology and most of them are available in downloadable

form in our website www.iancas.org.

IANCAS has conquered a mile stone in organizing a Workshop in Imphal, Manipur University againstmany testing security conditions that are prevailing in that part of the country. IANCAS compliments theauthorities of the BARC for the encouragement and all the resource persons who have conducted the workshop with zeal and sense of duty.

G.A. Rama Rao

April 2008 94 IANCAS Bulletin

From the Secretary’s Desk

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Water Chemistry in Nuclear Reactors

Guest Editor

Dr. S. Velmurugan Water and Steam Chemistry Division,

BARC Facilities, Kalpakkam

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Water cooled nuclear power reactors accounts for a significant percentage of electricity generated in theworld. Chemistry plays an important role in the operation and maintenance of these water cooled nuclearpower reactors. In these reactors, water plays several roles. It acts, as a moderator to slow down the fissionneutrons, as a heat transfer fluid to transfer the fission heat to the steam generator to raise the steam, as steamto run the turbine and as cooling water in the condenser that dissipates the heat to the environment. InPressurized Heavy Water Reactors (PHWRs), the mainstay of Indian nuclear power program, heavy water

(D2O) is used as moderator as well as primary coolant. The primary heavy water coolant transfers the fissionheat from the fuel bundles to the light water in the steam generator. The steam generated in the steam generator turns the turbine generating the electricity. The steam coming out of the turbine is cooled by the cooling waterin the condenser. The cooling water is sourced either from the sea or a river or lakes. The quality of water usedvaries from system to system. In the moderator system, the heavy water coolant is maintained under neutralcondition and at a conductivity of < 1 µS/cm. The primary heavy water coolant is maintained under alkalineand de-oxygenated condition. All volatile treatment is followed in the secondary light water coolant. As thetertiary coolant system viz. the cooling water is sourced directly from the natural water bodies, it contains allthe inorganic, organic and biological materials that are normally expected from these water sources.Similarly, the operating conditions of the various coolant systems also vary from system to system. The primary

coolant is operated at 290-320oC and at high pressure of 90-100 kg/cm2 pressure. Where as, the process waterand cooling water systems are operated at close to ambient conditions. In addition, the nature of the problemsencountered also vary from system to system. In the primary coolant system, the major problem is radiationfield build-up which arises due to the interaction of water coolant with the system structural materials formingthe corrosion products. Activation of the transported corrosion products by the neutron flux in the coregenerates the radioactive contaminants which in turn causes the radiation field and exposure of operatingpersonnel to the radiation field. As this problem is unique to the nuclear power industry and as the industry hasthe mandate to keep the radiation exposure 'As Low As Reasonably Achievable’ (ALARA), all efforts are beingmade to control the radiation field as much as possible. Similarly, corrosion of reactor coolant system is ofconcern to the nuclear power industry. As corrosion manifests in several forms and as all forms of corrosionare detrimental to the system, effort is made to keep the corrosion to the minimum. In addition, depositaccumulation in any part of the system especially on heat transfer surfaces is undesirable and should beprevented. It is good that Indian Association for Nuclear Chemists and Allied Scientists (IANCAS) is bringingout a special bulletin to highlight the importance the water chemistry in the efficient running of nuclear powerstations.

IANCAS Bulletin 97 April 2008

FOCUS

Dr. S.V. NarasimhanAssociate Director, Chemistry Group &

Head, Water and Steam Chemistry Division,BARC Facilities, Kalpakkam

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The article on “Chemistry in operation of nuclear reactors” deals with the management of chemistry indifferent water circuits of water cooled nuclear reactors. The efficient management of chemistry domainaddresses reduction in rate of radiation field build up in the primary coolant circuits, minimizes radiolyticdegradation in moderator and ensures SG tube integrity while inhibiting primary coolant leaks. Several ofthese control measures happen by good chemistry specification based on action levels.

The article on “Corrosion of Primary Heat Transport system carbon steel material in PHWR” deals withthe mechanism of activity transport in water cooled nuclear reactors. This is the only problem of seriousconcern in nuclear industry which has a direct link to man-rem budget, In international scene, every effort ismade to have as low a man-rem exposure budget as possible per reactor per year. The paper discusses newmethod of radiation field control measures like metal ion passivation. The recently encountered problem offlow accelerated corrosion is also discussed.

The article on “Chemical Decontamination Strategies“ discusses the methods of chemicaldecontamination successfully developed and applied in Indian PHWRs. Not only it elaborates the basis ofinitial process development but also it mentions some of the improvisations carried out to better theperformance. Article also deals with two unique problems namely removal of stellite particulate activity frommoderator system of PHWRs and removal of 124 ,122Sb from PHT system of PHWRs.

There is an interesting article entitled “Role & Responsibilties of a station chemist in a nuclear powerstation – a perspective” in this issue from a Station chemist who is entrusted with a job maintaining goodwater chemistry domain while complying with an uninterrupted operation of the reactor within the allowedtechnical specification. Very clearly the job is of multidisciplinary nature and the task requires instantbalanced judgment to implement corrective actions quickly while not compromising the plant life. Stationchemist not only ensures efficient and safe operation but also ensures Plant Life Extension.

Another article dealing with “Removal of Turbidity from coolant systems using ElectrochemicalFiltration”, describes a new method of turbidity removal employing physical filtration and charge basedretention under an applied voltage. While the former is attributable to large surface area provided by thecarbon felt, the latter is clearly due to charge carried by the particulates in the medium. The pressure drop, amain constraint in filters, is no longer a problem in the new technique. It has versatility in application. It cantackle turbidity and near nano levels, be it from iron, silica, antimony, indium etc and can be used in any of thewater circuits from primary to tertiary !

Happy reading

April 2008 98 IANCAS Bulletin

Guest Editorial

Dr. S. Velmurugan

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Chemistry in the Operation of Nuclear Reactors

Introduction

Water cooled nuclear power reactors are ingeneral prevalent all over the world. They have beenproducing power very effectively and economically. Water, in its pure state, is used for transferring theheat generated in the core to the turbines to produceelectricity. The properties of water are considerablyaffected not only by the high temperature but also bythe radiation field. Nevertheless, the interaction ofmaterials with water at high temperature is enhancedconsiderably. In addition, the radiolytic degradationof water and radioactivation of the corrosionproducts that is transported by the coolant water adds another dimension to the electricity generationscenario. In this paper, the water chemistry domainsemployed in NPPs are discussed with possiblemethods of control.

Primary heat Transport System (PHT)

The primary objective of the heat transportsystem is to transfer efficiently the heat generated inthe core of the reactor by fission process to the steamgenerator. In PWRs and PHWRs the heat is pickedup by water in single phase (liquid water) in thetemperature range of 245°C to 310°C. Thetemperature dependence of specific heat of waterallows maximum useful extraction of heat in thistemperature range (Data). Natural interaction ofmetallic elements present in the alloys constitutingthe structural materials in the PHT system with thecoolant water produces corrosion products andH2(g). Metal oxidation occurs with a corresponding

complementary cathodic reduction of H+ orDissolved oxygen. The metallic ions so producedgenerally belong to the transition metal category.They are readily hydrolysed in the water mediumand converted to insoluble metal hydroxides,oxy-hydroxides and oxides, which are termed ascorrosion products. Many of these chemicalreactions are kinetically enhanced by thetemperature prevailing in the coolant. The thermalstability of the corrosion products is primarilydictated by the Pourbaix diagram. Their relativestability is thus decided by thermodynamics thoughseveral other factors like kinetic and hydrodynamicparameters also play a significant role. Since thecorrosion products are insoluble and are produced atextremely slow pace, they remain in suspended

particulate form in the size range 0.1 to 2 mm with a

maximum around 0.3 mm. The distribution ofparticle size is controlled by size dependent removalby filtration and surface deposition.

It is also well known now that aqueous hightemperature metal oxidation leads to the formationof two layers of oxide under quiescent or normalflow conditions. At the metal water interface, metalgets oxidized to oxide and released partly as metalion to the coolant fluid. Across this in-situ formedoxide layer (called inner layer) there is a constanttransport of metal ions outward and oxide ionsinward. The relative rate of such ion transfers has arole to play in deciding the porosity, protectivity andstructure of the oxide. It is matter of debate and

IANCAS Bulletin 99 April 2008

Dr. S.V.Narasimhan, Associate Director, Chemistry Group and Head, Water and Steam Chemistry Division, BARC Facilities,Kalpakkam, Tamil Nadu 603 102; E-mail:

Dr. S.V. Narasimhan Joined BARC in 1971, after Post Graduation in chemistry fromMadras Univ. (1970). He did his Ph.D. (Phys.Chem.) in 1981 from Bombay University.He is presently the Associate Director, Chemistry Group and is also the Head, Waterand Steam Chemistry Division, BARC Facilities, Kalpakkam, Tamil Nadu 603 102. Inaddition he is also Chairman of a DAE advisory Committee On Steam & WaterChemistry (COSWAC). His areas of specialisation are High temperatureelectrochemistry, Dilute chemical decontamination, Activity transport and surfaceanalysis, Water chemistry, and Thermal ecology. He has 90 Journal papers apart fromseveral presentations in symposiums. Presently he is guiding six PhD students inMadras University and in HBNI.

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mechanistic quantification as to whether thetransport of the ions is decided by pore or grainboundary route. Nevertheless the transport doesoccur which keeps the inner oxide under dynamicequilibrium.

The outer layer of oxide over the metal isformed essentially by precipitation due to solubilityand is also driven by forces of particle adhesion.There is a dynamic equilibrium between dissolvedmetal ions, suspended particulate oxides anddeposited oxide.

It is this dynamic equilibrium which is a causefor concern in a nuclear power plant (in comparisonto a thermal power station). In the core of the reactorwhere fission produced heat is released, both

thermal and fast fission neutrons are present (ff, Ef,

ft, Et). The corrosion product ions and particulatespresent in the coolant reside in the core region fordefinite time period repeatedly. In this process, thenuclides of the metallic elements undergo nucleartransformation resulting in radioactive elements.Such transformation combined with the dynamicequilibrium described earlier results in the spread ofcontamination of out of core surfaces. As these

nuclides are both b and g emitters with varying t½ and Energy of the radiation, they have a significantimpact on the man-rem problem faced by the powerplant.

Antimony present in some of the fuel surfacesand pump seals in the heat transport system getsreleased due to mechanical wear. As the antimonychemistry is quite complex, its removal from coolantbecomes very difficult. Majority of the inventory ofantimony resides in the core on zircaloy surfaceduring regular operation of the reactor. Duringshutdown and start-up, there is sharp release ofantimony activity. It is known that there is oxygenexcursion in the coolant along with temperaturefluctuations during these periods. The radioactiveantimony (122Sb, 124Sb) so released from the coregets easily deposited on out-of-core surfaces if notremoved effectively by specific ion exchangers.This problem has been encountered in severalPWRs. Specific shut down procedures have beenworked out to minimize the release of radioactiveantimony. which Prior to shut down, injection of

oxygen is carried out in the PHT system, followed by ion exchange removal of antimony.

In PHWRs also antimony problem hassurfaced in reactors which used antimony as alloyelement in moving parts. This problem is yet to beaddressed fully in PHWRs. During full systemchemical decontamination of PHWRs antimonyproblem had surfaced which further enhancedradiation field on out- of-core surfaces due toselective deposition on carbon steel pipes. Modifiedprocedures have been evolved to address this issue.

The Chemistry of the coolant fluid in theprimary heat transport system is maintained in thealkaline medium with lithium hydroxide. Thedissolved oxygen in the water produced byradiolysis is kept under control by use of Hydrogengas externally added to the system. The structure ofdifferent corrosion products present in the coolantsystem surface is altered significantly by variation inthe concentration of dissolved hydrogen and H+. The dependency is represented by the followingequations.

Fe2+ + 2OH- ® 1

3Fe3O4 +

2

3H2O

While the general corrosion is kept at minimum by the alkaline pH conditions, the transport andredistribution of corrosion products are not easy tocontrol even though chemistry specifications aremaintained within the specified ranges. This isattributable to the non-isothermal conditionsprevailing in the PHT circuit. Compromising allthese aspects, optimum pH region for the circuit isarrived at and it would ensure that inside the core theresidence time of the corrosion products can be keptto minimum.

There is an alternative route to improve theprotectivity of the oxide over structural materialssurface. This is called metal ion passivation (MIP)technique. Selected metal ion is injected at very lowconcentration in the coolant. As the protective oxidelayer is formed, these ions alter the structure of bothinner and outer layer of the oxide. The transport ofmetal ion across by these oxide layers is thushindered. In fact the origin of this technique istraceable to the behaviour of GE BWRs employingZn as alloying element in condenser tubes. The

April 2008 100 IANCAS Bulletin

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corrosion caused by condensate released ppb levelsof Zn which upon incorporation in the protectiveferrite/ chromite film rejected the Co activity.Nevertheless the mechanism of this technique inactual reactor system is not very clearly understood.

In the presence of radiation, the coolant waterundergoes radiolytic de-composition producinghydrogen and oxygen as molecular products besidesseveral oxidising and reducing radicals. The extentof the formation of molecular products is alsodependent on partial boiling in the core near metalsurfaces and the extent of stripping due to gas phaseexchange and ion exchange purification. Metal -water reaction also produces hydrogen to someextent at elevated temperature which may besignificant only in PHWRs as carbon steel is used asthe major construction material.

Moderator System

The objective of moderator system is tothermalise the fission neutrons and also to removeheat deposited in the moderator. While in PWRscoolant acts as moderator also, in PHWRs these twosystems are well separated in terms of design. Thisstructural material of the moderator system isstainless steel and the calandria tubes are made ofzirconium alloy. The total inventory of themoderator is residing in the core and interacts withthe neutron. Thus the radiolitic degradation of themoderator is also significantly high. The radiolysisproducts are hydrogen and oxygen which get stripedinto cover gas prevailing over the moderator. Thecover gas acts as transporting medium for themolecular products hydrogen and oxygen. The gases are recombined over palladium loaded aluminacatalyst. The cover gas also prevents entry ofmoisture and oxygen into the moderator. Themoderator system is operated between 50ºC and70ºC. Considering the above physical and chemicalfeatures of the moderator system, the pH ofmoderator system is maintained in the neutralregion. At low temperature and in neutral pH the SSis fully compatible. The addition of any type of pHmaintaining agent is not desirable from the point ofview of radiolysis.

In several PHWRs, no specific issue hassurfaced in the moderator circuit. Ingress of nitrogen and oxygen(air) in cover gas, ingress of carbon

(ingress of ion exchange fines) and ingress ofcooling water impurities degrade the chemicalquality of the moderator system. The specificconductivity of the moderator system is thus

maintained at <1 mS/cm to ensure that there are noharmful impurities in the system.

In a few selected PHWRs, due to mechanicalinteraction of stellite ball bearings present in theadjuster rod control mechanism, stellite powder gotintroduced into the moderator system. As the Coparticulates circulated through the neutron zone inthe core, 60Co was produced. This radioactive cobaltgot deposited in low flow areas as particulatesresulting in high radiation fields. This problem wasaddressed by two methods:

1. Removing stellite containing ball bearings andreplacing for non-stellite alloys.

2. Remove the existing radioactive deposits bychemical cleaning at low temperature.

Steam Water System

The steam required for turning the turbine isproduced in the steam generator by using the heatfrom the primary heat transport system. Thetemperature domain of the secondary circuit ranges

from 45°C (in condenser) to 110°C (in deaeartor)

195°C (in final feed water entering the SG. In

addition the steam is raised at 250°C and 40 kg/cm2

pressure. The SGs produce saturated steam with anatural recirculation of water. The steam is dried(<0.5) and sent to Turbo Generator (TG) set forpower production. The materials in the secondarycircuit consist of SG tubes (made of monel/ incoloy/inconel 690 TT), carbon steel piping, feed waterheater tubes (Stainless steel) and condenser tubes(SS, Ti, Al-brass- admiralty brass etc). Thechemistry of the secondary circuit is maintainedunder alkaline reducing environment using volatileamine (Ethanolamine-ETA and hydrazine-N2H4).Over years of operational experience, it is learnt thatthe use of all volatile amine treatment is better toprotect the water and steam circuits of the secondarysystem.

The pH is maintained by the hydrolysisreaction of the amine giving rise to OH-. Since theamine is a weak base, there is an equilibrium existing between the free amine and the dissociated form.

IANCAS Bulletin 101 April 2008

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The free amine reacts easily with acid (generated byingress of impurities or by thermal hydrolysis oforganics) to produce amine salt which alters the pHof the medium as per the BL-equation. The aminehas a definite distribution coefficient between steamand water. The condensate contains varying amountof amine depending on the location in the SG circuit.This offers protection to the structural material in thesteam circuit as well. The hydrazine is added at theboiler feed pump suction to provide reducingatmosphere and to remove traces of dissolvedoxygen from the system. Excess hydrazine couldthermally decompose to ammonia and enhance thepH of the system in addition to the role played by theamine. The mixture of ammonia and amine will havea different impact in the condensation along with thefirst drop of water in the steam circuit.

The integrity of the SG tube is very importantin nuclear reactors because it acts as a boundarybetween the radioactive primary coolant and theenvironment. Due to the steaming on the secondaryside of the SG tubes, large amount of salts getdeposited on the tubes, tube sheets etc. Such coatingformation is deleterious to the heat transfer processand can result in excess localised attack on SG tubesresulting in catastrophic failures. In order to preventsuch deposit formation ingress of cooling water inthe SG circuit is to be totally avoided or thecondensate should be fully purified by ion exchangeprocess. In addition soluble corrosion product ironcan get generated in the steam- water circuit andhence iron can find its way into the SG tube. It willfurther complicate the deposit formation on SGtubes and tube sheets. Hence iron input to SG is avery important parameter that should be kept to aminimum at all times.

Blow down of SG water reduce sludge buildup. However, it results in loss of heat and purifiedwater. Hence both heat and the water are recoveredin boiler blowdown recovery system. Similarly theuse of full flow condensate polishing unit forpurifying the condensate free of soluble impuritieshas been quite successful in preventing the entry ofsalts. However, the regeneration methodologyemployed in the condensate polishing units has itself introduced some slip of low concentration ofchloride or sodium. Better methods are nowavailable for preventing such slips of Cl- and Na+.

Chemistry control specification

The management of chemistry parameters inthe primary and secondary circuit of nuclear reactors is very critical for the efficient and economicoperation. This carries additional significancebecause of the fact that the primary coolantcontaining radioactivity should be contained at alltimes and can not be allowed to escape toenvironment from radiation hazard point of view.The chemical constituents are of many types asdetailed below:

1. Intentionally added chemical to maintain acertain chemistry domain;

2. Impurities entering into the system due toingress of process cooling water, ion exchangeresins, oils, etc

3. Impurities generated in the system due toradiolysis

4. Impurities generated in the system due tocorrosion of materials

Some of these parameters are of immediaterelevance to safety of the plant and personnel whilesome of the parameters may have long termimplication on the life of the reactor components.The variation in the concentration of the parametersin reactor systems occur at different rates dependingupon several factors involved in the operation.Similarly the control of these parameters within apreferred domain is also expected to take a definiteduration as the system is designed essentially tooperate for power production and not for containingthe impurity ingress. Considering these aspects thetechnical specification has been arrived at. Theparameters are divided into control parameters anddiagnostic parameters. Control parameter is onewhich decides whether the reactor should continueoperation at full power or not when it is found to beoutside a normal range of values (NRV). When thevalue of the control parameter is outside the NRV,the value is expected to fall in any one of the threeaction levels. The action level (AL) prescribes acertain band width for the magnitude of the chemicalparameter which is also associated with a certainallowable time span. The combination of AL and Tis so chosen as to minimize the deleterious impact ofthe impurity on the structural material. Similarly theaction level 2 and 3 are designed followed by a

April 2008 102 IANCAS Bulletin

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direction to shut down the plant. The details aregiven below:

Action Level 1

In this action level, damage to the system canoccur over a long period of operation. Hence actionis to be initiated to improve the chemistry in areasonable time mentioned therein. Samplingfrequency should be increased as deemed fit.

Action Level 2

Damage to the system can occur to a certainextent as a consequence of operation in this actionlevel. Hence prompt action is necessary within theduration specified. The corrective action should besuch as to restore the value of the parameter to NRV.A technical review of the incident should bedocumented. An incident report should be preparedand discussed at SORC. Sampling frequency shouldbe increased as deemed fit.

Action level 3

It is not advisable to prolong the operation ofthe plant, if the value of the chemical parameter is inthis action level. For parameters related to safety,action is to be initiated to lower the power and shutdown the reactor within 4 hours. For other controlparameters, where shut down (S/D) has not beenspecified, action should be taken to bring the valuesto action level 2 within 24 hours, otherwise actionshould be initiated to shut down the reactor withinthe next 4 hours. However, if there is a significantimprovement in these chemical parameters towardsNRV, during the process of shut down, poweroperation can be continued. Technical review of theincident should be documented and discussed inSORC/COSWAC.

In general chemistry related failures do notsuddenly cause collapse of the structural integrity ofthe system except in cases like stress corrosion

cracking and the like. Hence there are no scramsproposed upon violation of chemistry parameters.Only planned shutdown is recommended. It isexplicitly known that the field experience, R&D data and operating constraints have together led to theabove classification. The action levels betweenNRV and S/D are on the conservative side andprovide enough breathing t ime for theimplementation of corrective actions.

Several chemistry parameters are inter-relatedand some of them are designated as diagnosticparameters. Usually the parameter which has highest sensitivity and quickest to respond to a perturbationis chosen as control parameter while the associatedparameters are chosen as diagnostic parameters.Diagnostic parameters usually have only one rangeof values.

Conclusion

The chemistry domain of the operating nuclearpower plant is complex because of the temperaturedomain, variety of materials of construction, natureof the coolant and the radiation field. Yet,management of the chemistry is made possible so asto operate the reactors effectively. Constantimprovements in the chemistry controlspecifications are needed because of the improvedunderstanding of the processes, materials anddesign. Specific problems encountered in operatingnuclear reactors are due to unusual material,improper operating procedure etc. Most of theseproblems can be solved easily with a betterunderstanding the chemistry of the domain and alsothe design of the operating plant. The prevailingconditions in India have so far led to successfuloperation of all nuclear power plants without anyserious failures traceable to any violation inchemistry domain. In several cases the plant lifeextension is also made possible by maintaining goodpractices.

IANCAS Bulletin 103 April 2008

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Chemical Decontamination Strategies

Introduction

The term `Radiation’ is synonymous with`Nuclear’. Radiation field builds up in the nuclearcoolant systems of nuclear reactors and causesexposure of personnel to radiation. Efforts are beingmade world over to reduce the radiation field thatbuilds up in the reactor coolant systems. Radiationemanating from the fission of uranium and the decayof fission products are contained very well within the core by the multi level shielding provided to thecalendria / reactor vessel. Thus, the radiation fieldobserved around the coolant system arises mainlydue to the radioactive contaminants deposited ontothe out-of-core surfaces such as coolant systempiping, pumps and steam generators etc. Depositionof radioactive contaminants takes place due to thetransportation of corrosion products into and out ofthe reactor core. These corrosion products are maderadioactive by the neutron flux present in the core.Fission products escaping the failed fuel elementscontribute to some extent to the radiation field.Hence, the major contribution to the radiation fieldarises from the neutron activated corrosion products. Stainless steel, Inconel-600, Inconel-690,Incoloy-800, carbon steel, zircaloy-2 / 4 andZr-2.5%Nb alloy are the major alloys used in the

reactor coolant system. These structural materials ofthe reactor coolant system are made of iron, nickel,chromium and zirconium. Few reactors in the worlduse copper containing Monel-400 as steam generator tube material. Alloys containing cobalt such asstellite were used earlier as wear resisting materialsin valves. All the above alloys interact with the hightemperature (upto 320oC) water present in thecoolant system and forms oxides (Fe3O4, Fe2O3,NiFe2O4, FeCr2O4 etc.) of elements constituting thealloys. The composition and nature of the oxidesformed on the structural material surfaces of thecoolant system depends on two main factors i)material composition of the structural material ii)chemistry of the water coolant. The corrosionproduct oxides thus formed on the surfaces of thestructural materials incorporate the radioactivenuclides transported by the coolant by processes ofadsorption, absorption and by chemical reaction.Among the several radioactive contaminants present in the system surfaces 60Co, 59Fe, 54Mn, 51Cr, 58Co,124Sb and 110Ag are important as they have relatively

long half lives and the g-rays emitted by them arehaving energy sufficient to penetrate the thickness of pipes to cause exposure of personnel manning thepower plant to radiation. These radio active isotopes

April 2008 104 IANCAS Bulletin

Dr.S.Velmurugan, Water and Steam Chemistry Division, BARC Facilities, Kalpakkam, Tamil Nadu 603 102; E-mail: [email protected]

Dr. S. Velmurugan of Water and Steam Chemistry Division, BARCF, Kalpakkamobtained his M.Sc(Chemistry) from Madurai-Kamaraj University and Ph.D fromUniversity of Madras and joined BARC through 28th Batch of training school. Since1985, he has been carrying out R&D activities in the field of water chemistry asrelevant to Pressurized Heavy Water Reactors(PHWRs). The objective of the workprogram is to control the radiation field built-up in the reactor coolant systems ofIndian nuclear reactors. Extensive work to understand and optimize a chemicalprocess for the decontamination of reactor coolant systems of PHWRs were carriedout. This includes studies on oxide/oxide film dissolution, ion exchange studies withmetal ions, activities and complexing agent pick-up on ion exchange resins, studies oncorrosion behavior of reactor structural materials in the chemical formulations usedfor the decontamination, chemical cleaning etc. The chemical process thus evaluatedhas been applied ten times to decontaminate the Indian PHWRs. Currently he isengaged in studies on flow accelerated corrosion and in optimization of waterchemistry to AHWRs. He has 33 Journal papers and 64 International/nationalconference papers to his credit.

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are formed by the following nuclear reactionsinvolving neutron (n) and the parent inactiveisotopes present in the corrosion products:

59Co + n ® 60Co* (t1/2 5.26 years)58Fe + n ® 59Fe* (t1/2 44.5 days)54Fe + n ® 54Mn* (t1/2 244 days)50Cr + n ® 51Cr* (t1/2 27.2 days)58Ni + n ® p + 58Co* (t1/2 70.8 days)123Sb + n ® 124Sb* (t1/2 60.3 days)*indicates radioactive isotope

In recent years, the 124Sb contribution hasincreased especially during shutdown owing to theuse of antimony containing materials as seals andbearings in primary coolant pumps. In addition tothese activated corrosion product isotopes, fissionproducts such as 125Sb, 95Zr, 95Nb, 103Ru, 106Ru,137Cs, 141Ce and 144Ce were also observed in thesystems but their contribution to field is relativelyless (< 10%) as compared to the activated corrosionproducts.

Efforts are being made to minimize theradiation field in the reactor coolant systems ofnuclear power plants by careful selection ofmaterials. As 60Co is the most important radioactivecontaminant because of its long half life (5.26 years)and hard gamma (1.17 and 1.33 MeV) emission,cobalt containing materials such as stellites areavoided and in its place nickel or iron based hardfacing materials are chosen. In addition, the cobaltcontent in the alloys chosen for steam generator tubematerial or the alloy chosen for coolant piping arespecified in such a way that it is kept as minimum aspossible. Similarly antimony and silver containingmaterials are avoided to the extent possible. In orderto reduce corrosion and activity pick-up on thesystem surfaces, some of the PWRs use componentsthat are electropolished to get smooth surface.

The other option available to reduce theradiation field in the coolant system components isoptimization of the chemistry of the coolant which in turn reduces the quantity and/or the release rate ofthe corrosion products. The reducing and alkalinechemistry condi t ions mainta ined in thePHWRs/PWRs primary coolant systems’ ensure theformation of spinal type oxides. The protectivenature of these oxides ensures that the rate of

corrosion decreases as the oxide film grows. InBWRs, even though alkaline conditions are notmaintained, the impurities in the water are kept atvery low levels that corrosion of reactor materialsand coolant system materials ( stainless steel) arevery low. In western BWRs, zinc is added at ppblevels to the coolant that modifies the oxide filmformed over the structural material surfaces makingit more corrosion resistant and adherent. Also, theykeep the coolant condition reducing by addinghydrogen or hydrogen after noble metal treatment.Though hydrogen addition is practiced to preventIGSCC failure of stainless steel, it also enables theformation of protective spinel type oxides on thesystem surfaces.

The efforts taken in choosing the right materialfor construction of coolant systems and inmaintaining the right coolant chemistry have helpedto significantly reduce the radiation field in theout-of-core surfaces of reactor/primary/moderatorcoolant systems of power reactors. But, as far asradiation exposure of plant personnel is concerned,the principle of `As low As Reasonably Achievable(ALARA)’ is followed by the nuclear powerstations. Hence, the stations look for other means tofurther reduce the radiation field. In this respect,chemical decontamination has proved to be an easyand efficient way of reducing the radiation field inthe reactor coolant systems.

Fundamental principle involved in Chemical

Decontamination

Nature of the oxide formed in Structural

Materials

The chemicals added during chemicaldecontamination react with the oxide film present inthe coolant system structural materials’ surfaces anddissolve or dislodge the oxide film along with theradioactive contaminants. The metal ions, crud andthe radioactive contaminants released from thesurfaces are taken out of the system either bydraining the decontaminating fluid and disposing off as liquid radioactive waste (rarely practiced) or bycollecting the metal ions, activities on ion exchangeresins and filters and disposing them as solidradioactive waste. The efficiency with which theradiation field is reduced by decontaminatingreagent depends on so many factors. The most

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important factor is the nature of the oxide film. Inmost part of the system surfaces, the oxide film has adouble layer structure (Fig. 1). The double layerstructure of the oxide film was proposed by Potterand Mann. The oxide film consists of a fine grainedinner layer and a coarse grained outer layer. Theinner layer is grown on oxide and the outer layer isformed by precipitation of the oxides from thecoolant saturated with the dissolved metal ions.Hence, the composition of the oxide between the two layers varies from each other. In multi element alloys such as stainless steel, Incoloy-800, Inconels etc.,the composition varies within the layer itself.

In the case of boiling water reactors (BWRs),the reactor coolant system, the re-circulation lines,the steam generator tube are made of stainless steel.The reactor core is lined with stainless steel. Underthe oxidizing chemistry conditions maintained insome of the BWRs (as in TAPS#1&2), hematite

(a-Fe2O3) is the dominant corrosion product oxide.The top layer is expected to have less chromiumbecause of the continuous removal of chromium(III)in the oxide to Cr(VI) and its subsequent dissolutionby the water medium. However, the inner layer of the oxide film is expected to retain some of thechromium(III) formed by the corrosion process. InTAPS#1&2, it was reported that it contains moreamount of chromium than that was expected for aBWR operated under oxidizing chemistry condition. This was at tr ibuted to the deposi t ion ofchromium(III) formed from the chromate addedduring shut down. However, this observation needsto be established by experimental investigations. InBWRs that adopt Zinc Ion Passivation (ZIP)

technique to reduce radiation field, zinc isincorporated in significant quantities on the oxidefilm making the film thinner and tenacious. In BWRs that follows hydrogen water chemistry with orwithout noble metal(Pt/Ir) chemical addition, theoxides formed are ferrites and chromites. Thethickness of the oxide film is an important parameteras it decides the concentration and quantity ofdecontaminating reagent to be added. Under theoxidizing chemistry and neutral pH condition of thecoolant, the stainless steel surfaces of the BWRs,forms a thick oxide film as hematite is not aprotective oxide. Depending on the duration ofpower operation the thickness of the oxide film can

grow upto 15 mm.

In PWRs and VVERs, the same stainless steel(304 or 316) is used as structural material of theprimary coolant system. The light water coolant inthese reactors is conditioned by alkalies ( LiOH orKOH) to maintain a high temperature pHT of 6.9 –7.4. The concentration of lithium or potassium isadjusted according to the boron concentration to getthe above high temperature pH. In addition, reducing condition is ensured by adding hydrogen (10 – 30cm3/kg) either directly or through the addition ofammonia. Under these conditions a thin adherentoxide film is formed. The oxide film is composed ofmixed ferrites and mixed chromites (Fe(1-x)NixFe2O4, Fe(1-x)NixCr2O4, FexNiyCrzFe [3-(x+y+z)]O4 etc.).

In PHWRs, the mainstay of the Indian nuclearpower program, carbon steel is extensively used. Allthe primary coolant system feeders and headers aremade of carbon steel. The steam generator tubematerial is either Mone-400, an alloy of copper

April 2008 106 IANCAS Bulletin

Fig. 2 Dilute Chemical Decontamination (DCD)ProcessFig. 1 Oxide double layer structure

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(30%) and nickel (70%) or Incoloy-800 (an alloycontaining 32% nickel and 22% chromium andremaining iron). The pressure tube and the fuel cladin the core are made of zircaloy or Zr-Nb alloy. Theheavy water primary coolant, which is maintained atpHa 10-10.5 and hydrogen concentration of 3-10ml/kg, interacts with the structural material formingcorrosion product oxides. As carbon steel has a largesurface area (1500 m2 for 220 MWe PHWRs) andalso because of its relatively high corrosion rate, thecorrosion product formed on the carbon steel viz.magnetite (Fe3O4) dominates the corrosion productinventory in the system. Magnetite is formed by thefollowing sequence of reactions:

Fe ® Fe 2+ + 2 e-

H2O + 2 e- ® OH- + H2

Fe2+ + OH- ® Fe(OH)2

3 Fe(OH)2 ® Fe3O4 + 2 H2O + H2 (Schikorr reaction)

The thickness of the magnetite formed over thecarbon steel under normal flow conditions can bedetermined by the logarithmic rate law. Thickness

values of 20–40 mm have been observed on carbonsteel surfaces that has seen 10 years of operation.Some variation in thickness is expected because ofthe temperature difference within the system. Inaddition, the areas affected by flow accelerated

corrosion would have very thin oxide film (< 2 mm).The double layer magnetite (Fe3O4) film formedover the carbon steel surfaces undergoes dissolutionand are transported as ferrous ions and as magnetiteparticulates and deposited over the steam generatorand zircaloy surfaces in the core viz. fuel andpressure tubes. It has been reported that in nickelbased steam generator tube surfaces, someconversion of the deposited magnetite (Fe3O4) tonickel ferrite (NiFe2O4) is possible. The parent oxide in Incoloy-800 formed at the primary coolantoperating conditions would be the mixed ferrite andchromites (Fe(1-x)NixFe2O4, Fe (1-x)NixCr2O4,FexNiyCrzFe [3-(x+y+z)]O4 etc.), but the x,y,z values aredifferent from that formed on stainless steels.

In all the reactor types zircaloy-2 / 4 or Zr-Nballoys are used as materials for in-core componentssuch as fuel clad, pressure tube/channels etc. Thesezircaloy surfaces also undergo corrosion and form athick oxide film (ZrO2). As the zircaloy components

are inside the core which is heavily shielded, noeffort is made to remove the zirconium oxide film.However, the iron, nickel, chromium oxidestransported to the core and deposited over the ZrO2

film by the coolant require to be removed to avoidre-contamination after decontamination.

Activity incorporation in the Oxide Film

In the primary/reactor coolant systems ofpower reactors the concentration of cobalt ions in the coolant and the percentage composition of cobalt inthe crud or deposits is insignificant as compared toiron, chromium and nickel etc. Hence, the chemicalform in which cobalt is present in the oxide is verydifficult to identify. However, it has been proved that the active cobalt isotope (60Co & 58Co) along withthe inactive precursor can get incorporated in thechromite matrix. Calculation of octahedral sitestabilization energies for Fe2+, Co2+, Ni2+ indicatedthat the cobalt is stabilized in the tetrahedral sites ofthe chromites which has a normal spinel structure.This clearly shows that the cobalt chromiteformation is thermodynamically favourable underthe reactor coolant conditions. In addition to thismechanism of cobalt incorporation in the oxidelattice, other mechanisms such as cobalt adsorptionby ion exchange over the surface hydroxyl groups ofthe oxides which act as inorganic ion exchangers isalso proposed. The cobalt ion initially adsorbed overthe surface can further react and can form part of theoxide. The mechanism of incorporation of 51Cr and59Fe activities in the oxide lattice is obvious.

In view of the high contribution of antimonyactivities during shut down in some of the reactorsincluding PHWRs, the mechanism by whichantimony activities (124Sb and 122Sb (t1/2 2 days) arepicked up on the surfaces of primary coolant systems of PHWRs and PWRs is being debated. Theantimony released from the pump seals and bearingsis transported to the core and gets activated by theneutron flux present in the core. The hightemperature pourbaix diagram indicate that the pHT

and the potential condition of the PHWR primarycoolant lies in the interface between Sb [elemental(metalloid) form] and the Sb3+ form. Hence, theexact chemical form in which it resides in the core isnot clearly established. There are indications that itexists in Sb3+ form either adsorbed or deposited overthe ZrO2 film in the in-core zircaloy surfaces.

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Similarly, the chemical form of antimonyactivities in the out-of-core surfaces is also notknown clearly. Possibility of Sb3+ adsorption onoxides, plating out on carbon steel surfaces andformation of antimony containing iron compound(FeSbxOy) are being postulated.

Chemical dissolution of the oxide

The radioactive contaminants causing theradiation field in the reactor / primary coolant system have got incorporated in the oxide film. Hence, inorder to remove these radioactive contaminants, theoxide film itself has to be removed. This can beachieved by dissolving the oxide film usingchemical reagents. Large numbers of chemicalreagents are used for the removal of oxide film fromthe coolant system surfaces. These reagents aredifferent from the ones used for removing floor orsurface contamination which are meant for theremoval of loosely held contaminants and aresurfactant based. The chemical reagents meant forthe removal of radioactive contaminants fixed ontothe oxide film can be broadly classified into threecategories:

1. Simple acids

2. Reducing agents and/or Organic complexforming acids

3. Oxidizing compounds

Dissolution of Oxides by Acids

Most of the corrosion products in the coolantsystem are iron containing oxides. The ironcontaining oxides can be dissolved by reacting withacids

Fe3O4 + 8 H+ ® Fe2+ + 2 Fe3+ + 4 H2O

Thus, even mineral acids such as hydrochloricacid or sulphuric acid can be used for dissolving theoxide film containing iron. However, consideringtheir high acidity and their incompatibility with theunderlying metal, strong mineral acids are avoided.Organic complex forming acids such as

1. Ethylene di amine tetra acidic acid (EDTA),

2. Nitrilo Tri Acetic acid (NTA),

3. Picolinic acid (PA),

4. Citric aicd (CA)

are favoured because of their low acidity andcompatibility with the system structural materials.Also, these acids do not contain sulphur which isavoided because of its incompatibility with nickeland copper based alloys. Under the low acidicconditions provided by these weak organic acids, the iron oxide dissolution reaction is expected to be low.This is partially compensated by the complexforming ability of these organic acids. The complexformation react ion drives the dissolutionequilibrium to the right.

Fe3O4 + 8 H+ ® Fe2+ + 2 Fe3+ + 4 H2O

Fe 2+/3+ + Y x- ® Fe (x – 2 / 3) –

Yet, the high temperature formed oxides andespecially oxides such as hematite and nickel ferriteresist dissolution by the organic complex formingacids. The dissolution rates of these oxides are quietlow with these organic acids. Experiments carriedout with these oxides showed that reducing agentsaid the dissolution of these oxides

Reductive dissolution of Oxides

Fe3O4 + 8 H+ + 2 e- ® 3 Fe2+ + 4 H2Oe- is provided by the reducing agent

Reduction of ferric in the oxide lattice results in the formation of ferrous ion having a larger ionic size and hence destabilizes the lattice. Also, the ferrousion formed in the lattice makes the oxide moresoluble there by enabling faster dissolution of theoxide by the acid. Both organic and inorganicreducing agents are used for this purpose. Amongthem the following reagents are popular andextensively used:

(i) Oxalic acid

(ii) Ascorbic acid

(iii) Low oxidation state metal ions (LOMI) eg.,V2+(picolinate)

Apart from these reducing agents, the ferrousion complexes formed insitu in the dissolutionreaction eg., ferrous oxalate, ferrous-EDTA etc., can also act as a reducing agent. In the case of oxidesformed over carbon steel, its dissolution iscontrolled by the underlying metal. The underlying

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metal itself acts as a reducing agent by participatingin the dissolution reaction

Base Metal Aided Dissolution

Fe3O4 + Fe + 8 H+ ® 4 Fe2++ 4 H2O

The participation of underlying base metal is so effective that it makes the externally added reducingagent ineffective.

Thus, dissolution by organic complex formingacids aided by an organic or inorganic reducingagents is a preferred method. Mixtures of complexforming acid and a reducing agent with or without achemical inhibitor, normally constitute a chemicaldecontamination formulation. Some of the wellknown chemical decontamination formulations are:

1. Citric acid and Oxalic acid (CITROX)

2. EDTA, Citric acid, Oxalic acid (CANDECON)

3. V2+ (Picolinate), Picolinic acid (LOMI)

4. Pyridine di carboxylic acid, Ascorbic acid

5. EDTA, Ascorbic acid and Citric acid (EAC)

6. NTA, Ascorbic acid and Citric acid (NAC)

These chemical formulat ions, app l ied inconcentrations of one to few gms/litre, have beenproved to be effective in dissolving iron and nickelcontaining oxides and some of them have beenapplied in coolant system decontaminationsachieving good decontamination factors

Decontamination factor (DF) =

Radiation field before decontamination

Radiation field remaining after decontamination

In systems which do not contain chromium,decontamination factors in the range 2 – 50 areobtained depending on the nature of the system andthe material involved. However, these chemicalformulations give very poor decontaminationfactors when they are applied to coolant systemsurfaces that contain significant amount ofchromium.

Oxidizing reagents for the Dissolution of Chromium

Containing Oxides

The chemistry of chromium containing oxidesdiffers very much from the chemistry of iron oxides.The chromium containing oxides in the coolantsystem have varying composition such as Cr2O3,FexNiyCrzO4 etc. It is very difficult to reduce the Cr3+

in these oxides to Cr2+. Chromium (VI) is highlysoluble. Hence, instead of reducing the Cr(III), it isoxidized to Cr(VI) by using oxidizing agents such aspermanganate.

Cr2O3 + MnO4 - ® 2 Cr(VI) + MnO2

Permanganate as oxidizing agent, can beapplied in three different forms:

1. Alkaline permanganate (KMnO4 + NaOH)(AP)

2. Nitric acid Permanganate (KMnO4 + HNO3)(NP)

3. Permanganic acid (HMnO4) (Used in CORDprocess)

All the three are effective as oxidizingpre-treatment reagents. However, their effectiveness varies with material to material. Inconel alloy wasfound to be effectively decontaminated by alkalinepermanganate. Where as, stainless steel andIncoloy-800 has been found to be effectivelydecontaminated by acidic permanganate reagents.

Development of Chemical Decontamination

processes

From the fore going discussion it is clear thatthe choice of chemical reagents for effectingdecontamination of a system or a component ismaterial and system specific. The knowledge ofmaterial composition, operating conditions andchemistry of the system/component is essential topredict the nature of the oxides formed and theactivities present in the surfaces. The chemicalreagent is chosen from the nature of the oxides to bedissolved. An oxidizing pre-treatment step isintroduced if a system surface contains significantamount of chromium in its oxide film.

The reagents chosen are put to extensivematerial qualification tests by carrying out corrosioncompatibility experiments with all the major and

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minor structural materials that are present in thecoolant system.

After establishing the compatibility of thechemical formulation and its effectiveness inremoving the oxide f i lm and radioactivecontaminants from the system surfaces, the questionof mode of disposal of the radioactive waste arisingout of the decontamination process is addressed. The preferred mode of collecting the metal ions, radioactivities and the chemicals, used for thedecontamination, is by ion exchange.

The decontaminating chemicals added arere-circulated through a pump, heater and thecomponent /system to be decontaminated.Depending upon the process requirement, thetemperature of process is chosen. It is normally in the range 60 – 90oC. Some processes are applied at stillhigher temperatures. In the case of processesoperated in regenerative mode, a cation exchangecolumn is connected in the circuit. Finally, the addedchemicals, the metal ions and activities releasedfrom the system surfaces are removed by a mixedbed ion exchange columns.

Full system decontamination of primary coolant

systems of Pressurized Heavy Water Reactors

(PHWRs)

Most of our reactors are of Pressurized HeavyWater Reactors (PHWRs). Unlike the PWRs andBWRs, the PHWRs are of tube type reactors. Theprimary heavy water (D2O) coolant passes throughzircaloy fuel channels and takes the heat to steamgenerator through carbon steel feeders and headers.Radiation field in the primary heat transport (PHT)system of PHWRs builds up over a period of time. Aprocess has been developed to decontaminate theentire coolant system. This process called DiluteChemical Decontamination (DCD) process isapplied to the full system when the reactor is undershutdown. This process has the followingadvantages:

1. The decontaminating chemicals are added tothe heavy water coolant without significantdowngrading of heavy water

2. The decontamination is carried out with thefuel in the core

3. The metal ions, activities and the addedchemicals are removed on ion exchange resins.Hence, only solid radioactive waste isgenerated.

4. The system is brought to normal operatingcondition within 3 – 4 days

The chemical formulation consisting of achelating agent, acid and a reducing agent is added in concentration of 1 g/litre. The chemical is injectedinto the system as slurry. The system is kept undercirculation using the primary pumps and thetemperature is maintained in the range 80 – 85oC.The schematic of the process is given in Fig. 2. Theprocess is carried out in a regenerative mode. As theconcentration of chemical formulation is very low,the formulation tends to saturate because of itsreaction with the oxides. The partially spentchemical formulation is continuously passedthrough cation exchange resin columns in themodified purification system which removes themetal ions and activities and regenerates theformulation constituents. The regenerated chemicalformulation joins back the main system andcontinues the oxide dissolution/decontamination.After exhausting all the cation exchange resincolumns, the decontamination process is terminatedby valving-in the mixed bed columns consisting ofcation and anion exchange resins. The mixed bedcolumns remove all the remaining metal ions,activities and all the decontamination chemicalsthereby bringing back the coolant system to normaloperating conditions.

This process has been applied ten times inIndian reactors (MAPS#1&2, RAPS#1&2 andNAPS#1&2) with varying degree of success.Chemical formulations based on EDTA or NTAhave been used in these full primary systemdecontamination campaigns. Good decontamination factors in the range 2 – 30 were obtained on carbonsteel components of the system. Where as onMonel-400 and other non carbon steel portions of the system the DF used to be in the range 2 – 7. Thisprocess works well in systems that have 60Co andactivities other than antimony (122Sb and 124Sb). TheFig. 3 gives the radiation field in various components of the primary coolant system before and after eachof the three chemical decontamination campaignscarried out in MAPS#1.

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In systems dominated by antimony activities,the above chemical decontamination process bringssurprises. Radiation field on the system componentsdoes not reduce after decontamination, insteadincreased fields were observed in certain locations of the primary coolant system. This was attributed tothe deposition of antimony activities on the systemsurfaces during decontamination. The antimonyactivities (122Sb and 124Sb) present in the corezircaloy surfaces were released during the chemicaldecontamination campaigns. These activities wereexisting in anionic form and hence were not removed on cation exchange resin. Under the acidicconditions prevailing in the formulation, theseactivities deposit on the out-of-core carbon steel andsteam generator surfaces. This deposition ofantimony activities offsets the field reductionachieved by removing other activities such as 60Co,leading to little decrease in radiation level or in somecomponents increase in radiation field wereobserved.

Modification of the DCD process to systems where

antimony is the dominant activity

Detailed studies carried out on the adsorptionbehavior of Sb3+ indicated that it interacts directlywith Fe2+ formed in the corrosion reaction anddeposits there itself. This gave an indication that ifcorrosion process is inhibited the deposition ofantimony on the surface also can be hindered.Experiment carried out on the deposition ofantimony on carbon steel in medium containingchemical decontamination formulation and in thepresence of corrosion inhibitor (Rodine 92B),

proved that antimony deposition can be prevented by the corrosion inhibitor.

Based on this study a modified chemicaldecontamination process is applied to primarycoolant systems which are having significantquantities of 124Sb activities. An additional antimony removal step is introduced before the normaldecontamination process. A mixture of NTA (100mg/l)+Citric acid (100 mg/l) + Rodine 92B (100mg/l) is added to the system and circulated for abouthalf an hour at 85oC under non-regenerative mode(without regenerating the formulation throughcation exchange resin as it will remove the inhibitor). The antimony activities released from the core arefinally removed on the mixed bed ion exchangecolumns.

After the antimony removal step and afterremoving all the added chemicals, activities andmetal ions, the normal decontamination carried outin regenerative mode using cation exchange resin iscarried out to remove other activities.

This process of removal of antimony activitiesis superior to the process that uses oxidizing agent.Hydrogen peroxide is used as the oxidizing reagent.It oxidizes Sb(III) to Sb(V), the antimony in the latter form does not deposit on the surfaces and hence allthe antimony released from the core are removed onanion IX or the mixed bed. This method has thedisadvantange of using an oxidizing agent.PHWRs/PWRs are normally maintained, bothduring operation and shutdown, under reducingcondition.

Problem of ̀ Hotpsots’ in the moderator system of

PHWRs and its removal

In the moderator systems of some of thePHWRs, ̀ Hotspots’ (localized high radiation fields)were observed. Systematic investigations of the‘Hotspots’ indicated that they are due to thedeposition of particulate activities in the low flowareas. Control rod drive assembly contains rollersmade of stellite, a high cobalt ( 40 -60 %) containingmaterial. Wear of this material result in the release ofparticulate. These particles are neutron activated inthe core to give particles of high specific activity.These active particles settle down in low flow areascausing `Hotspots’.

IANCAS Bulletin 111 April 2008

Fig. 3 Radiation field reduction observed in eachdecontamination campaigns in MAPS

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The moderator system is a stainless steelsystem which is operated under low temperatureconditions (60 – 70oC). Hence, hardly any oxide film is expected on the stainless steel surface. Thus,attempt was made to develop a chemical formulation that is capable of dissolving the stellite particle itself. As stellite contains chromium along with cobalt, thereagents used for removing chromium containingoxide films were tested. Experiments carried outwith alkaline permanganate, acidic permanganateand permanganic acid indicated that permanganicacid followed by a reducing formulation (EDTAbased reducing formulation) is superior indissolving the stellite particles. Oxidation bypermanganic acid followed by reduction by reducing formulation has to be carried out at about 90oC andthis cycle has to be repeated thrice to get gooddecontamination factors. This process has beendemonstrated in a component removed from themoderator system of a PHWR. Decontaminationfactors as high as 11 was achieved on thiscomponent.

Decontamination process for stainless steel surfaces of

BWRs

The reactor coolant system of BWRs is mademostly of stainless steel. At the high temperatureoperating condition and under the oxidizingchemistry condition, hematite oxide film containingnickel and chromium is expected to be formed.Permanganate under acidic condition followed bytreatment with a reducing formulation is normallyrecommended. As the oxide film is thin and theredox cycle has to be repeated, the process is carriedout under non regenerative mode.

Conclusion

From the knowledge of system structuralmaterial, operating condition and the chemistrycondition of the coolant, it is possible to arrive at asuitable chemical decontamination process and toreduce the radiation field in the system.

References

1. S.Velmurugan, V.S.Sathyaseelan,T.V.Padmakumari, S.V.Narasimhan andP.K.Mathur, Behavior of ion exchange resinsand corrosion inhibitors in dilute chemicaldecontamination, Journal of nuclear scienceand technology, vol.28(6), pp.517-529, June1991.

2. S.Velmurugan, S.V.Narasimhan, P.K.Mathur,and K.S.Venkateswarlu, Evaluation of a dilutechemical decontaminant for pressurized heavywater reactors, Nuclear technology, vol.96,pp.248-258, Dec.1991

3. S.Velmurugan, A.L.Rufus, V.S.Sathyaseelan,T.V.Padmakumari, S.V.Narasimhan andP.K.Mathur, Corrosion of PHWR PHT systemstructural materials by dilute chemicaldecontamination formulations containingascorbic acid, Nuclear Energy, 34, No.2,pp.103-116, Apr.1995

4. Rufus A.L., Velmurugan S., Padmakumari S.Kumar, Satyaseelan V.S., Narasimhan S.V.and Mathur P.K. Ion exchange considerationsfor dilute chemical decontamination processesoperated in the regenerative mode. NuclearTechnology (USA), 122, 228-249 (1998)

April 2008 112 IANCAS Bulletin

Fig. 4

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5. Satyaseelan.V.S, Velmurugan.S, Rufus.A.L,Narasimhan.S.V, Mathur.P.K. and KamalKishore, Analysis of all the constituents offormulation used for chemicaldecontamination, Power Plant Chemistry2(10), (2000)

6. Pr ince.A.A.M, Mary Remona.A.A,Velmurugan.S, Narasimhan.S.V,Raghavan.P.S and Gopalan.R,Dissolutionbehaviour of mixed ferrites and chromites in

aqueous solutions containing chelating agents,Power plant Chemistry 2(11), 545-550,(2000)\

7. Prince A.A.M, Velmurugan S, Ramesh C,Murugesan N, Raghavan P.S, Gopalan R andNarasimhan S.V, Dissolution behaviour ofmagnetite film formed over carbon steel indilute organic acid media, Journal of nuclearmaterials, 289, 281-290, (2001)

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Removal of Turbidity from Coolant Systems usingElectrochemical Filtration

Introduction

In many aqueous coolant systems suspendedsub-micron size particles in a low / mediumconcentration is referred as the turbidity of thecoolant. At low concentrations parts per billion(ppb) level of metals, solution may apparently lookclear, but at parts per million level (ppm) the coolantcan appear very turbid. Turbidity itself or itsdeposition on surface can cause heat transferproblems to the nuclear power and other industriesas well. Such problems were encountered in the form of aluminum turbidity in Dhruva reactor in 1985, inthe form of radioactive indium turbidity in Rajasthan Atomic Power Station Unit # 2 (RAPS #2 )moderator heavy water system and in the form ofiron turbidity in the active process water system(APWS) of Kaiga Generating Station Unit # 1 ( KGS # 1). In Dhruva and RAPS it resulted in highradioactivity in coolant which was addressed and inKGS fouling of moderator cooling intermediate heatexchanger was combated. Removal of turbidity dueto its feeble particle charge and low concentration isproblematic. Electro-deposition of particles on

porous graphite/Carbon electrodes is one of thebest-suited methods for such turbidity removal.Initially, a prototype electrochemical filter (ECF)was fabricated and tested for indium turbidityremoval at RAPS #1. Subsequently a larger versionof the ECF was designed and in house fabricated andwas deployed for iron turbidity removal at Kaiga and for silica and iron turbidity removal at Kalpakkam.ECF showed 75-80% turbidity removal along with50% capacity for non-reactive silica removal andnear complete removal of microbes.

PZC of iron turbidity particles and ECF carbon felt

Turbidity in solution arises due to charge on the particles. Most of the suspended particles containing hydrours / hydrated or hydrous oxides or mixedoxides will have point of zero charge (pzc) Forexample, iron containing Fe in the Fe3

+ or in[Fe2++Fe3+] state, will have PZC values in the range

of 6.0 to 8.5: F3O4: 6.5, a-Fe2O3 : 6.7, gFe2O3 : 6.7,

a-FeOOH : 6.7, g-FeOOH 7.4, Fe(OH)3 (amorph) :

April 2008 114 IANCAS Bulletin

G. Venkateswaran, Analytical Chemistry Division Bhabha Atomic Research Center, Trombay, Mumbai 400 085and A.G. Kumbhar,Water and Steam Chemistry Division, BARC Facility, Kalpakkam, Taml Nadu; E-mail:

Dr. G.Venkateswaran is a post-graduate in Chemistry from the University of Madras , aPh.D. from University of Mumbai and is from the 14th batch of Bhabha Atomic ResearchCentre (BARC) Training School. His areas of specialization are: nuclear power reactorfuel performance evaluation, suspended corrosion product removal from reactorcoolants, chemical decontamination of nuclear reactors, metal-ion passivation etc.Turbidity removal from the Dhruva coolant and TAPS Clean-up SystemDecontamination are his notable projects executed. He over 165 publications ininternational journals and conferences He is a recognized guide of the Ph.D. programmeof Mumbai University and he is a Professor in the Homi Bhabha National Institute inMumbai. He is currently heading the Analytical Chemistry Division of BARC.

Dr. A.G. Kumbhar is a M. Sc. (Inorganic Chemistry) from Shivaji University, Kolhapurand Ph. D. (Chemistry) from University of Madras, Chennai. He is Experienced in the area of Electrochemical Speciation, Condensate Polishing, Ion exchange, ChemicalDecontamination and Health Physics. Currently working in the area of RadiolyticHydrogen Generation, nano-size turbidity removal with modified ion exchanger andelectrochemical filtration for water purification. He is a Post-graduate Teacher at theHomi Bhabha National Institute.

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8.5 [1]. At a particular solution pH particle surfacecharge ism governed by the equation:

V = k (pzc – pH) (1)

where ‘V’ is the zeta potential of the suspendedparticle, ‘pzc’ is its point of zero charge and pH is thesolution acidity in pH units. The zeta potential ofgraphite felt particles suspended in distilled waterwas found to be -25 mV at neutral pH. Even at a pHof 1.5 the graphite felt particles were found to carry anegative surface charge. Hence by the natural zetapotential effect the hydrated / hydrous oxides of Fe3+

will be electrostatically repelled from the fibrousgraphite felts. However, in the present study, thesegraphite felts are made anodic / cathodic with thehelp of an applied potential thus overcoming itsnatural zeta potential effect.

Turbidity in a large cooling water system, dueto suspended micron or submicron size particles andat low particulate concentration, poses a problem forits removal by normal micron / sub-micron filtrationor by ion exchange process. Surface modified ionexchangers resins i.e., precipitated ion-exchange(PIE) resins can be used for this purpose but thisrequires a back-up normal ion-exchange column toremove the soluble metal ions, resulting from thelimited solubility of the precipitate from the PIEresin, which otherwise can enter the main system asimpurities [2]. When the turbidity levels are low, this washing-out effect impacts on the throughputrealizable by these precipitated ion-exchangers.Thus the use of PIE resins has limitations if oneencounters large system volumes of dilute turbidityto be cleaned up. Commercial Zeta-potential filterson the other hand employ a special cartridge (housedin an outer shell), which has a thin coat of a materialon a base matrix with zeta-potential opposite in signto the zeta potential of the suspended particles. Theyare very suitable for treating very dilute turbidities{< 5 Nephelometric Turbidity Units (NTU)} but inthe middle range (5-10 NTU) and high range (> 10NTU) can give rise to problems of cartridge changewhich requires new filter procurement as thesefilters are once-use throw-away type [2].

Electro-deposition of suspended particles from a turbid solution on graphite felts is another methodfor this type of dilute turbidity removal from water[3]. The higher surface area (typically 10-12 m2/g)

with a concomitant improved contact with flowingsolution, high fluid permeability with free flow ofthe solution without back pressure to higher flowsand chemical, electrochemical inertness, theirregenerability and reuse makes the graphite feltelectrochemical filter more suitable for diluteturbidity removal.

Indium Turbidity removal from RAPS # 1,

Moderator Heavy water:

It is very difficult to remove metal ion basedcolloidal turbidity from water using normal filters,which can remove particles of up to a few micronsize only. In nuclear power stations such a turbiditycontaining an element, which gets activated byneutrons, can create a radiation exposure problem tothe operation and maintenance staff. For example, aleaky calandria Over Pressure Rupture Device(OPRD) of moderator system of Rajasthan AtomicPower Station (RAPS-I) was sealed using indium(In) metal in March 1998. Under normal operatingconditions, moderator does not come in contact withthis indium sealant. However, the condensingmoisture on this sealing surface containing someradiolytically produced HNO3 caused corrosion ofthis indium metal and introduced indium in themoderator heavy water. In the neutral pH regime ofmoderator the indium seemed to have formedcolloidal indium turbidity. Due to a reasonably highneutron absorption cross section (170 barns) 115In(95.7% isotopic abundance) got converted toradioactive In116m (t1/2 = 54 min, Eg = >1 MeV). Thiscreated operational problems while handlingmoderator heavy water samples for analysis ofchemistry parameters. Hence it was necessary toremove the indium turbidity from the moderatorsystem. As the size of turbidity particles was verysmall (< 1 µm) and indium concentration was verylow (100-150 ppb), it could not be removed bynormal filtration or by the system purification ionexchangers. Two approaches were studied toremove this indium turbidity. A Mg-Mg(OH)2

precipitated weak acid cation exchanger resin whichwas earlier demonstrated by us in laboratory as wellas in the actual reactor system for removal ofaluminum turbidity (2) was tried and found tosatisfactorily remove this indium turbidity. Removal of indium turbidity was also attempted by

IANCAS Bulletin 115 April 2008

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electrosorption on fibrous graphite. The results ofelectrosorption study are given bellow.

Fabrication of an Electrochemical Filter (Fig. 1)

The basic design of the electrochemical filter in this study is based on an earlier work reported inliterature regarding removal of aluminum turbidityfrom D2O in a nuclear reactor (4). The filterfabricated by us had 14 cathode anode pairs offibrous graphite felt discs (each felt of ~6 mmthickness and of 35mm dia) The felt discs wereseparated and supported by 2 mm thick perforatedpolyethylene plates. A central SS rod connecting aset of 14 such felts and a outer SS cylinderconnecting another set of 14 felts served as theelectrode leads for impressing the potential in orderto make the two felt sets as anodes and cathodes. Thefilter could be operated at a flow rate of 23 ml/min, so as to give a contact time of 2 min.

(i) Lab generated turbidity removal

Resul ts of a run performed onlaboratory-generated turbidity with electrochemicalcarbon felt cell are shown in Fig. 2. At high (4.6 ppmIn) and low (0.23 ppm In) indium inlet turbiditylevel, outlet indium was less than 0.001 ppmexcepting the initial slip of 0.03 ppm at the beginning of low concentration run. Under closed circuitconditions applied field during low concentrationrun, 50 V emf was applied to cell and a current of 20mA was observed. During the high concentrationrun 16.5 V emf was required to get 20 mA [5].

(ii) Removal of moderator turbidity

A block diagram of the experimental setup asconnected to the moderator sampling station asshown in Fig. 3. As shown, the filter was operatedwith the inlet moderator D2O flowing from thebottom of the column to top and the exiting heavywater was collected in a plastic carboy. The valvearrangements made in the hook up of this column tothe moderator sample point permitted a minimum

flow rate of about 30-35 ml/min. A »1.2 m heightsemicircular lead screen mounted on a trolley wasemployed to isolate the experimental set up in themoderator sampling area. The turbidity removal wasfollowed by monitoring the 116mIn radioactivity inthe electrochemical filter column inlet and outletsolutions. The 2112.3 keV gamma (yield 15%) waschosen to minimize the compton scatteringinterference in the photo peak area determination ofthis isotope. HPGe (high purity germanium) detector coupled to a 4 K multichannel analyzer was used forthe gamma counting. Additionally the dose rate

April 2008 116 IANCAS Bulletin

Fig. 1 Schematic of ECF

Fig. 2 Indium Turbidity Removal: fromlaboratory generated turbidity usingElectrochemical filter

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measurements near bottom (close to inlet), middleand top (close to outlet) zones of the column werecarried out to assess the progress of Indium turbidity

removal. This was done using an teletector g dosemonitor. Since the different zones of the columncould not be shielded, a zone with a higher field(expected to be the bottom inlet zone) contributing to the dose measured at the upper lower dose zones(middle and top) is anticipated

In order to minimize the radiation exposure topersonnel involved in the experiments it was feltprudent to connect the electrochemical filter to thesystem immediately after a shutdown of the reactorand monitor both inlet and outlet solution Indium

radioactivity levels at regular intervals of time on4-12-01 at 1342 h. The electrochemical filter column was connected to the system within 90 minutes afterreactor shutdown (i.e., 1510 h). Since reactor wasshutdown, the normal ion-exchange inlet samplingpoint (SS#3) could not be made use of for providingthe moderator D2O to the electrochemical filtercolumn and instead the adjuster rod moderator D2Ocooling water line sampling point was used for thistrial removal study. Since it takes more than 40minutes to get the heavy water flowing through thissample line from the core to the sampling point, thefirst column inlet and outlet samples were taken at1620 h i.e., 70 minutes after valving-in the column.The electrochemical filter was operated at an applied

potential of 40 V and a current of »0.8-1.4 mA couldbe realized. The temperature of the moderator wasclose to 303 K during this study.

Table 1 shows the performance of theelectrochemical filter column in removing Indiumfrom the moderator in terms of 116mIn radioactivitylevels at the column inlet and outlet, percentageIndium removed, cell currents and cell voltage. Asseen in the data of Table-1, the inlet activity wasdecreasing with time since the experiments beganafter the shutdown of the reactor. Except for the firstinlet value (1620 h), the other values seem to followclosely the half life of 116mIn. The first value (3700

mCi / l ) appears to be » 20% lower than its expectedvalue which is calculated from the second and

IANCAS Bulletin 117 April 2008

Fig. 3 Block diagram of Indium turbidity testremoval setup connected to RAPSmoderator sampling point

TABLE 1. Test removal of Indium from moderator of RAPS-1: Radioindium data

No Sampletime

(minutes)

CellVoltage

(V)

Cellcurrent(mA)

116mIn ac tiv ity( mCi / l )

Per cent ageIndium removal

Columninlet

Column outlet Removal Factor (RF)*

1 0 40 1.3 3700 200 94.6 / 18.5

2 72 40 1.0 2258 189 91.6 / 11.9

3 135 40 0.9 918 89 90.3 / 10.3

4 215 40 0.8 425 65 84.7 / 6.5

5 275 40 1.4 143 24 83.2 / 6.0

*Removal Factor (RF) = Column inlet activity / Column outlet activityPercentage Removal = [ {1 (1 / RF)}] 100

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further activity values using the radioactive decayequation after applying the decay correction. Theadjuster rod cooling water-sampling point is notnormally used for moderator sampling duringreactor operation. Hence the somewhat lower firstvalue could possibly be because of some mixing ofstagnant heavy water in the sample line with theactual moderator sample. The waiting period of 70minutes after valving-in (at 1510 h) and beforesample collection (at 1620 h) appears to besomewhat less than the actual time lapse required fora representative sample collection after valving-inthe column. Once a steady flow of the actualmoderator heavy water was established through thecolumn, samples were collected at any time fromboth the inlet and the outlet positions of the column.It may be noted that it takes about 6 minutes for theinlet water to come out of the column and in this

period there could be » 8 % reduction in the activityof outlet samples compared to sample entering theinlet. Hence any reduction in the outlet activitygreater than 7.5% is to be attributed to the sorptioncapacity of the column. As such the activity of theoutlet samples (Table 1) was not corrected for decayfor this period of transit (6 min) through the column.However, the radioactivity values of inlet and outletsamples were decay corrected for the time elapsedbetween sample time and count time.

The percentage Indium removal can beexpressed by the equation (1):

% removal = [ {1 (1 / RF ) }100 ] (1)

where RF, the removal factor = Column inlet activity / Column outlet activity

Due to electroadsorption of colloidal Indium,the electrochemical filter column outlet activityvalues are lower by a factor (RF) ranging from 18.5to 6. As seen from the table, the Indium removal has

decreased from » 95% in the initial stages to » 83% at the end of about 6 h of run. It may be noted for this12% decrease in removal, the RF value hasdecreased by 66%, i.e., from an initial value of 18.5to the end of run value of 6. The decrease in %removal as indicated by radioactivity measurementsmay be arising due to decrease in the inlet activityvalues and not due to any reduction in the efficiencyof column to sorb the Indium. It is well known inchemical decontamination operation that locations

with higher initial radioactivity tend to show higherdecontamination factors (higher % oxide removal)than those where the initial activity is lower. We thus infer that a 85-90 % removal efficiency can beassigned to the electrochemical filter column. Wemay also argue that the efficiency could have beenhigher than 90% had the column been operated at its

designed flow rate of » 20 ml / min against theminimum flow rate of 30-35 ml / min that could beachieved in this test removal experiment. We couldascribe this reason since in a pilot run conducted aday earlier when the reactor was operating atconstant power of 90 Mwe and when the flow ratecould only be adjusted to a minimum of 60-70 ml /min, no sorption of Indium activity by the columnwas observed.

Table 2 shows the radiation field accumulatedon the column with the progress of the test removalrun. The radiation field on the column at any time isa resultant of the earlier sorbed Indium activitydecaying with time and freshly sorbed activity, thelatter being at a lower value at as compared to the

value at an earlier time t - Dt) . Accordingly theradiation field observed at the bottom of the columnhas shown a lower decrease with time than thedecrease warranted by half-life. However, theradiation field at the column outlet had remained

nearly steady at » 300-400 mR / h (3-4 mSv/h)without showing a decrease similar to the bottom of

the column. This is due to the background g shinefrom the bottom of the column contributing to thedose measurements at the top of the column. Thehigh field at the bottom of the column shows that it isthe initial 4-5 anode/cathode pairs, which essentiallycontributed to the sorption process. The cell current

of » 1 mA applied to the electrochemical cellinduced a voltage of 40 V. Since the moderator had a

conductivity of 0.5 mS cm-1, it is likely that most ofthe voltage drop occurs across the solution resistance and only a small portion of the applied voltage isexperienced by the electrical double layer to drivethe adsorption process. Unlike the experiment withlaboratory generated turbidity, the presentexperiment with moderator Indium turbidity couldbe not be conducted without applying the field (since radioactivity in the moderator was decaying and thecell could only be operated in the desired appliedfield mode to collect the turbidity removal data) to

April 2008 118 IANCAS Bulletin

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assess as to what extent the applied field has helped.In the case of laboratory generated Indium turbidity,the removal was quantitative even without applyingthe electrical field. However, it is reported that in theremoval of aluminum turbidity (colloidal Al2O3) bythis fibrous carbon electrode method, the application of electric field had helped in clearing the turbidity to

the clean water level while without field about 90%reduction in turbidity was noticed (4).

Zeta potential of carbon felt particlessuspended in distilled water was found to be <-25(clost to 5mV) mV at neutral pH (Fig.4a) and wassimilar in sign to indium turbidity (-22 mV).

This indicates that during open circuitconditions turbidity removal is by physicaladsorption and during close circuit condition byelectrostatic attraction and physical sorption.

Microbes removal from RAPS #2 Moderator Heat

exchanger Water

Significant sensitivity reduction was observedin online tritium monitor system of RAPS-2. Thiswas identified as due to microbial fouling of surfaceof the plastic scintillation detector [6]. A twentytimes reduction in microbial population wasobserved when the sample was passed though ECFunder closed circuit condition (Fig.5a). Based on this work sample conditioner system modifications weresuggested in existing online tritium monitoringfacility at RAPS-2 (Fig.5 b)

Iron turbidity removal from APWS of KGS #1

The Active Process Water System (APWS) atKaiga Generating Station (KGS) units-1&2(Schematic-A) experiences iron turbidity to

IANCAS Bulletin 119 April 2008

TABLE 2. Radiation field on the electrochemical filter during test removal of Indium from themoderator of RAPS-1

No Sample time (min) Ra di a tion Field on Elec tro chem i cal Filter Column (mR / h )

Bottom (inlet) ofcolumn@

Middle of column Top (outlet) ofColumn

1 0 > 10000 2000 400

2 72 5000 1800 350

3 135 3000 800 300

4 215 2500 700 300

5 275 1400 450 300

@The terms bottom, middle and top of the column refer to about 10-12 cm length of each of these portions of the column as seen by thesensor of the teletector monitor.

Fig. 4a (i) Plot of charge vs. pH for PZC ofKGS#!1, APWS turbidity.(ii) Plot of charge vs. pH for carbon feltpowder used in ECF.

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different levels during various operational periods of the system. The entry of iron corrosion productsfrom the backup fire water system seems to be thecause for the observed turbidity levels in APWS. Onthe one hand, APWS cools the shell-tube type

moderator heat exchanger [7] and on the other handit rejects this heat to the Active Process CoolingWater System (APCWS) through plate type heatexchanger(s). The water in APCWS in turn getscooled by the Induced Draft Cooling Tower(schematic-A). The continued operation of turbidityridden APWS can result in fouling of the plate type

April 2008 120 IANCAS Bulletin

Fig. 4b Sample conditioning system modifications for online monitoring Tritium monitoring system

Fig. 5a Macrographs of microbes grown innutrientRich medium in process water sample ofRAPS-2 collected after the sub-micronfilter(top a), after passed through theelectrochemical filter without field (left b)and after passed through theelectrochemical filter with field (right c)

Fig. 5b Macrographs of microbes grown innutrient rich Medium in process water collected directly(before the system Filter) passed throughthe electrochemical filter without field (leftd) and with field (24V, 350 mA) (right e)

Page 28: Vol. VII. No.2 Editor : B.S. Tomar April 2008 CONTENTS · the corrosion products. Activation of the transported corrosion products by the neutron flux in the core generates the radioactive

HXs through deposition of iron corrosion products.Such a fouling of the heat exchanger reduces thedesired cooling efficiency of APWS to maintain thetemperature of moderator water within the specifiedlimits, which in turn will have safety implications.

An in-house designed and fabricatedelectrochemical filter (ECF) containing alternatearray of 33 pairs of cathode and anode graphite feltswas successfully tested for the removal of ironturbidity from Active Process Water System(APWS) of Kaiga Generating Station unit-1 (KGS #1).

Electrochemical filter (ECF) fabrication

A cross-sectional view of the fabricated ECF isshown in Fig.6. The outer cylinder (integrated withflanges), central pipe leading the inlet turbid solution and the inlet / outlet connections of the filter aremade of stainless steel. 33 pairs of circular graphitefelt anode and cathode of about 6mm thickness 150mm diameter supported on perforatedpolymethylmethacrylate (Perspex) plates wereassembled inside the cylinder (clearance between SS

shell and the felt housing made of Perspex is 13 ± 6ìm). Alternately, a set of 33 discs of graphite felt wascontacting outer SS cylinder at periphery of thecylinder and was isolated from the central SS pipeusing spacers and another set of 33 discs wascontacting central SS pipe of the filter and wasisolated from outer periphery of the cylinder using

IANCAS Bulletin 121 April 2008

Scheme A: Active Process Water System(Apws) At Kgs

Fig. 6 Cross sectional view of electrochemical filter

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box type cathode support perspex plates. Thus theelectrodes could be used as alternate anodes andcathodes while applying potential. Both inlet andoutlet of the filter were connected from top of thefilter. The central stainless steel pipe served as inletto the filter with water flowing down through thepipe and rising above from the bottom through abottom end spacer, then through the perforatedperspex plates holding the cathode/anode graphitefelts before exiting. The inlet flange portion of thecentral SS pipe and the flange part of the main SSshell were used as contact points for imposing theelectromotive force. The central SS pipe was Tefloncoated from inside to avoid streaming currents due to flow. Graphite felts were activated by heating themin oven at 450ºC for 2 h in air oven prior to packingthem in the ECF.

Effect of Potential, flow, and inlet turbidityvariation on ECF outlet are shown in Fig.7. Theoperation of electrochemical filter has revealed thepossible occurrence of three phenomenasimultaneously: a) the settling of negatively chargedoxide particles on the anode surface, b) the release ofgravity settled particles causing turbidity possibly

from the cathode surface, and c) the effect of O2 andH2 evolution on the settled oxide particles from theelectrode (anodic and cathodic) surfaces. When theturbidity values are high, application of potentials ofthe magnitude of 20 V appears optimum for turbidity removal (75% removal) . Once suff ic ientaccumulation occurs on the fibrous felts, thisefficiency is observed even when there is no appliedpotential. But once low levels of inlet turbidity arereached (< 5 NTU) then outlet turbidity could be

suppressed further (£ 1 NTU) by increasing thepotential beyond 20 V i.e., 25 to 30 V. Hence foreach appl ication of turbidity removal anoptimization of parameters like potential and flowvis- vis inlet turbidity requires to be carried out.

After flowing 40 m3 of APCW through theECF, with the existing 0.5 hp pump, flow could notbe maintained at 10 lpm and it decreased slowly to 6lpm. This may be due to the clogging of the filter andhence the run was terminated. At this point the outletECF turbidity was 0.6 NTU indicating that the filterhas still capacity to remove turbidity and it has not itreached to saturation. Towards the end of the run, the applied potential was 29 V, current was 1.4 A and the filter showed an efficiency of 87 %. As far as asubmicron sized and low concentration turbidityremoval is concerned such an efficiency exhibitedby the ECF indicates its satisfactory performance. At the termination of the experiment, a throughput of >2.08x105 NTU-liters could be realized and still thefilter was working with about 85% efficiency. At theend of the experiment the internals of ECF wereremoved for observation. Only about 30% of thefelts from the bottom of the filter were found to beused up and the rest appeared new and unused.Hence the throughput of this filter is expected to bemuch more than 2x105 NTU-liters.

Turbidity removal from Pond Water used for

Cooling Heat Exchanger at Kalpakkam

Turbidity of HTHP cooling pond was 3-5NTU. In case of APWS KGS #1, the water was DMwater with additive to make pH to 9.0-9.5. But, inthis case it was a open storage tank natural water,hence it contained both macro and micro turbidity.As, the ECF is exclusively for removing microturbidity, the bottom felts of ECF were often gettingchoked due to macro turbidity. Out of two runs

April 2008 122 IANCAS Bulletin

Fig. 7 ECF testing at KGS #1, APW system. : ECF Outlet turbidity as a function of potentialapplied, inlet turbidity, current and flow

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conducted with this water in the first run 17.2 m3

water was processed with 2.15 x 104 NTU-litersturbidity removal. In this run a clogged bottomcarbon felt pairs were removed each time when 4.65,12.14 and 15.92 m3 of water was processed. At theend of 4.65 m3 through put a cartridge filter was alsoincorporated in the before the inlet of ECF to takecare of macro turbidity. After 12.14 m3 throughput itlooks like other 31 felts also might have got cloggedwith the turbidity and hence removing the third pairof bottom felts at the end of 15.92 m3 did not help inextending the run further. Due to back pressure therun has to be terminated at 17.21 m3 throughput.

At this point the storage pond turbidity wasreduced from 3.6 NTU to 0.85 NTU (75 % turbidityremoval).

With the average inlet turbidity of 1.67 NTUand outlet turbidity of 0.42 NTU. ECF efficiency of74% was realized. The effect of applied potential,current, flow rate and inlet turbidity on ECF outletturbidity are shown in Fig. 8 and 9. Flow rate of10-20 lpm, potential of 5-8 V with current of ~ 1Aand an attachment of a cartridge filter before inletwere the optimized as ECF operational conditionsfor the efficient turbidity removal of Kalpakkamwater.

In the second run ECF was packed with top 25empty Teflon spacers followed by six cathode /

anode pairs and two bottom empty spacers. Thecartridge filter was also attached before the ECFinlet. Effect of applied potential, current and flowrate is shown in Fig. 9. As, in the earlier first runearlier most of the macro turbidity was removed theinlet turbidity level in this was only 0.85 NTU. In this run most of the time ECF inlet and outlet turbiditylevel remained constant with a inlet value of 0.85NTU and a outlet value of 0.27 NTU. Continuousdecrease in flow rate (18.0-4.5 lpm) with increasingthroughput was observed during the run, indicatingthe continuous loading of filter with turbidity.Optimum potential of 5.2 V and current of 1 A wasestablished for efficient functioning of ECF. 6.65 m3

of water was processed with 3.87 103 NTU-literturbidity removal. The efficiency of 68 % wasrealized which is quite satisfactory for low level (> 1NTU) and sub micron turbidity removal.

Silica (Si) content in Kalpakkam water was19-29 ppm, of which 0.7-0.8 ppm was non- reactiveSi. Non reactive Si is crucial to super critical steamgenerators as it passes through ion exchangepurification system and then gets converted in thereactive Si resulting in silica deposits on the turbineblades. Table.3 shows Si analysis from WSCD,

IANCAS Bulletin 123 April 2008

Fig. 8 Run No. 1: Effect of inlet turbidity and flowon ECF operation at WSCD Kalpakkam

Fig. 9 Run. No. 1: Effect of potential and currenton ECF operation at WSCD, Kalpakkam.

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Kalpaakm experiment. Although, no reactive Siremoval was shown by ECF, 50 % efficiency for nonreactive Si removal was observed. By consideringlow inlet non reactive Si concentration (0.6 ppm),the observed 50 % reduction in outlet (0.3 ppm) isquite effective. ECF also showed near completeremoval of Coliform S microbs from water.

Conclusions

1. Prototype electrochemical filter shown toremove radioactive indium turbidity fromRAPS # 2 moderator heavy water

2. The filter was also tested for microbes removaland a modification in tritium detector assembly was suggested for preventing fouling.

3. Test of the pilot plant scale electrochemicalfilter employing fibrous graphite feltelectrodes with APWS of KGS #1 and WSCDKalpakkam service water has shown that thefine turbidity from the system could beremoved effectively.

4. Applied potential, flow rate and the effect ofopen-circuit conditions were evaluated for theturbidity removal. An applied potential of 20Vand a flow rate of 10 lpm was found to beoptimum for APWS, KGS #1, and appliedpotential of 5-8 V and flow rate of 10-20 lpmwas optimized. In both the cases ECF showedan average efficiency of 75%.

5. Turbidity removal by ECF involves noaddition / hookup of any chemical orchemically loaded ion-exchanger in the system and the method is independent of zeta-potential of the particles unlike in the case of commercial zeta-potential filters

6. ECF can also be used for microbes removal and non reactive Silica

Acknowledgements

The authors are grateful to Dr. T. Mukherjee,Director, Chemistry Group and Dr.S.V.Narasimhan, Associate Director, Chemistry Group and Head,Water and Steam Chemistry Division for their keeninterest in this work. The authors thank theauthorities of KGS-1&2, the staff of ReactorChemistry Laboratory of KGS-1&2 and Shri T.V. K. Mohan, WSCD Kalpakkam along with his

April 2008 124 IANCAS Bulletin

TABLE 3. Effect of Applied potential and flow on turbidity and non reactive silica removal by ECF

Date Time(h)

Thput

(M3)

Flow

(lpm)

Potential (V)

Cur rent (A)

ECF In let ECF Out let

Re ac tiveSi

Nonre ac -

tive Si(ppm)

Tur -bid ity(NTU)

Re ac -tive Si

(ppm)

Non-reactive

Si(ppm)

Tur -bid ity(NTU)

03.06.08 17.35 00.45 10.0 0 0 19.2 0.85 2.6 18.8 0.54 0.63

20.05 01.80 09.0 2.76 1.09 19.20 0.70 2.4 19.10 0.38 0.57

04.06.08 00.30 03.31 05.0 1.64 0.80 19.31 0.49 2.4 19.12 0.28 0.80

11.00 04.50 06.5 0 0 19.20 0.70 2.9 19.10 0.20 0.48

05.06.08 11.20 04.85 13.0 0 0 19.00 0.50 2.0 18.80 0.30 0.40

06.06.08 11.00 14.20 21.0 14.35 7.25 18.90 0.40 1.4 19.10 0.10 0.24

Fig. 10 Run No.2: Effect of Inlet turbidity, flow,potential on ECF operation at WSCD,Kalpakkam

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colleagues for providing all the facilities for carrying out this experiment at site. Authors express theirthanks to Dr. S. Ramanathan, Dr. M.P. Srinivasan,Shri P. Candra Mohan, Dr. S. Bera and Shri A.N.Shirsat for their help in obtaining the iron turbiditycharacterization data and interpreting the same. Theauthors gratefully acknowledge the help rendered by Dr.A.D.Belapurkar, Shri B.K.Gokhale, ShriV.Balaji and the Centre for Design and Manufactureduring the various stages of study and ECFfabrication.

References

1. Parks, G. A. (1965). The isoelectric points ofsolid oxides, solid hydroxides, and aqueoushyroxo complex systems. Chem. Rev., 65: 177.

2. Venkateswarlu , K.S. , Shanker , R. ,Velmurugan , S. , Venkateswaran G.,Ranganatha Rao M. (1998) Removal ofaluminum turbidity from heavy water reactorsby precipita tion ion exchange usingmagnesium hydroxide. Nuclear Technology,82: 243-250.

3. Oren, Y. and Soffer, A. (1983) Graphite felt asefficient porous electrode for impurity removal and recovery of metals. Electrochemica Acta,28 (11):1649-1654.

4. H. Tobias, E. Tarangan, Y. Oren, A. Soffer.(1987) Removal of suspended aluminapart ic les f rom heavy water byelectroadsorption on fibrous carbo. electrode.Nuclear Technology, 77: 46 -49.

5. A. G. Kumbhar, , G. Venkateswaran, K.Kishore, A. D. Belapurkar, B. K. Gokhale, A.Dalavi, (2003) Removal of indium turbidityfrom water using a magnesium ion loadedweak acid cation exchanger and fibrousgraphite electrode. Separation Science andTechnology, 38 (9): 2107 -2120.

6. G. Venkateswaran, B. K. Gokhale, A. D.Belapurkar, A.G. Kumbhar, V. Balaji, (March15-172004) Turbidity and microbes removalfrom water using an electrochemical filter.Proc. Of National Seminar on Roll ofChemistry in the Emerging Areas of AppliedSciences, S.V. University Tirupati: 46-50.

7. Venkateswaran, G., Kumbhar, A. G., Gokhale, B. K., Balaji, V., Sarangi, N. K., Sinha, A. K.,Gupta, M. D. P., Jawale, S. B., Harikrishana,K., Nayak, N., Rao, V., Kumar, T. S.,Choudhari, A. (2007) Iron Turbidity removalfrom the Active Process Water System of theKaiga Generating Station Unit #1 Using anElectrochemical Filter. PowerPlant Chemistry, 9(9), 541.

IANCAS Bulletin 125 April 2008

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Corrosion of Primary Heat Transport System CarbonSteel Material in PHWR

Structural materials in power plants interactwith high temperature aqueous environment in theheat transport system. The main structural materialsin the primary heat transport system are Carbon steel106 Gr-B as piping, Incoloy-800/Monel-400 as thesteam generator material and Zr-Nb/Zircaloy-2 inthe core. Every effort is made to minimize thecorrosion and its impact on operation of the plant. Amajor emphasis is given to maintain the chemistry ofcoolant water during operation of the reactor and itsshutdown. This paper mainly deals with thecorrosion behavior of carbon steel in the primaryheat transport system of PHWR. Corrosion ofcarbon steel structural material contributes to theradiation field build up in out of core surfaces andleads to excessive wall thinning of carbon steeloutlet feeders necessitating mid course en-massereplacement of feeders. Any attempt to inhibitcorrosion would also address these two phenomena.

The Radioactive Deposit Problem

Radioactivity build-up in the primary heattransport (PHT) system, due to corrosion andactivation of corrosion products in nuclear reactors;results in exposure of personnel to radiation fieldduring maintenance work. Considerable R&D isbeing done to reduce the radiation field build-up inthe primary coolant system. Radioactivity build-upin the primary heat transport system is due tocorrosion and activation of corrosion products.World over attempt is being made to develop newstructural materials and to frame strict chemistrycontrol regimes to mitigate this problem. There is

very little scope of tinkering with the structuralmaterials in operating reactors except for minorrefurbishment. However effective water chemistrycontrol can help in taming this problem.

Structural materials used in primary heattransport system such as Carbon Steel, Stainlesssteel, Monel-400, Incoloy-800, Stellite etc corrodeto form solubles, colloids and particulates which, are transported to the core and activated. These activated corrosion products are re-transported by the coolantand deposited on out of core surfaces. 60Co is foundto be one of the main contributors to the radiationfields existing on out of core surfaces. Most of thecorrosion product oxides in the PHT system arespinel type of oxides. Effective pH and chemistrycontrol, Hot-conditioning etc. minimize corrosionand corrosion product solubili ty whereassub-micron filtration, Ion-exchange purification etc. reduces the inventory of corrosion products in thewater coolant. Full system decontamination andcomponent decontamination help in reducing thisradiation field but the beneficial effect is availablefor short duration. A long-term remedy shouldaddress the root cause of the problem namelycorrosion and corrosion release. All the externaladditives added to the PHT system aim at achievingthis goal.

Protective Oxide Film on Metals

Controlling the corrosion and corrosion release of materials involve understanding the mechanismof formation and stability of the corrosion productfilms on them. Corrosion of structural materials like

IANCAS Bulletin 127 April 2008

Hariharan Subramanian, Water and Steam Chemistry Division, BARC Facilities, Kalpakkam, Tamil Nadu 603 102; E-mail: [email protected]

Hariharan Subramanian (M.Sc. Applied Chemistry, Cochin University of Science and Technology, India) joined Water and Steam Chemistry Laboratory of Bhabha AtomicResearch Centre in the year 1997. His field of interest includes decontamination andhigh temperature aqueous corrosion.

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Carbon steel, Stainless steel etc. in the PHT circuitresults in the formation of duplex layers (Fig. 1). Theinner layer is a few nanometers thick and finegrained. The outer layer can run in to a few micronsand consists of large crystallites and is highly porousin nature. Growth of oxide film proceeds by ionictransport in the film. The composition and structureof the film determines the species that moves acrossthe film. Build-up of oxide film on reactor structuralmaterials is due to the transport of oxygen andcationic species to and from Oxide-Solutioninterface. Cation transport contributes to filmgrowth, film dissolution and re-deposition. Thedriving force for this mobility is either aconcentration gradient or a potential gradient. MetalOxide to metal volume ratio (P.B ratio) for IronOxide Fe3O4 is ~2.1. This indicates that only ~50%of the iron (as oxide) corroding from the base metalis required to fill up the void created by its removal.The rest of the iron is transported to the oxidesolution interface. This iron can deposit insitu asouter oxide or can be transported and removed bypurification or deposited elsewhere in the PHTsystem. The growth stresses in the inner layer due tovolume constraints creates micro pores which canact as access channels for the water to reach the basemetal. In the case of availability of an external circuit for charge flow, the conversion of excess iron tooxide need not occur insitu. Depending on theconstituents of the base metal, the inner and outerlayer composition varies and it also affects thekinetics of the process.

Activity incorporation in Oxide

Many activity deposition mechanisms such asco-precipitation, adsorption, ion exchange areknown which result in accumulation of 60Co on these spinel oxides. The intake of activity in to this filmcan be in different ways. Activity as particulates canstick to these oxide surfaces. Activities in solubleform can be adsorbed or exchanged on the outerlayer oxide. The activity can also be incorporatedright during the formation of the outer layer. Theinner layer porosity is very less, so ingress of activity in to this layer demands transport through grainboundaries or by transportation along lattice defects. In the point defect model the film grows bygeneration of cation vacancies at the oxide solutioninterface and their annihilation at the metal oxideinterface. The resulting flow of vacancies is the basis of film growth in this model. These vacancies canpick up these active metal ions. An alternative to thisis the transportation of activity along the grainboundaries. The diffusion constants indicate that thegrain boundary diffusion is more (five orders ofmagnitude larger) feasible than volume/Latticediffusion. Of course the pore diffusion constant doesdominate, but as mentioned earlier the extent ofporosity in the inner layer is extremely small. So60Co could migrate in to the pores under aconcentration gradient. Electrical field in the oxidewill counteract this and the rate will be reduced. Atthe end of a closed pore, grain boundary transporttakes over and further incorporation in to the grain isby lattice diffusion. The latter step is a very slow oneas compared to the other two. Hence, activityincorporation can take place both in the outer andinner layer of oxide.

The activity transport and hence radiation fieldbuild up are part of the corrosion phenomenon andhence can be controlled by controlling the corrosionof reactor structural materials. Corrosion can becontrolled by the following ways:

1. Pre conditioning of structural materials (likehot conditioning)

2. Optimisation of water chemistry

3. Metal ion passivation

Use of structural materials containing no orminimum cobalt and full system decontamination

April 2008 128 IANCAS Bulletin

Fig. 1 Duplex film

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are other options available for reducing the radiationfield.

Flow Accelerated Corrosion (FAC)

Flow accelerated Corrosion is a process bywhich the normally protective oxide layer on carbonor low alloy steel dissolves under the influence of astream of flowing water or a water- steam mixture.Under the influence high flow velocity andturbulence of the coolant, the oxide layer becomesthinner and less protective. In some instances theoxide layer may be so thin as to expose bare metalsurface1. The damage caused by this type ofphenomena can lead to a general reduction of wallthickness rather than a local attack (Fig. 2). In asingle phase flow (only water) FAC, when thecorrosion rate is high, the metal surface has ascalloped appearance (Fig. 3). For two-phase flow,the surface will have ‘tiger striped’ appearance. Therate of FAC depends upon hydrodynamic factorssuch as flow velocity, pipe roughness and geometryof the flow path etc., In addition, the environmentalfactors like temperature, pH, reducing agent andoxygen concentration and metallurgical factors likethe composition of steel also affects the rate at whichthe carbon steel undergoes FAC. Thus, metal lossdue to this phenomenon occurs over a limited area ofpiping due to high turbulence.

FAC in PHWR Feeder

A schematic diagram of the PHWR primarycoolant system is given in Fig. 4. The primary circuitof PHWR reactors contains considerable quantitiesof carbon steel as the material of the feeder pipes andheaders that connect the reactor fuel channels to thesteam generator. FAC leading to wall thinning ofoutlet feeders, was first observed in one of the

CANDU reactor in 1994. Wall thicknessmeasurements, especially at the extrados of the firstbend, showed that this type of corrosion can reducethe wall thickness of the feeders to below theallowed limit within the reactor life time.

IANCAS Bulletin 129 April 2008

Fig. 2 FAC induced wall thinning

Fig. 3 Typical single phase FAC pattern

Fig. 4 Schematic of CANDU primary heattransport(4) system

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The susceptibility of outlet feeder for FAC canbe understood by observing the D2O flow path(Fig. 5). The D2O leaves the end fitting annulus at aright angle and enters the Grayloc hub resulting in adisturbed turbulent flow at the entrance to the outletfeeder. The operating coolant velocities in coolantchannels of PHWRs range from 8 to 18 ms-1,yielding turbulent Reynolds number.in the range of106 to 107. Steam quality in PHWRs is in the range 0– 4 wt%.

The investigations carried out on the specimentaken out from the reactor showed a clear indicationof single phase FAC in outlet feeders (seeing a

temperature of 300°C and a coolant velocity of15m/s) as its surface was having a scallopedappearance4. On comparison with the unusedspecimen, the corrosion rate of the outlet feeder was

found to be 100 – 150 mm/y which is much higherthan the corrosion allowance provided during the

design i.e. 75 mm/y. Where as, the grayloc hub of theoutlet feeder which joins the feeder to the end fittingand containing 0.13% Cr, showed corrosion rate of

only 20 mm/y.

Even though secondary side experiences show

that FAC can occur at the temperature of 170°C also,no FAC was observed on inlet feeders where similarflow conditions exist as that of outlet feeders. Theprimary coolant loaded with iron enters the steamgenerator where the temperature drops from 300 to250 C. This results in deposition of Iron in the steamgenerator tubes starting from the beginning of 180bend near the hot leg and continues up to the core

inlet. Coolant iron concentration drops to lowervalues during this transit. This fluid is again heatedto 300oC across the core. The Iron saturationsolubility is higher at 300oC as compared to 250oC atthis temperature. The fluid under saturated in ironexits the reactor core and interacts with the carbonsteel outlet feeders leading to excessive wear. Thisindicates that FAC is favoured when the coolant isunder saturated with respect to dissolved iron. TheCr content in carbon steel was found to prevent FACby forming a less soluble Cr rich oxide layer.Various loop studies showed that the threshold Crconcentration in Carbon steel to reduce FAC is0.04%. Hence, it is expected that 0.2 % of Cr in CSwill effectively reduce FAC.

Laboratory studies also indicated that lowering pH from 10.8 to 10.2 drastically reduced FAC rate.But the same effect was not observed in reactor, FAC rate decreased when pH was lowered from 10.8 to10.4 but increased to its initial value when pH wasfurther reduced to 10.2. Understanding the effect ofpH on FAC is important from the point o view ofreducing FAC in the operating plants, whereasswitching over to Cr rich carbon steel could solve the problem for new reactors.

Optimisation of Water Chemistry

By efficient water chemistry control it ispossible to control corrosion of these materialswhich in turn reduces the out-of-core contamination. In PHWRs, a pH300 of 7.4-7.6 is maintained usingonly LiOH and reducing condition is achieved byinjecting 3- 10 cm3/kg H2 into the primary coolant. In all the reactors, utmost importance is given to purityof water with main emphasis on checking ingress ofionic impurities to minimise corrosion. Similarlydissolved oxygen is controlled (to <10 ppb) in orderto protect the structural materials from general andlocalised corrosion like IGSCC etc.

Maintenance of pH is one of the main criteriafor coolant chemistry control. The importance ofwater chemistry control can be understood byanalysing the mechanism of activity transportbrought about by both soluble as well as particulatecorrosion product oxides. For practical purposes it isassumed that whatever passes through 0.45ìm filterconstitutes soluble species. In PHWR, the dominant

April 2008 130 IANCAS Bulletin

Fig. 5 Flow path of D2O in the End fitting outletfeeder region

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corrosion product oxide is magnetite (Fe3O4) andnickel ferrite (NixFe3-xO4).

Control of soluble species transport

The soluble ions along with the radionuclideget incorporated in the growing oxide layer throughco-precipitation. The dissolution/crystallization ofthe oxide layer is a combination of two processes i.e.dissolution/crystallization of oxide crystal on thesurface and mass transfer of dissolved ions acrossthe boundary layer (Fig. 6).

The processes are mainly driven by thedifference in concentration of iron in the bulk (Cb)and the solubility of iron in the corrosion productoxide (Cs ) at the temperature of the surface film.Solubility for pure magnetite and nickel ferrite hasbeen widely studied. Solubility of magnetite can berepresented by the following equilibrium,

1/3 Fe 3O4 + (Z-b) H+ + (4/3 – z/2) H2 «Fe(OH)b

(Z-b)+ + (4/3 – b)H2O

where z =2 refers to Fe2+ and Z=3 refers to Fe3+ , b=0to 3 for Fe2+ and b=3 to 4 for Fe3+

Solubility Cs = S[Fe(OH)b(Z-b)+]

As can be seen from the above equation,solubility is controlled by pH (maintained by usingLiOH ), dissolved H2 and hydrolysis constants of allthe iron species and their dependence ontemperature. The concentration of Fe2+ species isproportional to p(H2)

1/3 and Fe3+ is proportional top(H2)-1/6 , indicating that the dependence ofsolubility on dissolved H2 is fairly weak. pHT can be

calculated from the above equilibrium, by setting upcharge balance equation for the system, and usingbest estimated Kw values at any given temperature.In cases where boric acid/ ammonia is present alongwith LiOH, their dissociation reactions are alsoincluded for pH calculation. The hydrolysisconstants for various iron hydroxides are computedusing principles of thermodynamics.

Similarly for Nickel ferrite, the equilibrium isgiven by

3NiFe2O4 + 4H2 « 2Fe3O4 + 3Ni +4H2O

and NiFe2O4 + H2 + 6H+ « Ni+2 + Fe2+ + 4H2O

Ni2+ +m OH- « Ni(OH)m(m-2)-

Fe2+ + n OH- « Fe(OH)n(n-2)-

To reduce radiation field build up in reactorsthe recommended pH should be such that, at that pHT

there is minimum corrosion release from structuralmaterials and minimum deposition of corrosionproducts in the core. So, a pH of minimum solubilityand zero temperature coefficient of solubility [TCSi.e. (dS/dT)p H = 0] is desired. Numerousexperimental studies of magnetite solubility havebeen carried out by different groups, in the range of

200°C to 300°C with H2 in the range 10 – 20 cm3/kg.The pH300 of minimum solubility observed, rangedfrom 6 to 8. The variation of magnetite solubilitywith pH300 calculated ( Tremaine and Leblanc) isgiven in Fig. 7 .These solubility studies show that at

normal PHWR operating temperatures (~300°C)there is a negative temperature dependence ofsolubility of iron in acidic solutions, a zerotemperature dependence in weakly alkalinesolutions and a positive dependence in moderate andhigh alkaline solutions. Similar observations weremade by Sandler and Kunig in their experimentsmeasuring solubility of a variety of synthetic

non-stoichiometric nickel ferrite from RT to 350°C,with H2 10-20 cm3/kg that yielded a pH300 ofminimum solubility in the range of 5.0 to 8.5. Figure7 demonstrates the variation of solubility of iron inmagnetite with temperature for given pHT. It showsthat At pH25 <9.7 there is a negative temperature

gradient for solubility, where as pH25 ³ 10 haspositive temperature gradient of solubility. It implies that at PWR and PHWR operating temperatures, thecoolant traversing through the core sees drivingforce for dissolution if any oxide is present in coolant

IANCAS Bulletin 131 April 2008

Fig. 6

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or on in-core surfaces. For the steam generator

surfaces where temperature decreases from 320°C to

250°C, the solubility tends to decrease and thesupersaturation of the coolant is relieved by oxideprecipitation or crystallization on the surface. HencepH25 of 10 and above are favourable for minimizingin-core deposition and it is the basis for the existingpH25 range of 9.5 – 10.5 (approximately equal topH300 of 7.2 Fig. 8) in PHWR. These solubilitystudies are quite helpful in understanding thescientific basis involved in the phenomena. It shouldbe noted that the stoichiometric composition ofoxides formed in reactor systems are not well

defined and so are different from whatever oxidesare studied in laboratory experiments. Also lots ofuncertainties exist because of the differences in theavailable correlations for Kw used for hightemperature pH calculation. These factors lead tolarge standard deviation in pH of minimumsolubility and large pH range for the occurrence oftotal corrosion product solubility co-efficient (TCS)

³ 0.

Metal Ion Passivation

Once the transport of iron across the inner layer is altered, corrosion is reduced. This in turn reduces

April 2008 132 IANCAS Bulletin

Fig. 7 Magnetite solubility variation with temperature and pH

Fig. 8 Magnetite solubility as a function of High temperature pH

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the inventory available for activation in the core,which results in lowering of radioactivity build up.In the Metal Ion Passivation technique (MIP) ahighly protective, tenacious film is formed on themetal by continuous injection of the modifying ion(in ppb levels). This film results in reduced activitybuild up and lower corrosion rates. It is still not fullyknown how this added metal ion helps in achievinglower radiation levels. The added metal ion has beenfound as ferrite on the metal, but the added amount isnot sufficient enough to form a uniform protectivecoating over the metal. Its presence in grainboundaries, thus effectively blocking transportpathways have not been proved conclusively.Re-circulating loop experiments have demonstratedthe effectiveness of this procedure, but conclusiveproof is elusive.

Plant and loop experience

MIP methodology was first adopted by BWR’s and is widely used now[1]. Zinc as depleted ZincOxide (to avoid 64Zn) is the passivating agent used.Re-circulating loop and plant experience have amply demonstrated that Hydrogen water chemistry(reduces stress corrosion cracking of stainless steels) along with zinc injection reduces radiation fieldbuild up. In re-circulating loop experiments manyother ions like (Mg, Mn, Ni) have been tried andwere found to be effective. In PWR’s also beneficialeffects were found in loop experiments. It was foundthat on new metal surfaces, zinc addition results inthinner oxide layers and lower incorporation ofcobalt in to the oxide. Depth profile studies haveindicated presence of 60Co and Zn in the outer layer.In Farley-2 reactor, channel head dose ratesdecreased considerably during Zinc addition. [2]

MIP in PHWR

Under PHWR chemistry conditions only somere-circulating loop experiment data is available. In

the case of 410SS, the 60Co activity depositedreduced by a factor of 10 and for carbon steel itreduced by a factor of 2 a t 10ppb Znconcentration.[3] Similarly iron release rates forcarbon steel came down by a factor of 18 andcorrosion by a factor of 2.5 and for SS410 it reducedrelease by a factor of 16 and corrosion by a factor of8. Some studies carried out with Mg have also shown reduction of Corrosion and corrosion release inCarbon steel and Monel.

The beneficial effects of passivating metal ionwere found at lower concentrations and it did notimprove on further addition. This indicates that theprotective behaviour is not due to the formation offilms ie Zinc ferrite, but may be the presence of theseferrites or oxides in the grain boundaries and thusblocking them. The role of zinc ion in reducing theradiation field build-up in the stainless steel surfacesof BWRs and PWRs is being studied to understandthe mechanism of its action. Alternative metal ionssuch as Mg2+ can be a substitute for zinc ionespecially in PHWR primary coolant systems.Hence, an in depth study to understand the effect ofpassivating metal ions for a system dominated bycarbon steel such as the PHWR primary coolantsystem is necessary.

Reference

1. In addition experience under normal andHydrogen addition Chemistry, R.L. CowanJAIF98, pp 225-232

2. C.A.Bergmann et.al. Overview of Zincaddition in the Farley –2 reactor, WaterChemistry of Nuclear systems 7, pp 287-292BNES 1996

3. H.A.Allsop et.al. Water Chemistry of Nuclearsystems 7, pp 552-557, BNES1996

4. S.S. Bajaj , A.R. Gore, Nuclear Engineeringand Design 236 (2006) 701–722

IANCAS Bulletin 133 April 2008

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Role and Responsibilities of a Station Chemist in aNuclear Power Station – A Perspective

The job of a Station Chemist in a NuclearPower Station is multidisciplinary in nature and hehas a major role to play in the smooth, safe andefficient operation of the Power Station. The primeresponsibilities of the Station Chemist are :

1. Optimisation of Chemical Control parametersto minimise corrosion related problems in thereactor / conventional systems and in thevarious heat-exchangers of the processsystems.

2. To maintain the chemical parameters in all thesystems well within limits as required by theTechnical Specification Documents of theStations. Any deviations/off-normal values ofthe chemical parameters are to be brought tothe notice of the Station Management and alsoto be reviewed by the Station OperationsReview Committee (SORC).

3. To minimise the build-up of radiation fields onthe out-of-core surfaces of the Primary HeatTransport / Coolant System so as to reduceman-rem / person-sievert expenditure of thestation during maintenance works.

4. Active participation in the ageing managementand PLEX programmes of the Station.

5. To ensure the reliability of the analytical datagenerated in the Chemical Control Laboratory.

6. Upgrading the analytical facilities of thelaboratory and to ensure the reliableperformance of the laboratory analyticalinstruments as well as that of the on-line

analysers of the process systems to take prompt corrective actions as and when required.

7. Adoption of fast and reliable analyticaltechniques.

8. Updating the professional knowledge of thechemists by proper coordination with R&Dlaboratories and making available theliterature/ reports related to the latestdevelopments in the Power Reactor WaterChemistry.

9. Implementation of the good practices.

10. Strict chemical control measures to be adoptedin the water cooled systems of reactor safetyrelated equipment like Diesel Generators.( Ex:Jacket cooling water circuits )

11. Chemical and biofouling control in the tertiarycircuits of the Power Station (Ex: CoolingTowers, Condenser Cooling Systems). In thecoastal-based stations, macrofouling control in the sea water cooling circuits assumes utmostimportance for the efficient performance of theStation.

12. Preservation of process circuits/systemsduring shutdown periods.

In order to fulfill the above objectives anddischarge the responsibilities/duties in an efficientmanner the Station Chemist should have theknowledge of following .

1. Understanding the Operational & Engineeringaspects of all the systems of the Station.

April 2008 134 IANCAS Bulletin

Dr.K.S. Krishna Rao, Station Chemist & HW Manager, Madras Atomic Power Station, Kalpakkam 603 102;E-mail:

Dr.K.S.Krishna Rao is from the 14th Batch of BARC Training School and joined in theChemistry Division, BARC in 1971. Subsequently he was transferred to RAPS in 1974and then to MAPS as Station Chemist in 1976. He has rich experience of 37 years in thefield of Power Reactor Water Chemistry. He obtained his Ph.D degree from theUniversity of Madras in 1989.

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2. Metallurgical aspects of the structuralmaterials of the circuits /systems withreference to corrosion control.

3. Knowledge of the laboratory analytical/on-line instruments.

4. Radiological & Industrial Safety aspects.

5. Chemical and Physical properties of thelubricating / insulating oils used in StationElectrical Equipment and their testingprocedures.

6. Biological aspects of corrosion

7. Spectroscopy techniques viz., Infrared,Atomic Absorpt ion, UV –Visible ,Radiochemical & Gamma spectral analysesetc;

The normal routine analytical works carriedout in the Chemical Control Laboratory of the PowerStation( PHW type) are:

1. Isotopic analyses of heavy water samples in the range of 0.01% to 99.98% D2O

2. Determination of the concentration of ionicand metallic impurities at ppb/ppm levels inlight &heavy water samples.

3. Analyses of ion-exchange resins.

4. Radiochemical analysis for fission andcorrosion products.

5. Analyses of insulating and lubricating oils forcritical parameters.

6. Analyses of cover gas samples of Moderator,PHT& Turbogenerator systems by GasChromatography and also checking the purityof the gases in cylinders procured by theStation

The following significant chemistry relatedjobs carried out at MAPS illustrate the aboveviewpoints / importance of chemical control andgives a perspective of the role of the Station Chemist.

1. A total number of six Dilute ChemicalDecontamination Campaigns (three in eachreactor) were carried out in the Primary HeatTransport (PHT) Systems of MAPS-1&2during the period 1993-2003 in order to reducethe out-of-core radiation fields mainly due toCo-60 activity in collaboration with /guidance

of WSCD/ BARC, COSWAC and NPCIL -HQ after getting approvals from safety bodies. Theobjectives of the campaigns carried out during2001 in MAPS-2 and during 2003 in MAPS-1were to reduce the man-rem / person- sievertexpenditure during the Enmass CoolantChannel Replacement (EMCCR) jobs. Thehigh Co-60 activity in the PHT systemsencountered during the initial period ofoperation of the reactors was due to use ofstellite (Cobalt - based alloy) coated primaryseals in the Primary Coolant Pumps.Subsequently, the seals have been replacedwith Cobalt free alloys. Hence by reducing thesource term of cobalt 59 and with DCDCampaigns, the radiation fields on theout-of-care surfaces had got reducedsignificantly. During 1993 (i.e., before the firstDCD campaign of MAPS-1) the totalman-rem(external) consumption in bothreactors was 822 whereas it was 118 in 2007after the six DCD campaigns and taking thecorrective measures as mentioned in thisarticle.

2. The cover gas in the PHT storage tank waschanged from costly helium to nitrogen inMAPS-2 during the initial operation of thereactor in 1985 on an experimental basis. Afterensuring the satisfactory performance ofnitrogen gas with respect to Chemical Controland also from the operations viewpoint ,nitrogen was continued as the PHT cover gas.Subsequently the cover gas in the PHTSystems in all the Indian PHWRs had beenchanged over to nitrogen. This change over had proved to be cost effective and also beneficialfrom the chemistry view point. However thePHT cover gas in PHWRs abroad continued tobe helium. (Maximum limit for nitrogen : 6%V/V).

3. MAPS has twin PHW- type reactors that usessea water for cooling the main steamcondensers of the Turbines. In the case of leaksfrom the condenser tubes during the period1983 to 1989, the sea water contaminatedcondensate/feed water used to go directly to the Boilers/Steam Generators, resulting in highspecific conductivity and low pH (due tohydrolysis of MgCl2 present in sea water) in the

IANCAS Bulletin 135 April 2008

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Boiler water, highly conducive for corrosionphenomena. The congruent phosphate treatmentused to be carried out during the ingress occasions ofthe sea water has not been found satisfactory. Hencefull flow Condensate Polisher Plant (CPP) withmacroporous resins was retrofitted in 1989 in thecondensate and feed water circuits of both thereactors.

Morpholine has been used as the alkalizingagent to maintain the pH of the secondarycircuit (Boiler feed water) in the range of 8.8 to9.2 in all PHWRs. It gets uniformly distributedin the circuit as the distribution ratio betweensteam and water is 1.3 at 2500C. Since thecation resin of the CPP removes morpholine asmorpholinum ion, booster dosing is done at thedown stream of the ion-exchange (CPP) beds.As the cation gets saturated with morpholine,leaching of sodium ion increases from CPPbeds resulting in the pH variations and highionic conductivity in the SG/Boiler water. Inaddition, sulphate leaching has also beenobserved from the macroporous CPP resinswhen condensate temperature was high(>45oc) resulting in reduction in pH of BoilerWater . The increase in morphol ineconcentration has not been found to improvethe situation. In fact it has been observed thatthe leaching of ionic impurities from thesaturated beds used to increase with themorpholine concentration. Hence vigorousefforts have been made to identify a superioramine to replace morpholine. Based on thepublished reports and the R&D work carriedout at WSCD, BARCF, it has been decided touse Monoethanolamine (ETA) in thesecondary circuits of both MAPS-1&2 aftergetting necessary approvals from COSWACand safety bodies. The advantage with ETA isthat the pH in the secondary circuit increasesprogressively from hot well (8.5-8.6) toBoilers/ Steam Generators (9.3-9.5) and thequantity of chemical required is also less(One-third of morpholine) due to higherbasicity. As the concentration of ETA isminimum (~1 ppm) at CPP inlet (unlikemorpholine which will have concentration of6-8 ppm due to the uniform distribution), theservice cycle of the beds is prolonged before

saturation and hence minimises the leaching ofionic impurities. Apart from better ChemicalControl in SGs, the change over frommorpholine to ETA at MAPS resulted in theoverall savings of ~ Rs.25 lakhs per annummainly due to the lower consumption ofchemicals and also reduced frequency ofregeneration of CPP ion-exchange beds. Afterthe good experience at MAPS, the other IndianPHWR stations switched over to ETA.. Thecost effective chemical treatment in thesecondary circuit at MAPS has been selected as a good practice by CANDU OWNERSGROUP (COG) and put on their website asCOG-GP-20. MAPS-1 was the first PHWR toeffect this change.

4. Colloidal activity contributes 20-30% to theradiation fields on out-of-core surfaces of thePHT system and the major contributors areCo-60 & Zr-Nb- 95. In order to reduce theradiation fields due to colloidal activities,sub-micron filters (1.1 micron size absolutefilters) have been installed in the PHT systemof MAPS-1 since 1998 and in MAPS-2 from2003 onwards. The normal cellulose basedfilters used in the PHT system remove particlesof 10 microns and above only.

5. The performance of the heat-exchangers play amajor role in Heavy Water Reactors. Anypinhole leak in the tube of a heat-exchanger,results in the tritium and radioactivity releaseand contamination of cooling water on the shell side. In RAPS-1&2 lake water is used (once-through) for cooling these heat–exchangersand from MAPS onwards this has beendesigned as closed loop system withchemically treated demineralised water. Thischange helped significantly in minimising thecorrosion re la ted problems in theheat-exchangers. It is gratifying to note that theperformance of these HXs at MAPS has beenextremely good and the percentage of pluggedtubes in the past 25 years of operation was verylow. (< 5%)

6. The growth of small sized barnacles (Balanusreticulatus) has been found to be high in theProcess-Sea water Heat-Exchangers as thetemperature was conducive for their growth

April 2008 136 IANCAS Bulletin

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and as a result the heat transfer was affected.Further it has been found difficult to cleanthese HXs during shutdown periods as thefouling calcareous deposits were hard innature. Actibromide Treatment has beenstarted in these HXs since 1995 to control thegrowth of barnacles and the treatment wasfound to be effective in minimising the foulingand improved the performance of the HXs.Further it has been found easy to clean these

HXs in short time during shutdown periods asthese deposits were found loose and less inquantity with actibromide treatment.

Thus the Station Chemist plays a major role inminimising corrosion related problems, reduction inmanrem expenditure, PLEX programmes andefficient performance of the Station by optimisation/ maintenance of good chemistry control in variousprocess systems.

IANCAS Bulletin 137 April 2008

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Gamma spectrometric measurements on PHT andModerator systems of PHWRs

April 2008 138 IANCAS Bulletin

Dr. B.S.Tomar obtained his M.Sc. Degree in chemistry from Garhwal University,Srinagar in 1979. He joined the 25th batch of the BARC Training School in 1981 and wonthe Homi Bhabha Prize for securing the academic excellence. Subsequently he joined the Radiochemistry Division in 1982. He obtained his Ph.D. degree in Chemistry fromBombay University in 1990. His areas of research include Nuclear Chemistry in generaland Nuclear Fission, Nuclear reactions, Perturbed Angular Correlation, Ion BeamAnalysis and Speciation of actinides and fission products in particular. He is a Ph.D.guide of University of Mumbai as well as professor of Homi Bhabha National Instituteand has a large number of publications in the international journals. He is a member ofthe IAEA expert panel on Radiation Detection and Measurement. Presently he is heading the Actinide Chemistry Section of Radiochemistry Division, BARC.

Dr. V.K. Manchanda

Shri Sumit Kumar joined the Radiochemistry Division, BARC, in 2003 after graduatingone-year training program on Nuclear Science and Technology of BARC Training School.His research interests are application of Radio-analytical techniques in various scientificproblems and Actinide Speciation in environment.

Shri T.P. Chaturvedi, an electronic engineer, joined Radiochemistry Div, BARC in 1981.He has extensive experience in radiation detector systems and nuclear instrumentation. He has developed computerized data acquisition systems for fuel pin scanner and LVDTmicroscanner for post irradiation examination of reactor components. He interfaced andautomated the cryogenic temperature controllers for positron annihilation spectrometryand data acquisition system for photo acoustic spectrometer. His current interests includedevelopment of magnetic barkhausen noise acquisition system for the study of stresses inreactor components, digital signal processing for zero dead time spectrometers andassessment of the high radiation field at power reactors. He is a member of The Institutionof Engineers (I).

Dr. B.S. Tomar, Shri Sumit Kumar, Shri T.P. Chaturvedi and Dr. V.K. Manchanda, Radiochemistry Division, Bhabha AtomicResearch Centre, Mumbai 400 085; E-mail:

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Introduction

Minimising radiation field buildup in theprimary heat transport system (PHT) has been thefocus of water chemistry maintenance inwater-cooled nuclear power plants. Identificationand quantification of the radionuclides responsiblefor the high radiation levels in the PHT system helpsin planning the decontamination strategies, inpredicting the rate of build up and in evaluating theeffectiveness of water chemistry domain. Thisrequires on-line gamma ray spectrometricmeasurements at various locations of the PHT,where the radiation levels may vary from a few mR/h to a few hundred mR/h. Further the ambient

temperature in some areas may be as high as 40°C atwhich conventional high resolution HPGe detectorsare extremely difficult to use. HPGe detectorsrequire the cooling to liquid nitrogen temperatureand need the associated electronic set up. Further thelarge volume (50-100cm3) of the Ge detector,commonly available in radiochemical laboratories,leads to high-count rates and hence high dead time/pile up effects. NaI(Tl) detector, though can beoperated at room temperature, but suffers from thelimitations of poor energy resolution (~7% at 661keV) with which it is not possible to resolve the close lying gamma lines in the gamma ray spectrum. Inview of this a small volume (0.5cm3) CdZnTedetector connected to a portable multi-channelanalyzer (MCA) was used for gamma rayspectrometric measurements. The present articlegives a br ief descr ipt ion of some of themeasurements carried out at the PHT and moderatorsystems of PHWRs at Narora (NAPS#1 &2),Rawatbhata (RAPS#3 &4) and Kakrapar(KAPS1&2).

Detection System

The detector is based on high band gapsemiconductor (CdTe) with small amount of Zn toincrease the resistivity of the detector material. Thehigh band gap (1.6 eV) enables it to be operated atroom temperature. At the same time the relativelybetter energy resolution (~2% at 661 KeV)compared to NaI (Tl) detector is sufficient to resolvethe gamma lines of interest. The small volume of thedetector helps in using it in high radiation fieldswithout any dead time/ pile up effects, which was

further taken care of by shielding the detector with a75mm thick lead shield. The details of the detectorsystem can be found in [1]. Figure 1 gives thephotograph of the CdZnTe detector system. Sincethe dimensions of the source of gamma rays are large compared to that of the detector, the measuredactivity is the sum total of all the activity due toradionuclides deposited through out the pipelines inthe vicinity of the detector system. In order tominimise the contribution from surroundings, thedetector was housed in a cylindrical lead shieldhaving OD=75 mm, ID=30 mm with a collimator inthe front having OD=75 mm, ID=10 mm andlength= 100 mm. The entire assembly was housed inan aluminum casing so as to make the shield and thecollimator concentric. Figure 2 shows the schematicof the collimator.

Gamma Ray Spectrometric Measurements

The first set of Gamma ray spectrometricmeasurements were carried out on PHT, Moderator,End-shield and Calandria Vault of NAPS Unit # 2dur ing May 24-25, 2005. Subsequent lymeasurements were carried out on PHT andmoderator lines of both the units of Narora AtomicPower Station (NAPS) during May 15-18, 2006.These were followed by measurements on the PHTsystem of RAPS3 during September 8-9, 2006 and at KAPS1&2 during November 30- December 1, 2007. The length of the collimator for measurement atKAPS was reduced in view of the lower levels ofradioactivity. The efficiency calibration of the

IANCAS Bulletin 139 April 2008

Fig. 1 CdZnTe detector system

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detector was carried out by counting the standardsource of 154Eu in the desired geometry of a pointsource as well as an extended source in the form of apolypropylene tube of length 100mm and diameter30mm. Correction factors for contributions fromsideways to the spot of measurements were alsodetermined by measuring the count rate from intensesources of 137Cs and 60Co kept at a varying distancefrom the center of the collimator.

Results and Discussion

Figure 3 shows the gamma ray spectra of PHTpurification by-pass lines as well as the PHT fluidsample of NAPS-2, which suggests much higherconcentrations of fission and activation products inthe pipelines as compared to the fluid samples. Thespectra show that the major activity in both thesamples is due to 124Sb. Figure 4 shows the gammaray spectra of moderator pipelines in the purificationbuilding and the moderator fluid sample. In this casethe dominant activity is due to 60Co. Figures 5 showsthe typical gamma ray spectrum recorded at RAPS-3FM Vault (North) in the Reactor Building, where theactivity levels were maximum. The gamma rayspectra of CdZnTe detector were analysed using thepeak fitting program, PHAST, developed byElectronics Division, BARC. The program employsnonlinear least square fitting of the gamma peakswith a function comprising a Gaussian with lowerexponential tail and polynomial background. Theshape parameters of the peaks as a function ofgamma ray energy were obtained using the gamma

ray spectra of 154Eu, which was also used forefficiency calibration of different geometry samplesand energy calibration of the MCA. The lowerexponential tail is a significant feature of the gammaray peaks in CdZnTe detector due to large number ofelectron trapping centers present in the crystal. Theactivity of radionuclides deposited in the pipe lineswere obtained from the measured count rates aftercorrecting for the detection efficiency, contribution

April 2008 140 IANCAS Bulletin

Fig. 2 Collimator set up

Fig. 3 Gamma ray spectra of PHT system ofNAPS-2 (a) line (100s), (b) fluid (300 s)

Fig. 4 Gamma ray spectrum of Moderator line ofNAPS-2

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from sideways and the activity deposited on theopposite side of the pipe.

Table 1 and 2 give a comparative data of

activity of 124Sb and 60Co (in mCi/cm2) fixed on the

PHT piping and other locations in Reactor Buildingand Reactor Auxiliary Building of NAPS#1, RAPS#3 and KAPS#2.. As can be seen from thetables, PHT pipelines of all the reactors arecontaminated with 124Sb at certain locations, whichhas a half life of 60 days and has a large number ofgamma rays ranging from 603 KeV to 2.09 MeV.The spectra recorded on other parts of PHT lines also revealed some fixed activity due to 60Co though thePHT fluid sample did not show any activity due to60Co. The activity of 124Sb in the PHT fluid samplewas found to be very small compared to thatobserved in the PHT lines and hence was notcorrected for in the in-situ measurements. Thegamma spectrometric survey, from PHT bleedcircuit up to purification inlet line, indicatedpresence of 124Sb along with contribution from 60Co.Comparison of the activity in pipe lines and fluidsamples revealed that most of the gamma activity

IANCAS Bulletin 141 April 2008

Fig. 5 Gamma ray spectrum of EM vault (N) ofRAPS-3

TABLE 1. Comparison of activity (mCi/cm2) of 124Sb at different power stations

Lo ca tion NAPS1 NAPS2 RAPS3 KAPS2

Shut down start date ÷ 15.10. 2005 14.05.2006 29.08.2006 01.11.2006

Measurement date ÷ 15.05.2006 16.05.2006 08.09.2006 30.11.2006

Bleed Condenser 8.4 2.5 2.0

PHT Bleed Condenser Inlet 5.8

PHT Bleed Condenser outlet 8.4 2.5

Up stream BCD CV 8.2

Regenerative HX 6.6

SG Hot leg 0.4 0.9

SG cold leg 1.4

Shutdown HX-I 1.2

Down stream of primarypressurising pump

2.8

PHT PCP 0.7

PHT purification inlet 2.8 12.2 7.9

PHT purification outlet 1.8 9.8 2.1

FM Vault (S) Close position 34.5 7.2

FM Vault (N) close position 55.8 7.3

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observed in the pipe lines of PHT system has gotfixed in the pipelines. In comparison to otherlocations inside Reactor Building, the observedactivities are higher in FM Vault areas, which ismainly due to 124Sb and 60Co.

In the case of KAPS#2 the FM vault (N) wasobserved to have higher radiation levels than that inFM vault (S). The difference was found to be due to60Co, while the 124Sb activity was same in both thelocations.

Conclusions

The measurement of gamma activity ofradionuclides present in the PHT and moderatorlines were carried out using a small size CdZnTedetector . I t is now established that suchmeasurements can be easily made in power plants for quantification of radioactive contamination. Thedata showed significant activity of 124Sb in PHT lines and that of 60Co in moderator lines. Comparison ofthe on line measurement data with that of the fluid

samples revealed that most of the activity was fixedon the pipe lines. Measurements were also carriedout on the feeder pipes in FM Vault, which showedsignificant activity mainly because of 124Sb and 60Co.

Acknowledgements

Authors thank the station chemists ofNAPS1&2, RAPS3&4, and KAPS1 &2 for theircooperation and fruitful discussions during thesemeasurements. Thanks are also due to ShriH.R.Bhatt, Additional Chief Engineer (Chemistry,Fuel & Heavy water) Nuclear Power Corporation ofIndia Limited, for his keen interest and initiative inthis work.

References

1. Development of CdZnTe based portablegamma-ray spectrometry for field studies, B.S.Tomar, D.A.R.Babu, P.K. Mukhopadhyay,P.A. Satish and V.D.Shrivastava, NationalSymposium of Radiation Physics, BARC,Mumbai Nov. 2003, paper no. 82.

April 2008 142 IANCAS Bulletin

TABLE 2. Comparison of activity (mCi/cm2) of 60Co at different power stations

Lo ca tion NAPS1 NAPS2 RAPS3 KAPS1 KAPS2

Shut down start date ÷ 01.11.2005 14.05.2006 29.08.2006 — 01.11.2006

Measurement date ÷ 15.10.2006 16.05.2006 08.09.2006 01.12.2006 30.11.2006

Bleed Condenser 1.4 2.5 0.7

Moderator lines in purification building

18 36

Moderator pump 165 180

Moderator HX inlet 61 32

Moderator HX drain 284

SSS Tank -4 8 3 3.4 2.5

ALPAS Tank 6 3.4

Down stream of primarypressurising pump

26

FM Vault (S) lose 82 22

FM Vault (N) close 54 55

FM (S) outlet feeder 9.2 30

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2. Investigations on characterization and controlof 124Sb activity in PHT system, Rajesh Verma, Amit, Sanjay Kumar and Hemant Kumar,RAPS3&4, Internal report (2005)

3. Identification and estimation of radionuclidesresponsible for high radiation dose in the

PHT/Moderator pipe lines of NAPS#2,B.S.Tomar, T.P.Chaturvedi, S.K.Upadhyayand V.K.Manchanda, INS Annual Conference, Nov. 15-18, 2005, Mumbai.

IANCAS Bulletin 143 April 2008

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Roundup

The 66th

BRNS-IANCAS “National Workshop on Radiochemistry and

Applications of Radioisotopes” (NWRAR) was inaugurated by Prof.

Diwakar Shastri, President, Banasthali University on February 7, 2008

The workshop wasbeing jointly organized by the“Indian Associat ion ofNuclear Chemists and AlliedScientists” (IANCAS) andDepar tment of Physics,AIM&ACT, Banasthal iUniversity during 7-15 Feb.2008. Prof. Rekha Govil,Dean, AIM & ACT andConvener of the workshopwelcomed all the resource

persons from BARC, participants and students.

Dr. V.K. Manchanda, President, IANCAS andHead, Radiochemistry Division, BARC emphasizedthe need for energy in general and nuclear energy inparticular. The association celebrated its silverjubilee in January 2008 and has been playing animportant role in popularizing nuclear science ingeneral and discipline of radiochemistry inparticular. Shri S.K. Chande, Vice-chairman,Atomic Energy Regulatory Board (AERB)discussed about the Indian nuclear powerprogramme. He stressed that the safety standards ofnuclear industry worldwide as well as in India arevery high. He mentioned that whereas in the historyof nuclear industry, there have been only 2 majoraccidents when compared to many more in the sameperiod. However, the nuclear industry worldwidehas further enhanced the safety standards and the

regulatory aspects to ensure that this industry is safe.Shri Chande was very appreciative of the culturedeveloped in Banasthali in the staff as well as thestudents.

There were 5 special lectures delivered by ShriChande of AERB, Dr.Manchanda, Dr.MeeraVenkatesh, Shri Kanwar Raj and Shri B.K. Senrespectively on topics 1.Safety Standards in nuclearpower plants, 2. DAE activities at a glance, 3.Applications of Radioisotopes for the societalbenefit, 4. Nuclear waste management and 5.Production & Applications of Radioisotopes inIndustry.

Shri B.K. Sen, Head, Produuct DevelopmentDivision, BARC was the Chief Guest during thevaledictory function and handed over the equipmentto the host institute to encourage them to continue the work initiated by IANCAS in popularising thesubject of Nuclear Chemistry.

In addition to the main workshop there was alecture cum demonstration programme for thestudents of 11th, 12th and B.Sc./M/Sc in schools.

Dr.Veena Sagar and Dr.K.V.Lohitakshan arethe coordinators and Dr.P.K.Pujari, Shri K.Sudersan, Dr.Y.P. Naik, Smt. Sashikala Ojha,Dr.D.G.Phal from BARC and Shri Chandan Kumarfrom BRIT were the other resource persons.

April 2008 144 IANCAS Bulletin

Prof. RekhaGovil

IANCAS deeply regrets the sad demise of Prof. Rekha Govil, Ex- BARC, and also Coordinator of the recently held BRNS-IANCAS National Workshop at Banasthali on 10-09-2008