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Pfizer Asia Pacific Pte Ltd
Trigeneration Facility
At Pfizer
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Pfizer Asia Pacific Pte Ltd
Base Case (Pre Project) Steam / Power / Chilled Water Requirements
Configuration Of Trigeneration Plant
Overall Energy Efficiency Of Trigeneration Plant
Fuel And Electricity Savings
CO2 Emission Reduction
Challenges
Presentation Outline
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Pfizer Asia Pacific Pte Ltd
US$470 million Multi-purpose Active Pharmaceuticals Ingredient (API) manufacturing facility
Occupy 40 acres at Tuas Biomedical Park
24 hrs x 7 days operations with employment of ~260 people
Pfizer Asia Pacific Pte Ltd
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Pfizer Asia Pacific Pte Ltd
Site Aerial Plan
WWTP
SRU
INCINERATOR
Pfizer Global ManufacturingSingapore API plant
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Pfizer Asia Pacific Pte Ltd
Base case
Before Trigeneration, the average utilities usage of Pfizer facility :
Electricity ~ 6.5 MWSteam demand ~ 8T/hrChilled Water ~ 2500 RT/hr
Energy usage for Pfizer Singapore API facility is expecting to increase in near future due to higher production output & plant expansion
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Pfizer Asia Pacific Pte Ltd
Trigeneration Plant Configuration
Trigeneration ConceptSingle integrated system comprises of Gas Fired Turbine, Waste Heat Boiler & Absorption Chiller
Based on Pfizer’s energy demand profile, the Trigeneration plant design:
1 x 5.0 MW rated Gas Turbine Generator1 x 14 T/H rated Waste Heat BoilerTwo stage 1300RT rated Absorption Chiller
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Pfizer Asia Pacific Pte Ltd
Typical Energy Usage Profile
G
High PressureNatural Gas (20 bar)
8 T/h Steam(Process)
10-11°C6°C
Steam/Hot water Absorption
Chiller
P P
P P
1000 RT CWHeat RecoverySteam Generator
Cooling Tower
By pass Exhaust
4.6MW Electricity
11 T/hr, 8 bar Steam 3 T/h
Boiler Feed Water
Gas Turbine Generator
Trigeneration Plant Configuration
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Pfizer Asia Pacific Pte Ltd
100%100%
~15%
~52%
85% 45%
100%
15~20%
~3%
80~85%
Boiler Power Boiler & Power
CONVENTIONAL SYSTEM
TRIGENERATIO
N
Gas SupplierGas Supplier
System Efficiency System Efficiency
Fuel Input
Efficiency Losses
65%WeightedAverage
NGNG
ElectricityElectricity
NGNG
How Trigen Improves Energy Efficiency
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Pfizer Asia Pacific Pte Ltd
Fuel and Electricity Saving
Pfizer total energy cost (Electricity & Natural Gas) is reduced by ~US$587K/yr due to:
Better fuel utilization and improve plant energy efficiency (achieved ~ 83% efficiency with heat rate of 12.9 mmBtu/MW @ 4.6 MWh output )Reduce electricity consumption due to absorption chilling
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Pfizer Asia Pacific Pte Ltd
% 17
Ton/yr 5,976 Annual CO2 Reduction fromTrigeneration
T/mth2,434 Total CO2 Emission per month (Trigeneration)
T/mth389 CO2 Emission per month (Power Station)
kg/kWh0.45CO2 Emission (Average Power Station)
MW1.2
Power from the Power Station (less 0.7MW from Absorption Chiller)
Power from Power StationT/mth2,045
CO2 Emission per month (TriGeneration)
kg/kWh0.229CO2 EmissionMW12.4
TriGen Output (Electricity + Steam)
T/h11Steam generated from TrigenMW4.6Power generated
Trigeneration System
Other Benefits
T/Mth2,932 Total CO2 Emission per month (Conventional)
T/mth2106 CO2 Emission per month (Power Station)
kg/kWh0.45CO2 Emission (Average Power Station)
MW6.5Power from the Power Station Power from Power Station
T/mth826CO2 Emission per month (Boiler)
kg/kWh0.19CO2 EmissionmmBtu/mth15,120
NG Used (boiler @85% efficiency)
T/h8Steam OutputBar8Steam Pressure
Package Boiler
Conventional System
CO2 reduction estimated 6000 T/yr or 17%
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Pfizer Asia Pacific Pte Ltd
Challenges
Rigorous regulatory requirements by regulatory bodies e.g.
New power meters installationOnline metering data and status of breaker to EMA every 30 secContracted capacity subject to Capped or Summation scheme requirementNew interlock and inter-tripping requirement
Fully utilize all the heat energy to be cost effectiveExpertise to operate and maintain the system (partner with Tuas Power Ltd)Gas Supply Reliability
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Pfizer Asia Pacific Pte Ltd
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Pfizer Asia Pacific Pte Ltd
Thank You Welcome Welcome any any
comments comments and and
questionsquestions
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Pfizer Asia Pacific Pte Ltd
Energy Efficiency Estimation
-69,000mmBty/yrAdditional Steam capacity from Trigen = 3T
14%Energy efficiency improvement519,935602,465mmBtu/yrTotal Energy required per year499,320mmBtu/yrEnergy (NG) consumed by Trigeneration per Year
4.6MWElectricity generated by Trigen
Energy from Trigeneration184,000mmBtu/yrEnergy consumed by Steam Boiler per Year
85%%Boiler Efficiency118Ton/hrSteam generation
Energy Required At Existing Boiler89,615418,465mmBtu/yrEnergy (NG) consumed by Power Station per Year
2.6714.44MWEnergy consumed by Power Station Generation45%45%%Average Grid Power Generation Efficiency 1.26.5MWElectricity Demand from Grid
Energy Required At Power Station
With
Trigeneration
Conventional
SystemUNITSBASE CASE