45
TO: Via: E-Mail Transmission Mr. Jim Stapp, PAR Electric Mr. Travis Walser, PAR Electric Mr. Chris Larson, PAR Electric Mr. Lon Peterson, PAR Electric Mr. Steve D. Brown, PAR Electric Mr. Jeremy Atchison, PAR Electric Mr. Mike Olds, PAR Electric Mr. Kenny Bruce, PAR Electric Mrs. Mindie McIff, Sturgeon Electric Mr. Richard Reyes, Sturgeon Electric Co. Mr. Raul Guardado, Sturgeon Electric Co. Mr. Steve Cavanaugh, Sturgeon Electric Co. Mr. AJ Zartman, Diversified Mr. Hal Lindsey, Diversified Mr. Tim McBride, Southern Contracting Mr. Pat Baker, Southern Contracting Mr. Troy Meyers, Hotline Construction Mr. Jim Coleman, Hotline Construction Mr. Tom Hutchinson, Kathy’s Lift Truck Mr. Robert Pacheco, Pacheco Utility L/B Mr. Henry Escajeda, EE Electric Mr. Michael Escajeda, EE Electric Mr. Landon Kluck, Michels Power Mr. James Coleman, Pinnacle Power Mr. Aaron Boone, Pinnacle Power Mr. Shawn Spencer, Mountain Power Mr. Justin Greene, Mountain Power Mr. Don Weyhrauch, Edison Power Const Mr. Matt Tedder, HTE, Inc. Mr. Steve Hernandez, HTE, Inc. Mr. Jack Crabbs, Outsource Mr. Henry Daye, Petrelli Electric Mr. Leo Jordan, Faith Electric Mr. Mike Alkhoutoff, Faith Electric Mr. Mark Anders, Petrelli Electric Mr. Ward Andrews, Wilson Construction Mr. William Simmons, City Light & Pwr Mr. Lee Brown, ILB Mr. Dan Haggard, ILB Mr. Aaron Johnson, ILB Mr. Bruce Costa, Contra Costa Mr. Mike Ortiz, Hi-Voltage Splicing Co. Mr. Tom Arnold, Professional Safety S Mr. Johnny Lanning, New River Electrical Mr. Rob Grace, Grace Construction Mr. Greg Kludjian, Asplundh Mr. Chris Dichard, Asplundh Mr. Boyd Trove, TTR Substations, Inc. Mr. John Olsen, Intern Mr. Jason Combs, Intern Mr. Mike Levine, Black & Veatch Mr. Ron Cochran, Black & Veatch Mr. Jared Johnson, MGE Mr. Ryan Smith, MGE Mr. Matt Cruzat, MGE Mr. Jon Cloud, J. Cloud, Inc. Mr. Marty Roper, Weissker Mr. Ed Campbell, Henkels & McCoy Mr. Daniel Ashmore, Henkels & McCoy Mr. Chad Overacker, Henkels & McCoy Mr. Mike Croker, Henkels & McCoy Mr. Jim McAdams, Cupertino Electric Mr. Mike Hernandez, IBEW Local 47 Mr. Steve Roberts, IBEW Local 47 Mr. Rod Peterson, IBEW Local 47 Mr. Liz McInnis, IBEW Local 1245 Mr. Ralph Armstrong, IBEW Local 1245 Mr. Michael Saner, IBEW Local 1245 Mr. Charlie Randall, IBEW 9 th District Mr. Armando Mendez, Cal-Nevada JATC Mr. Charlie Jefferson, Cal-Nevada JATC Mr. Randy Tomlin, Cal-Nevada JATC

TO: Via: E-Mail Transmission...TO: Via: E-Mail Transmission Mr. Jim Stapp, PAR Electric Mr. Travis Walser, PAR Electric Mr. Chris Larson, PAR Electric Mr. Lon Peterson, PAR

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Page 1: TO: Via: E-Mail Transmission...TO: Via: E-Mail Transmission Mr. Jim Stapp, PAR Electric Mr. Travis Walser, PAR Electric Mr. Chris Larson, PAR Electric Mr. Lon Peterson, PAR

TO:

Via: E-Mail Transmission

Mr. Jim Stapp, PAR Electric Mr. Travis Walser, PAR Electric Mr. Chris Larson, PAR Electric Mr. Lon Peterson, PAR Electric Mr. Steve D. Brown, PAR Electric Mr. Jeremy Atchison, PAR Electric Mr. Mike Olds, PAR Electric Mr. Kenny Bruce, PAR Electric Mrs. Mindie McIff, Sturgeon Electric Mr. Richard Reyes, Sturgeon Electric Co. Mr. Raul Guardado, Sturgeon Electric Co. Mr. Steve Cavanaugh, Sturgeon Electric Co. Mr. AJ Zartman, Diversified Mr. Hal Lindsey, Diversified Mr. Tim McBride, Southern Contracting Mr. Pat Baker, Southern Contracting Mr. Troy Meyers, Hotline Construction Mr. Jim Coleman, Hotline Construction Mr. Tom Hutchinson, Kathy’s Lift Truck Mr. Robert Pacheco, Pacheco Utility L/B Mr. Henry Escajeda, EE Electric Mr. Michael Escajeda, EE Electric Mr. Landon Kluck, Michels Power Mr. James Coleman, Pinnacle Power Mr. Aaron Boone, Pinnacle Power Mr. Shawn Spencer, Mountain Power Mr. Justin Greene, Mountain Power Mr. Don Weyhrauch, Edison Power Const Mr. Matt Tedder, HTE, Inc. Mr. Steve Hernandez, HTE, Inc. Mr. Jack Crabbs, Outsource Mr. Henry Daye, Petrelli Electric Mr. Leo Jordan, Faith Electric Mr. Mike Alkhoutoff, Faith Electric Mr. Mark Anders, Petrelli Electric

Mr. Ward Andrews, Wilson Construction Mr. William Simmons, City Light & Pwr Mr. Lee Brown, ILB Mr. Dan Haggard, ILB Mr. Aaron Johnson, ILB Mr. Bruce Costa, Contra Costa Mr. Mike Ortiz, Hi-Voltage Splicing Co. Mr. Tom Arnold, Professional Safety S Mr. Johnny Lanning, New River Electrical Mr. Rob Grace, Grace Construction Mr. Greg Kludjian, Asplundh Mr. Chris Dichard, Asplundh Mr. Boyd Trove, TTR Substations, Inc. Mr. John Olsen, Intern Mr. Jason Combs, Intern Mr. Mike Levine, Black & Veatch Mr. Ron Cochran, Black & Veatch Mr. Jared Johnson, MGE Mr. Ryan Smith, MGE Mr. Matt Cruzat, MGE Mr. Jon Cloud, J. Cloud, Inc. Mr. Marty Roper, Weissker Mr. Ed Campbell, Henkels & McCoy Mr. Daniel Ashmore, Henkels & McCoy Mr. Chad Overacker, Henkels & McCoy Mr. Mike Croker, Henkels & McCoy Mr. Jim McAdams, Cupertino Electric Mr. Mike Hernandez, IBEW Local 47 Mr. Steve Roberts, IBEW Local 47 Mr. Rod Peterson, IBEW Local 47 Mr. Liz McInnis, IBEW Local 1245 Mr. Ralph Armstrong, IBEW Local 1245 Mr. Michael Saner, IBEW Local 1245 Mr. Charlie Randall, IBEW 9th District Mr. Armando Mendez, Cal-Nevada JATC Mr. Charlie Jefferson, Cal-Nevada JATC Mr. Randy Tomlin, Cal-Nevada JATC

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DATE

12/03/2015 RE:

Notice of Joint Safety Committee Meetings - 2015

E-MAIL: [email protected]

This is a reminder notice that the next, California Joint Safety Committee Meeting has been set for Tuesday, December 8, 2015 at 1:00pm in the North Classroom. The Meeting will be held at our Cal-Nevada JATC – Riverside Training Center, located at 9846 Limonite Ave., Riverside, California. The Meeting Minutes from our last safety meeting held on September 15, 2015 are attached. Please review the Minutes and let me know if you have other Accidents/Incidents to report that are not included in the attached Report or if you have any other edits to the Minutes. Thanks, Jules W. Weaver Chapter Manager

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MEETING MINUTES IBEW 47-1245 / WLCC-NECA JOINT SAFETY COMMITTEE

September 15, 2015 At IBEW Local 1245’s Hall Located in Vacaville, California

Present: Mgmt:

Jim Stapp AJ Zartman Hal Lindsey Ron Cochran Jason Combs Dan Haggard Aaron Johnson Steve Brown Jeremy Atchison Gregg Kludjian Jim McAdams Mike Olds Mark Anders Chris Dichard Chad Overacker Mike Crocker Lon Peterson Kenny Bruce Chris Hess Ryan Smith Matt Cruzat Jules Weaver

IBEW: Ralph Armstrong Steve Roberts Richard Ingle Rod Peterson Mike Cottrell Michael Saner

Cal-NEV JATC:

Charlie Jefferson Randy Tomlin

Meeting called to order by Chairman Armstrong at 10:25am. Chairman Armstrong welcomed the group and had everyone introduce themselves.

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Previous Minutes: M/S/C to approve the Meeting Minutes of the Joint Safety Committee Meeting held on June 23, 2015. Review of Accidents & Incidents: The updated Accident & Incident Report is attached hereto as Exhibit A. Local 1245 -Northern California: as reported by Chairman Armstrong: Chairman Armstrong discussed a hip injury that occurred on a contract crew in a substation and a PG&E lineman that received 2nd degree burns from a flash. Nothing else to report beyond the accidents or incidents that the Contractor’s will report on today and those incidents set forth in the Accident & Incident Report attached hereto as Exhibit A. Local 47 -Southern California: as reported by Steve Roberts: Mr. Roberts noted he didn’t have any accidents or incidents to report beyond what the Contractor’s will report on today and those incidents set forth in the Accident & Incident Report attached hereto as Exhibit A. Contractor’s Reports: The following Contractors noted they had no accidents or incidents to report and discuss. Cupertino Electric

MGE Underground, Inc.

The other Contractor’s present, reported on the accidents and incidents set forth in the attached Exhibit A that occurred during the 4th quarter of 2014 and up to December 2015. A couple of specific topics came out of the Contractors reports and discussions as follows:

1.   One of the biggest concerns that came out of the discussion is the lack of Testing. The employees must take the time to Test and if need be wait for the appropriate tools to do so. It was also noted that in almost all of our serious accidents the proper testing tools were available on the job site for the employees to utilize.

2.   Quality control issues were also discussed. Mr. Rod Peterson noted that many times the employee is laid off when in fact they should be terminated and with a layoff there is no opportunity for a real consequence. A general discussion followed.

3.   Also discussed is the importance of the Foreman role and our new Foreman training

program.

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JATC Reports: Mr. Tomlin discussed a couple of minor injuries that took place during climbing class. A discussion was held and it was noted that the accidents and incidents reports set forth in (Exhibit A) would be shared with the Apprentices and should be a very helpful learning tool for the Apprenticeship. Old Business:

1.   A discussion was held regarding dates to hold a Train-the-Trainer class for our IBEW-NECA Basic Helicopter Training for Power Line Work approved course. Given the schedule of our helicopter experts it was noted that we will be looking at dates around the end of this year or in the first 2 months of 2016.

2.   Secretary Weaver gave an update on the Electrical Industry Certifications Association [EICA] and that we are in the process of obtaining ANSI accreditation for our own Industry Crane Certification/Training Program and noted that we are process of pilot testing the practical exam.

3.   Chairman Armstrong discussed the updates to the Red Safety Book that will need to be made as a result of Federal OSHA’s updated Final Rule 29 CFR 1910.269 & 29 CFR 1926, Subpart V and California OSHA’s response and possible additions to this rule. Mr. Armstrong noted that Cal-OSHA should publish their final rules sometime in the first quarter of 2016. A general discussion followed and it was noted that the Red Book Subcommittee would convene to review Cal-OSHA’s Final Rule and update the Red Book accordingly. The Chairman and Secretary noted that Red Book Subcommittee is composed of the following 8 individuals from Labor and Management:

Labor Management Ralph Armstrong Ward Andrews Richard Lane Hal Lindsey Rod Peterson Chris Larson Steve Roberts Hank Rivera

New Business:

1.   A discussion was held regarding our utility customers adopting and implementing Federal OSHA’s updated Final Rule 29 CFR 1910.269 & 29 CFR 1926, Subpart V, prior to Cal-OSHA’s release of their updates. A general discussion followed.

2.   Secretary Weaver discussed the D-10 Safety Database and it was noted that we have 22,478 Student/Employee’s in the system and 178,633 separate training records/classes associated with those employees. Secretary Weaver will be giving a more in depth presentation of the database at the December 2015 Safety Committee Meeting.

3.   Mr. Cochran discussed the requirements set forth in Federal OSHA’s updated Final Rule 29 CFR 1910.269 & 29 CFR 1926, Subpart V for FR Clothing and a potential industry consortium. A general discussion followed.

M/S/C to adjourn made at 12:05 pm. Next Qrt Meeting: December 8, 2015 in Riverside at 1:00pm.

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12/3/15 Page  1

Date  Of  Incident Occupation Type  of  Incident

Body  Part  /  Root  Cause Description

9/17/14 Outside  Lineman Significant  Injury FractureSignificant  Injury  -­‐  9-­‐17-­‐2014,  A  lineman  sustained  serious  injuries  after  falling  from  a  bucket  that  was  at  cradle  height.  He  was  immediately  transported  to  Harbor-­‐UCLA  Medical  Center  where  he  remained  for  treatment  and  observation.

9/24/14 UG  Laborer Significant  Injury Fracture

Significant  Injury  -­‐  On  9-­‐24-­‐2014,  Two  UG  Laborers  were  injured  in  a  fall-­‐related  incident  while  working  on  a  vault  replacement  job  on  the  Jennings  12kV  in  Long  Beach  while  two  workers  were  inside  the  vault  assisting  a  saw  operator  in  preparation  for  cutting  a  vault  wall.  At  the  time  of  the  incident,  a  worker  was  ascending  a  ladder  to  exit  the  vault  while  the  other  worker  was  at  the  bottom.  As  the  worker  neared  the  top  of  the  ladder,  the  ladder  failed  causing  him  to  fall  and  land  on  top  of  the  second  worker.    The  crew  foreman  entered  the  vault  to  assess  the  situation,  saw  that  the  two  employees  were  in  need  of  medical  attention,  and  called  911.Both  employees  were  stabilized  inside  the  vault  by  medical  responders.  They  were  hoisted  out  of  the  vault  and  transported  to  a  nearby  hospital  for  evaluation  and  treatment.  As  a  result  of  the  incident,  one  employee  suffered  orthopedic  injuries.  

10/8/14 UG  Foreman Significant  Injury Fracture

Significant  Injury  –  October  8  2014,  A  crew  foreman  was  on  a  ladder  adjusting  the  vault  shoring.  Due  to  the  depth  of  the  excavation,  the  shoring  required  two  6-­‐inch  shields  stacked  on  top  of  each  other.  End  wall  plates  were  installed  at  each  end  to  prevent  the  soil  from  caving  in.  While  the  worker  was  installing  the  locking  pin  to  secure  the  connecting  pin  on  the  end  walls,  the  soil  shifted  behind  the  end  wall.  This  caused  the  employee’s  arm  to  become  pinched  between  the  end  wall  plate  and  shield  wall.  The  employee  pulled  out  his  arm  and  exited  the  vault.  He  was  taken  to  the  nearby  hospital  with  a  fractured  arm.  

10/9/15 Outside  Lineman Significant  Injury Crushing

Significant  Injury  -­‐  October  9,  2015  -­‐  Thousand  Oaks  -­‐    A  contractor  crew  was  trying  to  pick  up  a  pole  that  was  buried  in  the  55  to  60  foot  pole  pile.  They  had  moved  about  six  poles  already.  They  picked  up  the  next  pole  with  the  pole  tongs  and  put  a  cross  arm  under  it  to  re-­‐pick  it  on  balance.  A  lineman  told  an  apprentice  lineman  on  the  crew  to  get  off  the  pole  pile  because  he  did  not  want  him  standing  in  the  bite.  While  lowering  the  pole,  it  came  out  of  the    pole  tongs  while  it  was  about  1  foot  above  the  pile.    As  it  fell,  the  butt  shifted  pushing  the  head  toward  the  lineman,  smashing  his  left  foot.    The  crew  immediately  stopped  work.  The  foreman  removed  the  lineman's  boot  at  his  request.  He  then    made  all  the  appropriate  phone  calls  to  get  medical  help.  The  lineman  received  treatment  for  two  broken  toes.  The  crew  also  changed  the  method  of  lifting  the  poles.  The  contractor  will  now  be  using  steel  slings  to  move  poles.                

IBEW  47  -­‐  1245  /  WLCC  -­‐  NECA2014  4th  Qtr  &  2015  Accident/Incident  Reports

Contractor  Significant  Accidents

Exhibit A

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/5/14 IOU-­‐E  Lineman Significant  Injury BurnSignificant  Injury  -­‐  11-­‐5-­‐2014,  Primary  flash  occurred  and  burns  suffered  when  linemen  removed  an  energized  12kV  elbow  without  testing  or  grounding    EMS  called  and  employee  transported  to  hospital  for  treatment  for  burn  injuries

11/16/14IOU-­‐E  Lineman  /  Hot  Apprentice Significant  Injury Burn

Significant  Injury  -­‐  11-­‐16-­‐2014,  Two  workers  were  involved  in  an  electrical  flash  incident  while  working  inside  an  underground  structure  in  the  City  of  La  Puente.  Preliminary  information  indicates  that  a  journeyman-­‐lineman  and  hot  apprentice,  installed  600-­‐amp  components  onto  a  gas  switch  on  the  Coupler  12kV  circuit,  and  were  in  the  process  of  removing  a  200-­‐amp  elbow  on  an  adjacent  position  when  a  flash  occurred  resulting  in  burns  injuries.

12/5/14 UG  Laborer Significant  Injury Burns

Significant  Injury  -­‐  CCCI,  On  December  5  2014,  Two  workers  were  seriously  injured  in  an  electrical  flash  while  the  employees  were  chipping  concrete  away  from  duct  bank  during  work  to  replace  a  vault  on  the  Ringo  12kV  circuit  located  in  Irvine.    Initial  reports  indicate  both  employees  suffered  burn  injuries  when  they  punctured  primary  cable  with  a  jackhammer  resulting  in  an  electrical  flash  and  a  circuit  lockout.

12/16/14 Outside  Crew Significant  Injury Burns

Significant  Injury  -­‐  CCCI  –  On  December  16  2014,  Transmission  linemen  sustained  flash  burn  injuries  resulting  from  an  electrical  flash  incident  that  occurred  in  Ontario.  Preliminary  information  indicates  that  while  the  workers  were  in  the  process  of  removing  an  idle  section  of  the  Mira  Loma-­‐Archibald  66kV  line,  a  conductor  dropped  onto  the  Novac  12kV  underbuild,  causing  an  electrical  flash  and  the  line  to  relay.

1/7/15 IOU-­‐E  Lineman Significant  Injury FractureSignificant  injury  -­‐  On  January  7,  a  SCE  Worker  was  off-­‐loading  an  underground  oil  switch  when  the  load  shifted  hitting  his  leg  and  knocking  him  off  the  trailer  resulting  in  a  broken  leg  and  head  injuries  

1/23/15 Outside  Lineman Significant  Injury Burn

Significant  Injury  -­‐  CCCI  -­‐  On  January  23,  A  lineman  was  working  on  a  crew  tasked  with  removing  underground  conductors  and  equipment  in  preparation  for  a  vault  replacement.  Reportedly,  after  testing  the  cable  as  de-­‐energized,  the  lineman  proceeded  to  cut  the  cable  with  a  pair  of  ratchet  cutters  when  the  electrical  flash  occurred.  

2/2/15Sub-­‐Contract  Employee Significant  Injury Crushing

Significant  Injury  -­‐  On  February  2,  Preliminary  information  indicates  a  crane  operator  was  attempting  to  move  a  20,000  pound  cable  reel  onto  a  flatbed  truck  when  the  load  collided  with  an  adjacent  cable  reel.  This  reel  was  dislodged  from  its  cribbing  and  pinned  the  driver  of  the  flatbed  truck,  who  was  positioned  between  two  of  the  adjacent  reels.  Injuries  include  fracture  of  skull,  spine,  ribs,  and  hand.

2/3/15 Outside  Lineman Significant  Injury Broken  Arm

Significant  Injury  -­‐  On  February  3,  Preliminary  information  indicates  that  while  crew  was  loading  a  pole,  they  determined  the  pole  needed  to  be  turned  the  other  direction  in  order  to  set  it  properly  on  the  trailer.  As  the  lineman  began  moving  the  pole  into  the  desired  position,  his  left  arm  became  caught  between  the  pole  he  was  handling  and  a  stationary  pole  holding  the  pole  pile  together.  He  was  immediately  transported  to  Methodist  Hospital  in  Arcadia  and  is  being  treated  by  an  orthopedic  surgeon.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

2/18/15 UG  Laborer Significant  Injury Fracture

Significant  Injury  -­‐  On  Feb.  18,  a  worker  from  a  Sub  Contractor,  to  a  Contract  Crew,  was  seriously  injured  while  working  on  a  pole  replacement  project  on  the  Brookhill  4kV  circuit  in  Glendale,  CA.  Preliminary  information  indicates  the  injured  worker  was  on  a  digging  crew,  unloading  bags  of  gravel  from  trucks.  The  crew  typically  works  alongside  a  line  crew  to  dig  pole  holes.  In  the  vicinity,  the  line  crew  had  a  pole  on  a  stand  ready  for  framing,  with  the  head  of  the  pole  elevated  approximately  three  feet  above  the  ground.  The  pole  fell  and  struck  the  SoCal  Utility  worker  on  the  left  leg  and  foot.  He  was  immediately  taken  to  a  nearby  hospital  for  treatment  with  undetermined  injuries.

2/23/15 Outside  Lineman Significant  Injury Electrical  Contact

Significant  Injury  -­‐  On  Feb.  23,  a  lineman  from  a  Contract  Crew  was  involved  in  an  electrical  contact  event  that  took  place  on  the  Blimp  16kV  circuit  in  Carson,  CA.  The  lineman  was  working  on  a  crew  that  was  replacing  a  broken  cross  arm  on  a  section  of  the  circuit  they  had  de-­‐energized,  prior  to  the  replacement.  Once  the  line  was  re-­‐energized,  the  lineman  was  repositioning  himself  on  the  pole  before  continuing  his  work,  when  the  contact  occurred  and  he  sustained  injuries.  After  contact,  the  lineman  descended  the  pole  on  his  own,  was  transported  to  Harbor-­‐UCLA  Medical  Center  and  was  later  transferred  to  USC  Medical  Center  for  observation.  He  was  released  from  the  hospital  on  Feb.  25,  after  treatment  of  his  injuries.

3/2/15 Outside  Lineman Significant  Injury Head

Significant  Injury  -­‐  On  Monday,  March  2,  a  distribution  lineman  sustained  a  head  injury  after  falling  off  a  double  bucket  truck.  The  lineman  was  working  on  a  pole  replacement  on  the  Kuehner  16kV  line  in  Simi  Valley  as  part  of  a  five-­‐man  crew.  The  crew  had  just  completed  transferring  secondary's  onto  a  new  pole.  Preliminary  information  indicates  the  lineman  had  stepped  out  of  the  bucket  and  was  descending  from  the  bed  of  the  truck  when  he  fell  and  hit  his  head.  He  was  taken  to  a  local  hospital.  We  have  no  further  details  about  the  lineman’s  condition  at  this  time;  however,  the  contractor  has  initiated  their  investigation  process  to  determine  the  precise  cause  of  the  fall.

3/12/15 Outside  Crew Significant  Injury Knee  Injury

Significant  Injury  -­‐  on    March  12,  2015  -­‐  Work  was  being  performed  in  the  Napa  area  when  an  employee  stepped  into  a  hole  injuring  his  knee.    On  4/29/2015  the  EE  indicated  the  injury  was  not  better  and  requested  medical  attention.    The  employee  was  taken  to  the  nearest  clinic  where  he  was  given  a  prescription  for  pain  and  instructed  to  see  an  Orthopedic  Surgeon.    It  was  determined  the  issuance  of  the  medication  would  make  the  injure  OSHA  recordable.    Work  was  being  performed  on  a  hillside  with  uneven  terrain  covered  in  tall  grass.    The  crew  was  not  able  to  identify  the  holes  in  the  ground  due  to  the  covering  vegetation.    The  effected  employee  contacted  his  supervisor  and  noted  the  possible  injury  a  decision  was  made  to  apply  ice  to  the  knee  at  home  and  monitor  the  situation.    That  evening  the  knee  began  to  swell  and  the  pain  level  elevated.    The  next  day  the  employee  returned  to  work  and  reported  the  continued  discomfort  to  his  supervisor.    Base  was  called  and  the  safety  department  contacted  our  Insight  Health  representative.    The  EE  was  directed  to  continue  ice  application  and  monitor  the  injury.    Immediately  report  all  incidents  to  base.    Be  sure  to  identify  a  safe  path  of  travel  when  working  on  uneven  terrain  and  discuss  slip,  trip  and  fall  hazards  prior  to  the  commencement  of  work  activates.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

3/29/15 Outside  Crew Significant  Injury Fatal  Burns

Significant  Injury  –  FATALITY  on  March  29  2015,  Two  Outside  Journeyman  linemen  were  seriously  injured  in  an  electrical  flash  as  they  were  finishing  a  planned  outage  on  the  Cylinder  16kV  in  Hermosa  Beach  (South  Bay  District).  The  job  scope  entailed  decommissioning  a  subsurface  operating  enclosure  (a  type  of  vault),  housing  a  switch  and  a  transformer.  After  accounting  for  conditions  found  in  the  field,  it  was  decided  that  both  the  switch  and  the  transformer  were  to  be  relocated  and  installed  in  separate  but  adjacent  fiberglass  BURD  enclosures.  The  transformer  would  also  be  replaced  with  a  new  one.  In  preparation  for  this  work,  the  crew  de-­‐energized  and  disconnected  the  cables  running  from  an  adjacent  manhole  to  the  switch,  which  in  turn  de-­‐energized  the  transformer.  Once  the  new  configuration  was  complete,  the  crew  initiated  re-­‐energizing  the  equipment.  Preliminary  information  indicates  that  while  two  linemen  were  in  the  process  of  reconnecting  the  cables  back  onto  the  main  line,  an  electrical  flash  occurred.    The  linemen  sustained  serious  burn  injuries  and  were  immediately  transported  to  Little  Company  of  Mary  Hospital  and  later  transferred  to  Torrance  Memorial  Medical  Center.  A  third  crew  member  suffered  minor  burn  injuries  to  his  hands  while  responding  to  the  linemen  as  they  exited  the  manhole.  

4/14/15 Outside  Crew Significant  Injury Burns

Significant  Injuries  on  4-­‐14-­‐2015  -­‐  Two  workers  were  seriously  injured  on  Tuesday,  April  14,  while  performing  work  around  a  concrete  Buried  Underground  Residential  Distribution  (BURD)  structure  on  the  Bauxite  16kV  in  Rancho  Palos  Verdes  (South  Bay  District).  The  crew  was  tasked  with  replacing  cable  that  fed  into  the  structure.  While  the  injuries  are  under  investigation,  preliminary  information  indicates  a  foreman  and  a  lineman  were  confirming  the  status  of  the  line  when  a  flash  occurred.  Both  workers  sustained  undetermined  burn  injuries  and  were  immediately  transported  to  Torrance  Memorial  Medical  Center,  where  they  are  undergoing  evaluation  and  treatment.

5/31/15 Outside  Crew Significant  Injury Laceration Significant  Injury  -­‐  on  May  31,  2015  -­‐  Whittier  -­‐  Employee  climbing  pole,  gaffed  out,  resulting  in  cut  to  inside  of  right  ankle.  Examined  at  clinic,  placed  on  TTD.

5/26/15 Outside  Crew Significant  Injury Fracture

Significant  Injury  -­‐  on    May  26  2015  -­‐A  Contract  Operator  on  the  CHUG  project  sustained  a  broken  ankle  in  an  incident  as  follows;  The  water  truck  driver  had  returned  to  the  Baker  tank,  on  his  ninth  trip  of  the  day,  to  fill  his  tank.  He  safely  exited  his  truck,  connected  the  3”  discharge  hose  to  his  tank,  filled  his  tank,  disconnected  the  discharge  hose  from  his  tank  and  was  in  the  process  of  straightening  the  discharge  hose  to  store  it  within  the  baker  tank’s  secondary  containment  system.  While  completing  this  task,  the  truck  driver’s  left  foot  began  to  slip  in  the  mud  that  had  developed  during  his  previous  filling  operations.  At  the  same  time,  the  truck  driver’s  right  foot  stayed  stuck  in  its  position  in  the  mud.  Losing  balance,  the  truck  driver  fell  to  the  ground.    This  action  caused  an  abnormal  twisting  motion  in  his  right  ankle.    

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

5/30/15 Outside  Crew Significant  Injury Fracture

Significant  Injury  5-­‐30-­‐2015  -­‐  A  contractor  crew  consisting  of  an  E-­‐Crew  foreman,  two    linemen  and  one  groundman  was  tasked  with  replacing  a      deteriorated  pole  on  the  Ridgegrove  12kV  circuit  in  the  San  Joaquin  region.  The  crew  was  unloading  the  new  pole  from  the  companion  vehicle  truck  pole  rack  using  a  pair  of  pole  tongs  attached  to  the  winch  line  of  the  line  truck.  The  pole  was  accidentally  lowered  into  the  rack  on  the  companion  vehicle,  causing  the  tongs  to  release  the  pole.  This  knocked  the    groundman  down.  The  pole  fell  down  on  top  of  both  the    groundman’s  legs,  fracturing  his  right  ankle  and  injuring  his  left  knee.                                                                                                      

6/4/15 Groundman Significant  Injury Crushing

Significant  Injury  6/4/2015  -­‐  Crew  was  using  a  line  truck  to  off-­‐load  poles  from  a  Flatbed  truck  into  a  Dumpster.    The  operator  has  trouble  laying  the  pole  flat  in  the  dumpster.    A  groundman  entered  it  in  to  move  the  pole  by  pushing  and  pulling  on  it.    Co-­‐workers  yelled  at  the  GSM  to  get  in  the  clear  but  he  continued.    His  hand  was  crushed  between  the  dumpster  and  the  pole  butt  when  it  suddenly  shifted.

6/8/15 Outside  Crew Significant  Injury LacerationSignificant  Injury  -­‐  on  June  8,  2015  -­‐  Palmdale  -­‐  Employee  loading  bucket  of  bolts,  placed  hand  between  another  bucket  and  metal  tabs  from  lid  punctured/cut  his  palm,  thumb  area.  8  stitches  required  to  close  wound.

6/10/15 Outside  Crew Significant  Injury Induction Significant  Injury  -­‐  on  June  10,  2015  -­‐  Santee  -­‐  Working  on  de-­‐energized  tx  line,  cutting  open  jumper  and  appears  broke  EPZ.  Suffered  induction  voltage  injuries  to  left  hand,  hip  and  flank  area.

6/10/15 Outside  Crew Significant  Injury Laceration Significant  Injury  -­‐  on  June  10,  2015  -­‐  Del  Mar  -­‐  Employee  behind  transformer  skinning  wire,  right  hand  slipped  causing  knife  to  cut  left  palm.  Stitches  needed  to  close  wound.

6/12/15 Outside  Crew Significant  Injury LacerationSignificant  Injury  -­‐  on  June  12,  2015  -­‐  Diamond  Bar  -­‐  Reaching  for  cordless  drill  in  truck  bin,  as  employee  grabbed  it,  triggered  on  and  caught  left  middle  finger  resulting  in  a  laceration.  Stitches  required  to  close  wound  and  returned  to  full  duty.

6/23/15 Outside  Crew Significant  Injury Head

Significant  Injury  June  23,  2015  –  A  contract  crew  in  the  Redlands  District  was  assigned  to  continue  work  on  the  Preston  12kV  Line  Extension  Project.  The  crew  held  a  tailboard,  discussed  the  hazards  and  mitigation  steps,  and  then  set  up  traffic  control  to  protect  the  crew  and  the  public.  The  crew  started  removing  1/0  underground  cable  from  a  pad  mount  transformer.  The  approach  was  to  rig  one  end  of  the  cable  to  a  truck,  put  the  truck  in  drive,  and  pull  out  the  cable  from  the  transformer.  When  the  cable  was  completely  removed,  the  loose  end  of  the  cable  slid  across  the  ground  and  rolled  over  to  the  side  of  the  road  where  a  crew  member  was  standing.  The  cable  struck  the  employee’s  feet,  causing  him  to  trip  and  hit  his  head  on  the  ground.  The  other  crew  members  administered  basic  first  aid  and  called  911.  The  employee  was  transported  to  the  nearest  hospital  where  he  currently  remains.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

6/24/15 UG  Crew Significant  Injury Burn

Significant  Injury  June  24,  2015  –  A  contract  worker  was  injured  in  a  primary  electrical  flash  event.  The  employee  was  part  of  an  underground  civil  crew  working  on  the  Bryce  16kV  in  the  City  of  El  Monte.  Preliminary  information  indicates  the  worker  was  chipping  an  encased  energized  duct  bank  when  the  pneumatic  chipping  tool  punctured  the  conduit  and  contacted  the  primary  cable  inside,  resulting  in  a  flash.    The  worker  was  transported  from  the  scene  to  Los  Angeles  County+USC  Medical  Center  with  reported  burn  injuries  to  his  face,  neck,  wrists  and  ears.  He  was  kept  in  the  hospital  overnight  for  observation  and  may  be  released  later  today.

6/26/15 Outside  Crew Significant  Injury Head

Significant  Injury  June  26,  2015  –  One  of  the  contract  crew  members  was  injured  when  a  piece  of  equipment  became  dislodged  from  an  ascending  double  bucket,  fell,  and  struck  him  on  the  head.  The  worker  struck  by  the  dislodged  equipment  was  knocked  unconscious  and  was  subsequently  taken  to  the  local  hospital.  Preliminary  information  indicates  the  injured  worker  received  care  for  a  head  wound  and  underwent  several  tests  as  part  of  a  medical  evaluation.  He  was  released  from  the  hospital  Monday  afternoon.

6/26/15 Outside  Crew Significant  Injury Cut

Significant  Injury  June  26,  2015  –  A  contract  crew  was  working  on  a  deteriorated  pole  replacement  project.  The  crew  foreman  was  cutting  a  deteriorated  pole  butt  with  a  chainsaw.  Preliminary  information  indicates  the  momentum  of  the  chainsaw  threw  off  the  handling  and  propelled  the  saw  backward,  cutting  the  foreman's  left  foot.  The  injured  worker  was  taken  to  the  hospital  where  he  received  stitches  and  was  released  back  to  work  the  same  day.  

7/8/15 Outside  Crew Significant  Injury Crushing

Significant  Injury  -­‐  July  28,  2015  -­‐  PG&E  -­‐  An  employee  was  driving  ground  rods  for  a  newly  installed  power  pole.    After  he  had  driven  the  first  ground  rod,  he  removed  his  gloves  to  make  a  connection  with  the  clamp.    After  the  connection  was  made,  he  proceeded  to  drive  the  second  ground  rod  without  putting  his  gloves  back  on  from  the  previous  task.    As  he  was  using  the  manual  ground  rod  pounder,  he  over  extended  and  accidentally  brought  the  driver  off  the  ground  rod  and  smashed  his  hand  between  the  top  of  the  ground  rod  and  the  handle  of  the  ground  rod  pounder.    This  resulted  in  an  injury  where  a  gash  was  torn  on  the  side  of  his  right  hand  requiring  stiches.

7/22/16 Outside  Lineman Significant  Injury Burns

Significant  Injury  July  22,  2015  –  A  lineman  sustained  burns  to  his  forearm  and  the  side  of  his  head  while  working  in  a  subsurface  structure  in  Palm  Springs.  Preliminary  information  indicates  that  the  lineman  was  in  a  vault  when  a  flash  occurred  and  the  Spa12  kV  circuit  relayed  with  No  Test  Orders  in  effect.  The  worker  exited  the  vault  and  medical  services  arrived  on  scene.  He  was  subsequently  transported  to  the  hospital  where  his  injuries  were  assessed  by  medical  personnel,  and  he  has  since  been  released.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

7/29/15 Contract  Worker Significant  Injury Shoulder  Injury

Significant  Injury  July  29,  2015  –  A  Contract  worker  was  seriously  injured  after  falling  from  a  ladder  while  staging  cable  reels  at  the  TRTP  Mira  Loma  Material  Yard.    The  work  was  standing  on  an  extension  ladder,  placing  bird  netting  over  a  cable  reel,  when  he  lost  his  balance  and  fell  approximately  5  feet,  injuring  his  right  shoulder.    Preliminary  information  indicates  his  foot  became  tangled  in  the  netting,  which  threw  him  off  balance.    Emergency  medial  responders  were  immediately  summoned  and  transported  the  worker  to  Chino  Valley  Medical  Center.    He  was  kept  overnight  and  may  require  surgery.

8/11/15 Outside  Lineman Significant  Injury Fall

Significant  Injury  August  11,  2015  –  A  contractor  worker  in  the  Monrovia  District  was  climbing  up  to  the  boom  of  a  digger  to  clear  the  wire  that  was  caught  on  the  boom.  As  he  was  climbing  up,  he  stepped  onto  a  piece  of  steel  bar  holding  the  emergency  lights.  As  he  transferred  his  weight  to  the  steel  bar  to  make  his  climb,  the  bar  broke  and  the  employee  fell  approximately  10  feet  to  the  ground,  striking  his  lower  back.  The  lineman  went  back  to  work,  however  the  next  day  when  the  body  cooled  down  the  employee's  back  was  stiff.  He  saw  his  doctor  where  it  was  determined  he  had  a  lower  back  strain.  No  other  injuries  reported  at  this  time.

8/25/15 Outside  Crew Significant  Injury Fall

Significant  Injury  August  25,  2015  -­‐  A  contractor  crew  in  the  Dominguez  Hills  -­‐  Compton  District  was  tasked  with  replacing  a  deteriorated  pole  on  the  Senga  4kV  cutover.  A  "cold"  apprentice  lineman  climbed  up  to  the  phone  and  cable  line  to  work  at  the  communication  level.  The  apprentice  belted  off  with  his  rope  safety  above  the  first  cross  arm.  He  then  attempted  to  cut  the  cross  arm  (not  attached  to  the  buddy  pole)  with  a  chainsaw.  The  apprentice  inadvertently  cut  through  his  safety  and  fell  approximately  15  feet  onto  a  block  wall,  then  fell  another  5  feet  to  the  ground.  The  crew  immediately  called  911.  The  apprentice  was  alert  and  walking  around  but  was  taken  to  the  hospital  as  a  precautionary  measure.  He  received  three  stitches  to  his  chin  and  was  released  the  same  day.                                                                                                

9/4/15Occupation  Outside  Crew Significant  Injury Laceration

Significant  Injury  -­‐  On  September  4,  2015  -­‐  A  contract  crew  member  sustained  an  injury  Friday  morning  after  pressurized  fluid  from  a  failed  hydraulic  hose  caused  a  laceration  to  his  finger.  The  contractor  was  with  a  crew  working  in  a  de-­‐energized  splice  box  on  the  Elbowing  12kV  circuit  in  Visalia.  The  contractor  was  wearing  proper  PPE—including  leather  work  gloves—at  the  time  of  the  incident.  He  had  been  pressing  on  lugs  (connectors)  with  a  hydraulic  press  when  the  hose  failedat  the  point  where  he  was  holding  it  and  the  released  pressure  penetrated  the  bottom  of  his  pinky  finger  and  exited  on  the  other  side  between  his  finger  and  fingernail.    The  contractor  received  medical  attention  at  the  Kaweah  Delta  Hospital  after  his  injury  and  was  released  with  no  restrictions.  No  immediate  treatment  was  required  aside  from  basic  first  aid,  but  he  will  follow  up  with  a  physician  next  week.  The  incident  serves  as  a  reminder  to  thoroughly  inspect  all  equipment  prior  to  using  it,  particularly  pressurized  hydraulic  equipment  such  as  the  press  the  contractor  was  using.  Carefully  examine  all  hoses  and  connecting  points  and  ensure  that  everything  is  secure  and  in  good  working  order.    Verify  that  the  hoses  and  fittings  you  are  working  with  comply  with  the  proper  pressure  rating.  Additionally,  be  certain  you  are  always  wearing  the  proper  PPE  for  the  job  at  hand.

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Body  Part  /    Root  Cause Description

9/11/15 Outside  Crew Significant  Injury Laceration  

Significant  Injury  -­‐  On  September  11,  2015  -­‐  Valencia  -­‐  A  contractor  crew  was  working  on  tower  modifications  from  a  bucket  truck.  The  employee  removed  the  knee  brace  off  an  18-­‐foot  section  of  tower,  disassembling  the  lacing  from  the  bottom  up  on  the  tower.  After  the  employee  removed  the  knee  brace,  he  used  a  hydraulic  gun  to  loosen  the  lacing  on  the  leg.  As  he  did  this,  he  had  his  hand  on  the  leg  of  the  tower.    Once  the  leg  was  loosened,  the  lacing  swung  downward  and  caught  his  finger  between  the  lacing  and  the  leg  steel.  The  crew  STOPPED  work  and  lowered  the  bucket  to  the  ground.  The  employee  and  his  crew  mates  checked  out  the  injury.  Notifications  were  made.  It    was  determined  the  employee  need  to  go  to  the  hospital  to  be  evaluated.  The  foreman  transported  the  employee  to  the  nearby  hospital.  The  employee  sustained  a  laceration  and  contusion  to  his  right  index  finger.  

9/18/15 Outside  Crew Significant  Injury Ankle  Strain

Significant  Injury  -­‐  On  September  18,  2015  -­‐  Valencia  -­‐  A  contract  worker  twisted  his  ankle  while  working  at  a  tower  site.  The  tower  location  is  on  a  hill  with  about  a  12-­‐foot  slope  running  through  the  middle  of    the  tower.  Legs  A  and  D  are  on  the  top  with  6-­‐foot  leg  extensions  and  legs  B  and  C  are  at  the  bottom  with  18-­‐foot  leg  extensions.  The  contractor  crew  had  finished  working  on  the  north  face  of  the  tower  in    between  legs  C  and  D.      The  worker  was  going  down  the  hill  on  the  north  face  from  leg  D  to  C  so  he  could  inspect  the  crew's  work.    As  he  neared  the  bottom  of  the  hill,  his  foot  became  stuck  in  a  gopher  role,  causing  the  worker  to  roll    his  ankle  and  fall.  He  felt  pain  and  was  able  to  walk,  but  when  the  employee  went  home  and  removed    his  boot,  he  noticed  his  ankle  was  very  swollen.  He  went  to  the  nearest  medical  facility  to  have  his  ankle  X-­‐rayed.  His  ankle  wasn't  broken  but  strained.  The  worker  was  instructed  not  to  put  a  lot  of  weight  on  his  ankle.  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

9/27/15 Outside  Crew Significant  Injury Lacerations

Significant  Injury  -­‐  September  27,  2015  -­‐  San  Joaquin  -­‐  A  contractor  employee  was  retrieving  a  small  hand  coil  of  SEC  wire  off  of  the  belly  of  a  bucket  truck.    As  he  was  doing  this  he  did  not  notice  that  there    was  a  chainsaw  placed  next  to  the  wire.  When  he  pulled  the  wire  down  it  got  caught  on  the  chainsaw,    causing  the  chainsaw  to  fall  off  of  the  catwalk  of    the  truck.  It  fell  blade  first  and  struck  the    employee  on  the  right  leg  in  between  his  calf  and  ankle.  This  resulted  in  a  laceration  about  4  to  6    inches  long.  The  employee  was  taken  to  the  ER  and  received  15  stitches.  The  contractor  called  for  a    stand  down  on  Sept.  30,  to  go  over  the  incident  with  the  rest  of  the  crews  and  discuss  with  them              housekeeping  on  their  trucks  and  the  results  of  not  having  tools  put  away  or  in  a  place  where  there          wouldn't  be  a  chance  of  tools  falling  and  injuring  themselves  or  someone  else.        

10/27/15 Outside  CrewSignificant  Accident Lacerations

Significant  Accident  -­‐  October  27,  2015  -­‐  Foothill  -­‐  A  worker  sustained  a  laceration  to  his  left  thumb          while  working  on  the  air  compressor  on  his  service    truck  as  he  was  attempting  to  cut  a  zip  tie  that  was  holding  the  air  compressor  service  lines  together.      According  to  the  report,  the  workers  stopped  work    and  proceeded  to  walk  around  to  the  side  of  his    service  truck  to  retrieve  his  first-­‐aid  kit  but  as    he  was  walking,  he  was  looking  down  at  his  thumb  and  his  forehead  made  contact  with  an  open  bin  drawer  on  his  service  truck,  resulting  in  a  laceration  to  his    forehead.  The  worker  was  transported  to  the  Apple  Valley  Hospital  for  first-­‐aid  treatment.  This  report  reflects  all  information  received  to-­‐date  from  the  reporting  company  to-­‐date.      

11/10/15 Outside  Crew Significant  Accident

Lacerations

Significant  Accident  -­‐  November  10,  2015  -­‐  Foothill  -­‐  A  contract  worker  was  in  the  process  of  drilling  a  hole  with  a  mag  drill  when  the  drill  unexpectedly  shifted  to  the  left  and    made  contact  with  the  employee’s  left  hand  glove.  The  glove  became  entangled  with  the    spinning  drill  bit,  causing  lacerations  to  the  employees  left  middle  and  ring  fingers.  The  employee  was  transported  to  the  St.  Mary's    Hospital  emergency  room  for  treatment.  The    employee  received  several  stitches  to  his  fingers.  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

10/7/14 Outside  Crew CCCIImproper  Material

CCCI  -­‐  On  October  7  2014,  Workers  preparing  to  replace  a  pole  caused  an  energized  conductor  to  go  phase-­‐to-­‐ground,  putting  several  people  on  the  ground  at  risk  and  resulting  in  a  Crew-­‐Caused  Circuit  Interruption  (CCCI)  on  both  the  Weston  and  Bobcat  12kV  circuits.  No  one  was  injured  as  a  result  of  the  incident.  The  crew  used  an  incorrect  dead-­‐end  shoe  while  installing  a  set  of  isolators  to  de-­‐energize  a  small  section  of  line.  Because  the  incorrect  dead-­‐end  shoe  was  too  large,  wire  slipped  through  and  fell  onto  the  grape  vines  below,  going  phase-­‐to-­‐ground  across  the  steel  wire  used  to  support  the  grapes.  This  occurred  just  10  feet  from  several  vehicles  and  300  yards  from  field  workers.  The  field  workers  were  in  a  different  row  of  grape  vines  at  the  time  of  the  incident  and  were  unharmed.  

12/17/14 Outside  Crew CCCIImproper  Working  Position

CCCI  -­‐  On  December  17,  2014,  an  employee  was  positioning  himself  (while  aloft  in  an  Arial  bucket)  to  make  the  separation  between  the  arrestor  ground  and  the  open  wire  secondary  neutral,  when  he  inadvertently  pushed  the  boom  knuckle  located  behind  the  bucket  against  the  alley  side  secondary  conductor.    The  additional  pressure  applied  to  the  conductor  initiated  a  change  in  the  vertical  construction  sag  one  span  away  that  caused  a  phase  to  ground  contract  mid-­‐span,  which  resulted  in  a  transformer  level  outage  to  4  customers  lasting  approximately  45  minutes.    No  injuries  were  sustained  as  a  result  of  this  incident.    Causes:    The  employee  did  not  realize  the  upper  section  of  the  b  boom  was  resting  against  the  secondary  conductor  when  he  moved  the  bucket  into  position.    No  movement  in  a  bucket  position  should  have  permitted  prior  to  checking  that  the  surrounding  area  was  clear.    To  reach  the  work  area  via  bucket,  the  lineman  needed  to  position  himself  between  the  secondary  conductor  (above)  and  the  communication  cable  (below)  in  which  the  bucket  narrowly  fit.    Learning's:    The  lineman  could  have  stopped  the  moving  bucket  and  reassessed  the  situation,  or  utilized  a  ground  personnel  as  a  spotter.    When  maneuvering  bucket  trucks  into  position  sometimes  it  is  necessary  to  crouch  down  in  the  buck  for  clearance  purposes.    When  utilizing  this  approach  it  is  good  to  have  spotters  or  use  a  stop  and  act  think  review  approach  prior  to  moving  the  bucket  further  due  to  limited  visibility.

1/14/15 Outside  Crew CCCI No  Observation

CCCI  -­‐  On  January  14,  a  Contract  crew  was  assigned  to  remove  and  replace  a  deteriorated  transmission  pole.    The  crew  completed  setting  the  new  pole  and  began  transferring  the  12kV  circuit  to  it.  The  crew  was  using  2  buckets  to  move  the  conductors.  The  crew  first  moved  the  street  side  conductors  safely  to  the  new  arm  on  the  new  pole.  As  the  crew  moved  under  the  street  side  conductors,  they  had  just  transferred,  in  order  to  access  the  field  phases,  the  jib  on  one  of  the  buckets  caught  the  inside  street  side  phase.  Unknowingly,  they  kept  moving;  the  conductor  came  off  the  jib,  violently  jolting  the  line  thus  causing  the  two  street  side  phases  to  come  into  close  proximity  with  each  other,  relaying  the  Typhoon  12kv  circuit  into  the  Foreman’s  no  test  orders.  No  Injuries

Contractor  Circuit  Interruption  Incidents

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

2/17/15 Outside  Crew CCCI No  Observation

CCCI  –  On  February  17,  A  Contract  Crew    in  Crestline  was  in  the  process  of  replacing  a  set  of  double  arms.  The  crew  had  installed  the  first  arm  on  the  existing  through  bolt,  removed  the  old  arms  and  transferred  the  wire.  While  installing  the  second  arm  on  the  through  bolt,  they  failed  to  observe  that  the  DA  bolts  on  the  ends  of  the  arms  were  forcing  the  first  arm  off  the  through  bolt.  The  first  arm  came  off  the  through  bolt  and  wind-­‐milled,  resulting  in  a  circuit  lockout.

2/17/15 Outside  Crew CCCI Cable  Marking

CCCI  –  On  February  17,  A  Contract    crew  in  Monterey  Park    was  tasked  to  replace  existing  primary  and  secondary  CIC/direct  bury  construction  with  a  new  conduit  system.  An  outage  was  planned  on  Feb.  17.  After  de-­‐energizing  a  line,  the  crew  foreman  phoned  cable  from  a  BURD  switch  located  inside  a  vault  and  removed  line  and  load-­‐side  cables.  The  foreman  did  not  mark  the  cable  run  following  the  phone  procedure  nor  did  he  protect  from  back  feed.  Essentially,  the  foreman  wired  the  URD  switch  incorrectly.  It  was  wired  with  a  phase-­‐to-­‐phase  short  on  L1  through  R1.  After  this,  the  crew  continued  landing  cable  using  the  live-­‐line  tool  method.  The  foreman  released  clearance  and  the  Troubleman  closed  the  position  on  the  general  switch.  The  caused  the  fuse  to  blow  on  the  incorrectly  wired  BURD  switch.  No  injuries  were  reported.

2/18/15 Outside  Crew CCCI No  Observation

CCCI  -­‐  On  February  18,  a  Contract  crew  was  assigned  to  replace  a  deteriorated  pole  on  the  La  Grande  12kV  circuit.    The  crew  completed  the  installation  of  the  new  pole  and  were  in  the  process  of  transferring  the  conductors.  The  span  to  the  south  contained  flying  taps,  approximately  50’  from  the  new  pole,  with  30  inches  of  clearance  between  the  two  circuits.  The  crew  began  moving  the  conductors  onto  the  new  pole,  starting  with  the  field  side.  Once  they  secured  and  finished  transferring  the  field  side,  they  began  to  transfer  the  street  side  conductors.  The  crew  moved  the  inside  conductor  into  position  and  secured  it  and  then  began  to  move  the  outside  conductor  into  position.  As  the  crew  moved  it  closer  to  the  pole  they  inadvertently  allowed  the  conductor  to  sag  and  bounce  into  the  lower  conductor.  This  occurred  just  outside  of  their  protective  cover  and  caused  the  circuit  to  relay  into  the  Foreman’s  no  test  orders.  No  injuries.

2/25/15 Outside  Crew CCCI Operator  Error

CCCI  –  On  February  25,    A  Contract  crew  was  in  the  process  of  removing  an  old  KPF  switch  and  replacing  it  with  a  new  RCS  switch.  The  crew  had  already  installed  the  new  omniruptor  switch  and  removed  the  old  KPF  switch.  The  crew  positioned  the  tub  bucket  to  wire  up  the  potential  tap  (PT);  they  had  the  fiberglass  portion  of  the  boom  resting  against  the  covered  outside  phase.  During  this  process,  the  old  copper-­‐weld  wire  parted  and  fell  to  the  ground,  resulting  in  a  circuit  lockout  on  the  Desolate  12kV.The  crew  called  an  all  STOP,  regrouped,  and  after  meeting  with  the  local  Troubleman,  made  repairs  and  re-­‐energized  the  circuit.

2/25/15Contract  Tree  

Crew CCCI Operator  ErrorCCCI  -­‐  On  February  25  at  1450  hours,  the  Track  4kV  Circuit  out  of  Michillinda  Substation  relayed  and  reclosed.    An  SCE  contract  tree  crew  allegedly  allowed  a  boom  to  snag  phone  and  communication  lines  causing  phases  to  slap  together.

2/25/15 Outside  Crew CCCI Operator  Error

CCCI  -­‐  On  February  25  at  0958  hours,  Logan  12kV  Circuit  out  of  Earlimart  Substation  relayed  with  No  Test  Orders  in  effect.    An  SCE  contract  was  stringing  new  conductor  on  the  Vestal-­‐Columbine-­‐Delano-­‐Earlimart  66  kV  line  when  it  allegedly  parted  and  contacted  the  Logan  12  kV  line  and  a  flashover  occurred.  There  were  no  reports  of  injuries.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

2/26/15 Outside  Crew CCCI Conductor  Control

CCCI  –  On  February  26,  A  Contract  crew  was  set  to  replace  a  deteriorated  pole.  The  same  hole  set  was  required  due  to  the  five  telephone  trunk  line  dips.  The  pole  had  a  12kV  double  dead-­‐ended,  4kV  dead-­‐ended  and  a  secondary  triplex.  The  crew  was  in  the  process  of  transferring  the  12kV  336  acsr  conductors.  The  over-­‐the-­‐arm  taps  had  been  bypassed  out  and  Lineman  1  was  removing  the  field  phase  over  the  arm  jumper.  He  had  disconnected  one  side  of  the  jumper  and  was  bending  it  back  to  disconnect  the  other  side  in  order  to  remove  the  tap.  He  had  the  tap  in  his  hand  when  he  lost  his  footing,  slipping  in  the  bucket  and  losing  control  of  the  tap.  The  tap  sprung  out  from  his  hand  and  hit  the  center  phase  over-­‐the-­‐arm  tap,  with  enough  force  to  move  the  rubber  blanket  that  was  covering  the  center,  and  made  contact  with  the  bare  tap.  This  instantly  relayed  the  circuit  because  No  Test  orders  were  in  place.

2/27/15 Outside  Crew CCCIConductor  Control

CCCI  -­‐  On  February  27  at  0914  hours,  the  Hartle  4kV  Line  out  of  Cudahy  Substation  relayed  with  No  Test  Orders  in  effect.    An  SCE  contract  crew  reportedly  allowed  a  wing  arm  to  fall  and  contact  a  conductor,  which  caused  a  flashover.    There  were  no  reports  of  injuries.

2/28/15 Outside  Crew CCCI Boom  Contact

CCCI  -­‐  On  February  28,  an  SCE  contract  crew  reportedly  allowed  a  boom  to  contact  a  conductor,  which  caused  a  flashover  and  a  fuse  to  blow.    The  affected  section  of  the  Campbell  12kV  Circuit  out  of  Porterville  Substation  was  scheduled  for  a  planned  outage.  There  were  no  reports  of  injuries  or  additional  damage  to  equipment.

3/4/15 Outside  Crew CCCI Not  Clearing  the  Bond

CCCI  -­‐  On  March  4  at  0930  hours,  an  SCE  contract  crew  reportedly  contacted  a  conductor  with  an  insulator  pin  during  scheduled  work.    A  flashover  occurred  and  the  Poppet  Flats  12kV  Circuit  out  of  Cabazon  Substation  relayed.  There  were  no  reports  of  injuries  or  equipment  damage.  The  crew  did  not  remove  the  bond  which  was  grounded.

3/5/15 Outside  Crew CCCI Conductor  Control

CCCI  -­‐  On  March  5  at  1242  hours,  an  SCE  contract  crew  reportedly  allowed  conductors  to  contact  each  other.  A  flashover  occurred  and  two  spans  of  wire  fell  and  broke  a  cross  arm.  The  North  Beach  4kV  circuit  relayed  to  lockout  at  Manhattan  Substation.    There  were  no  reports  of  injuries.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

3/6/15 Outside  Crew CCCILocates  Not  Performed

CCCI  -­‐  On  March  5  a  four  person  line  crew  was  working  on  an  Agriculture  job  to  install  a  pole,  transformer  and  anchor  for  a  well  pump  in  Bakersfield,  CA.    Damaged  an  AT&T  line  containing  a  twelve  count  fiber  optic  cable.    On  3/4/2015  the  crew  set  the  pole,  installed  the  transformer  and  placed  the  anchor.    One  3/6/2015  the  crew  returned  to  the  jobsite  to  reinstall  the  anchor  as  it  had  pulled  up.    The  crew  completed  the  task  and  went  home  for  the  day.    Later  on  in  the  evening  of  3/6/2015,  a  PG&E  inspector  contacted  the  GF  in  charge  of  the  work  and  informed  him  that  there  was  a  fiber  line  outage  in  the  area  on  the  that  the  crew  had  been  previously  working.        Locates  were  not  called  in  the  jobsite.    Upon  further  investigation,  it  was  found  the  job  was  never  called  in  for  a  USA  ticket  to  locate  the  underground  facilities.    The  crew  completed  the  work  both  days  without  having  any  locates.      Learning's:    The  GF  and  Crew  violated  the  Companies  Employee  Standard  of  Conducts  rules:    7.2.12  -­‐  Gross  or  willful  neglect  of  established  safety  rules  which  create  an  actual  or  potential  threat  of  death  or  serious  injury  to  employees  or  customers.    7.2.13  -­‐  Violation  of  Company  Safety  Rules.    The  crew  failed  to  follow  the  process  set  forth  in  the  Companies  Rules  to  Dig  By.    There  was  no  One-­‐Call  ticket.

3/10/15 Outside  Crew CCCIImproper  

Transformer  

CCCI  –  on  March  10,  2015  –  Line  crew  was  working  to  replace  a  pole  on  Hwy  128  in  Boonville,  CA.  At  the  time  of  the  incident,  the  crew  was  working  to  energize  the  overhead  line  and  close  the  cutouts.    An  apprentice  unintentionally  hooked  the  under  arm  service  bus  wire  to  both  hot  legs  of  the  open  wire  secondary,  which  created  a  short  circuit.    The  line  was  energized,  which  blew  the  transformer  fuses.    The  crew  opened  the  line  back  up,  fixed  the  secondary,  changed  out  the  transformer  fuses  and  re-­‐energized  the  line.    They  double-­‐checked  the  meters,  which  appeared  to  be  OK.

3/18/15 Outside  Crew CCCI Conductor  Control

CCCI  -­‐  On  March  18  at  1127  hours,  an  electrical  disruption  occurred  when  the  Solar  4kV  Line  relayed  at  Maywood  Substation  when  neutral  conductor  parted  from  an  insulator  and  contacted  another  conductor  while  an  SCE  contract  crew  was  performing  scheduled  maintenance.  No  damage  or  injuries  were  reported.  

4/7/15 Outside  Crew CCCI No  ObservationCCCI  -­‐  On  April  7  2015,  an  SCE  contract  crew  was  performing  maintenance  on  a  4  kV  Circuit  when  a  conductor  reportedly  contacted  a  12kV  Circuit  causing  a  flashover  during  a  planned  outage.    There  were  no  injuries  reported.    

4/13/15 Outside  Crew CCCI No  ObservationCCCI  -­‐  On  April  13  2015,  a  16kV  Circuit  relayed  and  reclosed  during  scheduled  maintenance  to  replace  a  deteriorated  pole.  A  contract  crew  reportedly  allowed  conductors  to  make  contact  with  foliage  underneath.  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

4/22/15 Outside  Crew CCCIConductor  Control

CCCI  –  on  April  22,  2015  –  Line  crew  was  working  to  replace  a  three-­‐phase  tangent  pole.    Before  work  began,  the  crew  inspected  the  adjacent  structures  and  the  span,  which  included  a  12kV  single-­‐phase  tap  line.    The  tap  line  was  framed  in  such  a  way  that  allowed  one  of  the  conductors  of  the  tap  line  to  cross  under  the  three-­‐phase  line  at  a  angle.    The  crew  determined  they  had  enough  clearance  to  complete  the  work  without  covering  the  single-­‐phase  top  line.    Using  rubber  gloves,  the  crew  was  working  to  spread  the  field  side  phase  of  the  three-­‐phase  line  onto  a  hot  arm.    The  phase  was  removed  from  the  insulator  and  moved  about  sic  inches  out  and  down  to  the  fiberglass  hot  arm.    As  soon  as  the  phase  was  transferred  to  the  hot  arm,  it  made  contact  with  the  tap  line  causing  the  10-­‐amp  fuse  feeding  the  tap  line  (at  LCO51845)  to  open.    The  line  crew  immediately  stopped  work  to  assess  the  issue.    The  inspector  was  notified.    No  one  was  injured  and  apart  from  the  10  amp-­‐opening  fuse,  no  damage  occurred.    The  tap  line  was  re-­‐fused  and  re-­‐energized,  and  the  crew  was  able  to  complete  the  work  without  further  incident.

4/28/15 Outside  Crew CCCI Dig  In

CCCI  –  4-­‐28-­‐2015-­‐  Compton  District  -­‐  A  contractor  crew  was  working  on  a  vault  replacement  job.  The  crew  located  all  known  or  suspected  utilities  by  hand,  via  the  use  of  a  shovel,  prior  to  utilizing  a  backhoe.  A  4-­‐inch  SCE  conduit  was  located  at  80  inches  deep  and  on  top  of  the  SCE  encasement.  After  all  known  and  suspected  utilities  were  located  a  contractor  began  using  a  backhoe  to  remove  the  concrete  sand  slurry  backfill  that  was  on  top  of  the  previously  located  4-­‐inch  SCE  conduit.  As  the  worker  was  scratching  down  the  concrete  sand  slurry  with  the  backhoe,  he  struck  the  4-­‐inch  SCE  conduit  with  the  teeth  of  the  backhoe  bucket.  This  caused  one  of  the  cables  inside  of  the  conduit  to  arc.  The  4-­‐inch  conduit  was  struck  at  60  inches  deep,  3  feet  away  from  where  it  was  originally  located  at  a  depth  of  80  inches.

5/1/15 Outside  Crew CCCI No  Observation

CCCI  -­‐  on  5-­‐1-­‐2015  -­‐  North  Coast  Region  -­‐  Natural  Substation  Project  -­‐  A  contractor  crew  was  tasked  with  hanging  a  radio  repeater  on  a  dead-­‐end  wood  pole  and  transferring  a  conductor  to  make  room  for  TSP  footing.  After  hanging  the  radio  repeater,  the  crew  relocated  to  the  next  pole  over  in  order  to  transfer  the  conductor.  The  contractor  went  up  in  the  bucket  to  test  and  ground  the  line.    During  testing,  it  was  determined  that  the  line  was  still  energized.  The  crew  members  then  realized  they  were  working  at  a  location  that  was  not  part  of  the  planned  line  outage.

5/1/15 Outside  Crew CCCI Conductor  Control

CCCI  –  on  5-­‐1-­‐2015  -­‐  San  Joaquin  Region  -­‐  A  contractor  crew  was  involved  in  re-­‐conducting  a  section  of  the  Caratan  12kV  circuit  out  of  Vestal  Substation.  The  new  wire  was  in  and  energized  and  the  crew  was  in  the  process  of  removing  the  old  1/0  ACSR.      Three  contractors  on  the  crew  were  tasked  with  removing  a  section  of  the  old  1/0  ACSR,  which  was  spread  on  hot  arms.    This  was  also  over  an  energized  tap  line  below.  The  crew  cut      a  bubble  in  the  wire  on  the  side  held  by  the  foreman  and  on            the  other  side  held  by  a  lineman.  When  the  wire  was  cut,  the  hand  line  slipped  from  their  grasp  a  little.  When  this  occurred  the  wire  rolled  and  the  tail  made  contact  just  outside  of  cover  on  the  energized  #7  cu  on  the  tap  line      below,  locking  out  the  circuit.  The  foreman  contacted  Rector  Substation  and  notified  the  operator.  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

5/9/15 Outside  Crew CCCI Material  Failure

CCCI  -­‐  on  May  9-­‐2015  -­‐Ontario  -­‐  Crew  tasked  to  replace  pole,  phase  to  phase  arch  flash  occurred  as  crew  opened  a  fused  cut-­‐out  with  load  bust  tool.  Investigation  pending  results  of  material  failure  report;  N-­‐CCCI  vs  CCCI  which  affected  268  customers  for  approx.  5  hours.  No  injuries  or  property  damage.

5/9/15 Outside  Crew CCCI Operator  Error

CCCI  -­‐  on  May  9-­‐2015  -­‐  Ontario  District  -­‐A  contractor  crew  was  tasked  with  replacing  a  pole  that  had  a  primary  3-­‐phase  underground  dip  attached.  The  crew  foreman  and  a  lineman  went  up  to  clear  the  3-­‐phase  dip  on  the  pole.  The  crew  opened  the  first  fuse  without  incident.  While  they  attempted  to  open  the  second  fuse,  a  flash  occurred,  causing  the  circuit  to  relay.  

5/22/15 Outside  Crew CCCI No  Observation

CCCI  -­‐  on  May  22  2015  -­‐  A  subcontractor  was  in  the  process  of  picking  up  plywood  used  for  the  backyard  machine.  When  the  foreman  picked  up  the  outriggers,  he  did  not  put  the  boom  in  the  cradle  and  started  to  drive  with  the  boom  in  the  elevated  position.  The  boom  contacted  the  phone  line,  causing  one  phase  to  burn  down.                                                      

5/26/15 Outside  Crew CCCIInadequate  Attention/  Process

CCCI  -­‐  on  May  26,  2015  -­‐  Line  crew  was  working  to  pull  wire  across  four  spans.    The  crew  had  surveyed  the  four  spans  and  initially  decided  to  cover  an  energized  feeder  circuit  that  crossed  underneath.    However,  the  crew  had  difficulty  placing  equipment  in  position  to  cover  the  crossing,  and  decided  they  had  enough  clearance  over  the  feeder  (approximately  50-­‐60  feet)  to  do  the  pull  without  covering  the  feeder.    The  plan  was  to  pull  the  rope  with  the  old  wire.    An  employee  on  the  rewind  puller  end  told  the  crew  on  the  rope  puller  end  that  he  was  starting  to  move  on  his  end  (via  radio),  and  the  employee  running  the  rope  end  puller  acknowledged  via  radio.    As  pressure  was  starting  to  build  on  the  rewind  end  the  employee  on  the  rope  puller  end  started  to  release  the  brakes  on  the  puller.    The  employee  let  the  brakes  off  too  quickly,  allowing  the  wire  to  run  out.    The  wire  slacked  down  and  made  contact  with  the  uncovered  energized  feeder  circuit  that  crossed  underneath  the  pull,  which  caused  a  circuit  interruption  on  the  feeder.    The  crew  stopped  immediately  and  notified  the  general  foreman,  who  was  not  on  site  at  the  time.    No  one  was  injured.    The  equipment  was  grounded  and  barricaded.    A  precondition  is  a  pre-­‐existing  condition  that  contribute  to  the  occurrence  of  the  inappropriate  act  (e.g.,  inattention,  inadequate  process,  inadequate  oversight,  etc.)                                                    

6/24/15 Outside  Crew CCCI Operator  ErrorCCCI  –  on  June  24,  2015  -­‐  A  contractor  crew  in  the  Ontario  District  was  drilling  a  TSP  foundation  with  an  excavator  using  an  auger  bit.  When  the  contractor  reached  a  depth  of  36  inches,  the  auger  made  contact  with  a  12kV  conduit  and  4/0  ground,  damaging  the  conduit  and  causing  the  circuit  to  relay.    

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

6/25/15 Outside  Crew CCCI Operator  Error

CCCI  –  on  June  25,  2015  -­‐  A  contractor  crew  in  the  Covina  District  was  replacing  a  deteriorated  pole.  They  used  a  100-­‐foot  bucket  truck  and  installed  a  temporary  cross  arm  to  hold  up  a  336  4  wire  circuit  where  midspan  taps  had  been  originally  installed.  The  crew  secured  the  phases  and  installed  primary  cover.  After  shutting  off  the  bucket  truck,  the  crew  began  framing  the  pole  and  digging  the  hole  for  the  new  pole,  when  the  circuit  locked  out.  The  bucket  truck's  hydraulics  began  to  bleed  off,  causing  the  boom  to  lower  and  the  top  field  phase  to  contact  the  bottom  inside  field  pole  phase.  The  phases  were  both  damaged  and  the  crew  installed  temporary  bypasses  which  are  to  be  spliced  out  with  compression  splices.  Load  was  restored  without  further  incident.

7/6/15 Outside  Crew CCCI Cable  Failure

Significant  Injury  July  6,  2015  –  A  contractor  crew  in  the  Fullerton  District  was  tasked  with  replacing  several  runs  of  CIC  cable  beyond  a  fuse  dip;  however,  one  run  of  cable  was  not  scheduled  to  be  replaced.  Another  environmental  contractor  crew  was  in  a  structure  removing  debris.  Upon  completion  of  the  job,  the  other  contractor  crew  closed  the  fuse  to  re-­‐energize  the  radial.  The  fuse  blew.  The  crew  discovered  the  cable  failed  inside  the  structure  the  environmental  crew  was  inside.  The  crew  sent  notifications,  repaired  the  cable  and  re-­‐energized  the  radial  without  further  incident.  No  injuries  or  other  damage  was  reported.      

7/13/15 Outside  Crew CCCIImproper  

Transformer  Hookup

Significant  Injury  July  13,  2015  –  A  contractor  crew  in  the  San  Joaquin  District  had  replaced  a  12kv  pad  mount  transformer.  When  the  crew  closed  the  fuse  dip  to  energize  the  pad  mount,  the  fuses  blew,  causing  an  interruption.  It  was  determined  that  the  crew  had  miswired  the  pad  mount,  which  caused  the  circuit  to  go  phase-­‐to-­‐phase.  The  line  was  protected  by  a  fused  BURD  switch  and  the  fused  dip.  The  crew  uncrossed  the  phases  in  the  pad  mount,  replaced  the  fuses  and  re-­‐energized  the  tap  line.  The  crew  was  retrained  on  the  proper  wiring  of  this  particular  type  of  transformer.

7/16/15 Outside  Crew CCCI Flash

Significant  Injury  July  16,  2015  –  A  contractor  crew  in  the  San  Joaquin  District  went  to  the  rear  property  line  to  de-­‐energize  the  fused  dip  feeding  a  BURD  transformer.  The  crew  used  a  long  stick  to  open  the  fuse,  and  upon  opening,  it  created  an  arc,  relaying  the  circuit.  The  flash  did  burn  up  an  insulator  and  the  tap  that  feeds  the  dip,  and  a  single  phase  line  with  one  overhead  transformer  on  it.  The  crew  did  not  use  the  proper  tool  for  the  task  at  hand.  The  crew  should  have  used  a  load  buster  tool,  which  would  have  prevented  an  arc  from  forming.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

7/25/15 Outside  Crew CCCI Conductor  Control

Significant  Injury  July  25,  2015  –  A  contractor  transmission  crew  in  the  Ontario  District  was  tasked  to  replace  an  80  H5  pole.  The  crew  conducted  a  tailboard  and  inspected  both  adjacent  structures.  The  pole  to  the  east  had  been  replaced  by  the  same  contractor  company  a  few  months  ago,  and  the  pole  to  the  west  looked  good;  it  was  a  fairly  new  light-­‐weight  steel  (LWS)  pole.  The  crew  was  to  same  hole  set  the  pole  they  were  replacing.  The  crew  was  in  the  process  of  floating  the  12kV.  This  portion  of  the  line  runs  east  to  west.  The  crew  had  two  south  phases  floated,  and  when  they  were  floating  the  third  north  phase  about  halfway  down  they  heard  noises  coming  from  the  pole  to  the  west.  The  crew  reported  that  it  sounded  like  metal  on  metal.  The  pole  where  the  noises  were  coming  from  was  also  a  LWS.  The  crew  stopped  work.  The  two  ground  personnel  went  back  to  the  LWS  pole  and  reported  that  the  arm  looked  OK  and  the  insulators  and  clamp-­‐tops  were  not  pulled  over.  They  figured  the  noise  they  heard  was  the  through  bolt  on  the  arm  making  noise  in  the  steel  pole.  The  crew  then  decided  to  move  the  third  phase  back  to  the  arm  on  the  pole  being  replaced,  and  move  the  bucket  to  the  LWS  pole  where  the  noise  was  coming  from.  Before  they  moved  the  phase,  the  arm  on  the  LWS  pole  broke  on  the  south  side,  and  it  made  contact  with  the  pole  causing  a  phase-­‐to-­‐phase  arc.  The  arc  ran  down  the  line  toward  the  two  lineman  in  the  air.  The  crew  at  the  job  site  was  practicing  the  "1  +  1"  cover.  They  had  16  guts  on  the  pole  they  were  replacing.  When  the  arc  was  running  down  the  line  it  snuffed  itself  out  when  it  made  it  to  the  cover.  The  crew  did  have  No  Test  Orders.  The  crew  secured  the  area  and  called  for  a  troubleman.  No  injuries  reported.  No  damage  reported.  In  contractor's  investigation,  they  concluded  that  the  arm  had  a  date  on  1/08  stamped  in  the  cross  arm.  They  performed  wire  weight  calculations  and  found  they  were  well  below  50  percent  of  what  the  arm  is  good  for.

7/27/15 Outside  Crew CCCI No  Observation

Significant  Injury  July  27,  2015  –  A  contractor  crew  in  the  South  Bay  District  was  tasked  with  changing  out  a  deteriorated  transmission  pole.  The  crew  arrived  on  location,  tailboarded  and  began  the  process  of  obtaining  No  Test  Orders  on  the  Stringer  4kV  and  Occidental  16kV,  then  de-­‐energizing  the  section  of  66kV  line  to  be  worked.  While  in  the  process  of  setting  the  pole  (framed),  the  top  section  of  crossarms  contacted  the  energized  4kV  and  brought  two  of  the  phases  together  approximately  40  feet  from  the  existing  pole.  This  contact  resulted  in  a  circuit  interruption.  The  contractor  crew  notified  their  management  and  SCE  of  the  interruption.  SCE  troublemen  arrived  on  site  and  deemed  it  safe  to  re-­‐energize.

7/27/15 Outside  Crew CCCI Conductor  Control

Significant  Injury  July  27,  2015  –  A  contractor  crew  in  the  Saddleback  District  was  working  on  a  deteriorated  pole  replacement  project.  The  wire  slipped  through  a  clamp  type  insulator  one  span  away  from  the  pole  being  replaced,  causing  a  slack  or  a  "belly"  on  the  center  phase.  This  caused  two  phases  to  be  close  enough  to  arc  and  relay  the  Xerox  12kV  circuit.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

8/6/15 Outside  Crew CCCI Testing

Significant  Injury  August  6,  2015  –  A  contractor  crew  in  the  Santa  Barbara  District  was  tasked  with  changing  out  a  deteriorated  pole  with  an  RCS  with  aerial  cable.  Following  the  program  log  sheet,  a  clearance  was  issued  to  the  foreman  on  the  Armour  4kV  circuit  from  an  open  pole  switch  to  an  open  RCS.  The  foreman's  work  package  had  the  contractor's  COCO  note  that  the  requested  clearance  should  be  from  open  PS  ####  to  open  PS  ####.  After  the  foreman  received  clearance  on  the  4kV  primary,  the  foreman  instructed  the  lineman  to  test  and  prove  de-­‐energized  before  grounding.  The  lineman  tested  the  line  but  did  not  communicate  to  the  foreman  his  reading  and  proceeded  to  ground.  He  was  under  the  assumption  the  whole  line  would  be  de-­‐energized,  including  the  pole  due  because  the  aerial  cable  cannot  be  worked  on  while  energized.  He  put  on  the  first  ground,  which  tripped  the  circuit.

8/8/15 Outside  Crew CCCI Conductor  Control

Significant  Injury  August  8,  2015  –  Two  contractor  crews  were  in  the  Thousand  Oaks  Districts  tasked  with  replacing  two  adjacent  16kV  3/C  tangent  poles  on  the  Galahad  16kV.  Crew  1's  pole  had  a  single-­‐phase  transformer  on  it  and  Crew  2's  pole  included  a  3-­‐phase  bank.  Two  linemen  on  Crew  1  de-­‐energized  their  transformer  and  removed  it.  Then,  they  spread  the  energized  primary  out  on  hot  arms  in  preparation  for  setting  the  new  pole.  The  two  linemen  went  down  to  the  ground  to  help  frame  and  prep  to  get  the  new  pole  set.  Crew  2  de-­‐energized  their  bank  and  proceeded  to  secure  the  primary  conductors  in  a  "Christmas  tree",  also  known  as  a  3-­‐phase  hot  arm  attachment  which  is  mounted  to  a  jib  on  a  separate  truck.  Crew  2  notified  Crew  1  they  were  going  to  be  moving  the  energized  conductors  and  began  moving  them.  During  this  process,  the  street  side  phase  separated  and  contacted  the  ground,  and  then  the  tail  hit  one  of  the  lineman  on  Crew  1.  At  the  time  it  was  not  clear  if  the  conductor  was  energized  at  the  moment  it  made  contact  with  the  lineman.  He  did  not  appear  to  be  injured  but  was  transported  to  the  hospital  as  a  precaution.  He  has  since  been  released  back  to  work  and  suffered  no  injuries.  The  circuit  locked  out  at  the  RAR  which  the  crew  has  No  Test  Orders  on  at  the  time.

8/9/15 Outside  Crew CCCI Conductor  Control

CCCI  -­‐  On  August  9,  2015  -­‐  Conductor  Control  -­‐  Crew  tasked  to  replace  deteriorated  pole,  attempting  to  de-­‐energize  4kv  tap  line  with  load  drop  tool  when  primary  conductor  broke,  causing  circuit  to  lock  out.  Approx.  245  customers  affected  for  33  mins.  No  injuries  or  property  damage.  Crew  was  post-­‐acc  tested.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

8/13/15 Outside  Crew CCCIImproper  

Transformer  Hookup

CCCI  -­‐  On  August  13,  2015  -­‐  A  contractor  crew  in  the  Ontario  District  was  tasked  with  energizing  new  cable,  a  new  RAG  (gas  switch),  and  a  new  transformer  inside  a  vault.  The  switching  procedure  went  as  planned;  however,  the  crew  did  not  finish  the  switching  program  as  planned.  All  there  was  left  to  do  was  heat  up  a  6.9kV  transformer  in  the  same  vault  where  the  gas  switch  was.  This  transformer  was  fed  off  position  2  on  the  new  RAG.  The  next  day,  August  13,  a  troubleman  went  back  to  close  position  2  of  the  RAG,  energizing  the  transformer  in  the  same  vault.  When  the  troubleman  closed  position  2  the  circuit  locked  out.    After  a  quick  investigation  the  troubleman  realized  the  contractor  crew  had  wired  the  6.9kV  transformer  12kV  thus  creating  a  phase-­‐to-­‐phase  fault  in  the  line.  The  troubleman  then  opened  up  position  2  and  had  the  substation  operator  re-­‐energize  the  line.  The  circuit  tested  no  good.  It  was  determined  the  new  RAG  went  bad  due  to  the  phase-­‐to-­‐phase  fault.  The  troubleman  then  isolated  the  switch  and  restored  most  of  the  load.    The  contractor  crew  made  repairs.  No  injuries  reported.  No  other  damage  reported.

8/24/15 Outside  Crew CCCI Ignoring  Test  Equipment

CCCI  -­‐  On  August  24,  2015  -­‐  A  contractor  crew  in  the  Dominguez  Hills-­‐Compton  District  arrived  at  the  job  site  and  held  a  tailboard.  An  SCE  troubleman  opened  a  capacitor  bank.  The  second  SCE  troubleman  broke  the  parallel  at  the  gas  switch.  The  contractor  crew  foreman  asked  the  troublemen  if  they  could  proceed  with  opening  taps  at  a  structure.  The  troubleman  confirmed  "yes."  The  crew  foreman  asked  again  if  the  capacitor  bank  had  been  cleared,  and  the  troublemen  responded  "yes."  The  foreman  directed  a  contractor  lineman  and  apprentice  to  amp  clamp  phases  and  cut  open  the  taps.  The  tester  indicated  28  amps,  which  the  lineman  and  apprentice  believed  was  caused  by  induction  from  the  overbuild.  The  capacitor  bank  hand  not  been  properly  taken  offline,  resulting  in  a  circuit  interruption  when  the  arc  crated  by  opening  |the  taps  contacted  the  phase  above  (vertical  construction).

8/29/15 Outside  Crew CCCI Operator  Error

CCCI  -­‐  On  August  29,  2015  -­‐  Montebello  -­‐  Two  contract  workers,  a  lineman  and  apprentice,  were  working  on  a  16kV  circuit  from  a  bucket  truck.  The  bucket  was  positioned  near  the  16kV  C/O  arm.  The  lineman  attempted  to  move  the  bucket  was  attempting  to  trigger  on  the  pistol  grip  trigger,  which  he  was  not  fully  depressing.  He  adjusted  his  grip  and  was  able  to  depress  the  trigger.  When  he  did  this  the  bucket  moved  abruptly  toward  the  arm  and  made  contact,  which  shook  the  pole.  This  caused  the  4kV  to  the  east  to  slap  together,  relaying  the  circuit.    The  crew  STOPPED,  re-­‐tailboarded  and  continued  with  the  scheduled  work  without  further  incident.            

8/29/15 Outside  Crew CCCI Operator  Error

CCCI  -­‐  On  August  29,  2015  -­‐  Two  contract  workers  in  the  Montebello  District,  a  lineman  and  apprentice,  were  working  on  a  16kV  circuit  from  a  bucket  truck.  The  bucket  was  positioned  near  the  16kV  C/O  arm.  The  lineman  attempted  to  move  the  bucket  was  attempting  to  trigger  on  the  pistol  grip  trigger,  which  he  was  not  fully  depressing.  He  adjusted  his  grip  and  was  able  to  depress  the  trigger.  When  he  did  this  the  bucket  moved  abruptly  toward  the  arm  and  made  contact,  which  shook  the  pole.  This  caused  the  4kV  to  the  east  to  slap  together,  relaying  the  circuit.  The  crew  STOPPED,  re-­‐tailboarded  and  continued  with  the  scheduled  work  without  further  incident.    

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Body  Part  /    Root  Cause Description

8/31/15 Outside  Crew CCCI Cable  Marking

CCCI  -­‐  On  August  31,  2015  -­‐  A  contract  crew  in  the  Bishop  District  was  assigned  to  isolate  and  ground  CIC  cable  for  testing  by  a  second  contractor.  After  a  section  of  the  Underwood  12kV,  that  was  feeding  a  PMS  was  de-­‐energized,  two  contractor  linemen  were  dispatched  to  ground  and  isolate  the  cable  in  the  PMS.  The  two  linemen  failed  to  mark  the  cable  while  performing  this  task.  The  crew  was  then  assigned  to  verify  cable  at  a  BURD  switch  inside  a  structure.  The  second  contractor  crew  finished  testing  cable  from  the  PMS  to  the  BURD  switch,  and  one  of  their  linemen  was  assigned  to  install  the  removed  elbows  at  the  PMS.  When  he  arrived,  he  noticed  none  of  the  cables  were  marked,  so  the  original  crew  was  dispatched  to  verify  the  cable  positions.  The  original  crew  verified  the  cable  locations  and  installed  the  removed  elbows.  When  the  SCE  troubleman  attempted  to  re-­‐energize  the  Underwood  12kV,  the  circuit  relayed  and  locked  out.  After  the  SCE  TM  and  original  crew  investigated  the  situation,  it  was  determined  the  phases  were  crossed  in  the  PMS,  resulting  in  a  phase-­‐to-­‐phase  fault.  The  original  crew  rang  out  cable,  installed  new  transformer  bushings  and  installed  cable  on  the  correct  positions.  After  the  cable  was  reinstalled,  the  Underwood  12kV  was  energized  without  incident.    

8/31/15 Outside  Crew CCCI Cable  Marking

CCCI  -­‐  On  August  31,  2015  -­‐  Bishop  -­‐    A  contract  crew  was  assigned  to  isolate  and  ground  CIC  cable  for  testing  by  a  second  contractor.  After  a  section  of  the  Underwood  12kV,  that  was  feeding  a  PMS  was  de-­‐energized,  two  contractor  linemen  were  dispatched  to  ground  and  isolate  the  cable  in  the  PMS.  The  two  linemen  failed  to  mark  the  cable  while  performing  this  task.    The  crew  was  then  assigned  to  verify  cable  at  a  BURD  switch  inside  a  structure.  The  second  contractor  crew  finished  testing  cable  from  the  PMS  to  the  BURD  switch,  and  one  of  their  linemen  was  assigned  to  install  the  removed  elbows  at  the  PMS.  When  he  arrived,  he  noticed  none  of  the  cables  were  marked,    so  the  original  crew  was  dispatched  to  verify  the  cable  positions.  The  original  crew  verified  the  cable  locations  and  installed  the  removed  elbows.    When  the  SCE  troubleman  attempted  to  re-­‐energize  the  Underwood  12kV,  the  circuit  relayed  and  locked  out.      After  the  SCE  TM  and  original  crew  investigated  the  situation,  it  was  determined  the  phases  were  crossed  in  the  PMS,  resulting  in  a  phase-­‐to-­‐phase  fault.  The  original  crew  rang  out  cable,  installed  new  transformer  bushings  and  installed  cable  on  the  correct  positions.  After  the  cable  was  reinstalled,    the  Underwood  12kV  was  energized  without  incident.    No  injuries  were  reported.    

9/26/15 Outside  Crew CCCI Dig  In

CCCI  -­‐  On  September  26,  2015  -­‐  Palm  Springs  -­‐  The  contractor  crew's  scope  of  work  was  to  trench        out  of  an  existing  secondary  handhole  and  install  two  new  conduits  to  two  other  existing  handholes.        The  crew  foreman  excavated  out  of  an  existing  handhole,  operating  an  mini  excavator,  and  dug  into    a  primary  cable  causing  a  circuit  interruption  on  the  Pistola  12kV  out  of  Concho  Substation.                      

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Body  Part  /    Root  Cause Description

9/26/15 Outside  Crew CCCI Secondary  Marking

CCCI  -­‐  On  September  26,  2015  -­‐  Monrovia  -­‐  A  contractor  crew  was  tasked  with  replacing  a                transmission  pole.  The  pole  had  one  16kV  and  two  4kV    circuits.  The  pole  had  a  120/240  3  pot  bank  on  the  Highcliff  16kV.  Before  the  outage  started,  the  lineman  in  the  air  took  voltage,  rotation,  and  identified  the  208  leg  at  the  bank,  secondary  riser,  open  wire  secondary,  a  3  phase  service  to  the  west,    and  a  3  phase  secondary  to  the  east.  After  the  pole  and  bank  replacement  was  completed,  the  crew  restored  power.  Customers  then  reported  problems    about  their  lights  to  the  foreman.  The  foreman  then  took  voltage  at  a  panel  and  found  one  120  volt  was  heated  up  to  208  volts.  The  foreman  called  the  DOC    for  an  emergency  outage.  After  a  quick  investigation,  the  crew  found  they  had  mismarked  the  secondary's  to  the  pole  that  was  to  the  east.  The  contractor  had  an  electrician  on  site  assessing  the  customers.  Load  was  later  restored  later.  Initial  findings  for  damaged  customer  equipment  are  bad    ballasts  and  fans.      

9/29/15 Outside  Crew CCCI Dig  In

CCCI  -­‐  On  September  29,  2015  -­‐  Bishop  -­‐  A  contractor  crew  was  assigned  to  install  a  new  pole  approximately  10  feet  east  of  an  existing  dead-­‐end  pole.  The  crew  used  hand  tools  to  a  depth  of                  approximately  4.5  feet  and  did  not  see  any  underground  facilities.  They  elected  to  complete  the  hole  using  the  power  auger.  After  excavating  another  2  feet,  the  auger  struck  and  relayed  the  Underwood  12kV  circuit.    

10/9/15 Outside  Crew CCCIConductor  Control

CCCI  -­‐  On  October  9,  2015  -­‐  Valencia  -­‐    A  contractor  crew  was  tasked  to  replace  a  deteriorated  pole.  One  lineman  was  in  Bucket  1;    another  lineman  and  an  apprentice  were  in  Bucket  2.    The  crew  was  working  on  a  three-­‐phase  2/0  copper  double  dead-­‐end  with  a  336  double  dead-­‐end  neutral  on  10-­‐foot  cross  arms.  The  neutral  was  4  feet  below  the  phases  on  its  own  cross  arm.    The  crew  had  all  the  phases  transferred  and  double  dead-­‐ended  to  the  new  pole.  The  crew  was  in  the  process  of  moving  the  neutral  to  the  new  pole.  The  neutral  was  jumpered  out  and  a  hot  hoist  was  across  the  neutral.  The  men  in  Bucket  2  had  the  mac  and  hoist  secured  in  the  bucket's  jib.  They  were  moving  the  neutral  up  into  position  on  the  new  cross  arm.    In  the  process  of  doing  this,  the  operator  of  the  bucket  truck  that  was  moving  the  wire  did  not  move  the  wire  smoothly  and  caused  a  wave  in  the  wire.    This  combined  with  the  high  winds  caused  the  neutral  to  come  into  contact  with  the  outside  phase.  The    crew  foreman  was  watching  the  span  to  the  south,  and  the  lineman  in  Bucket  1  was  watching  the  span  to  the  north  when  the  incident  happened.      After  the  incident,  the  crew  foreman  checked  to  make  sure  the  men  in  the  air  were  OK  and  then  went  down  the  span  to  check  where  the  contact  happened.  The  Vincent  Substation  operator  called  the  crew  foreman  when  he  was  checking  the  span.  Everything  looked  OK    so  the  foreman  released  his  No  Test  orders  and  had  his  men  get  in  the  clear  before  giving  dispatch  permission  to  close  the  circuit  back  in.  The  circuit  went  back  in  without  a  problem.  The  crew  foreman  then  immediately  notified  his  general  foreman.      No  injuries  were  reported.

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Body  Part  /    Root  Cause Description

10/17/15 Outside  Crew CCCI Conductor  Control

CCCI  -­‐  On  October  17,  2015  -­‐  Thousand  Oaks  -­‐    A  distribution  contractor  crew  was  tasked  with                replacing  a  deteriorated  tangent  pole  in  Malibu  on  the  Galahad  16kV.  In  the  process,  the  crew  had  to  replace  some  automatics  on  #6  solid  copper  wire.    After  they  replaced  all  the  automatics  with                    compression  sleeves  ,  the  crew  went  to  working  on    the  pole  replacement  where  the  pole  was  going  from  a    40  foot  pole  to  a  45  foot  pole.  In  the  process  of    transferring  the  phases  to  the  new  pole,  the  center  phase  came  apart  mid  span,  going  to  the  ground  which  in  turn  opened  the  RAR  (0650).  As  a  result,  there    was  an  unplanned  outage  on  the  tap  line  they  were  working  on.  No  one  was  injured  and  they  called  the  switching  center  and  the  troubleman  to  let  them  know  of  the  situation.                                                                      The  foreman  took  the  wire  off  the  metal  fence  with  a  shotgun  stick.  He  then  contacted  the  substation  and  contractor  general  foreman.  The  crew  was  on  standby  until  the  SCE  troubleman  arrived.  The  troubleman  took  a  clearance  on  the  line  and  directed  the  crew  to  repair  the  wire.  The  crew  then  tested  and  grounded  the  line,  installed  new  compression    sleeves,  using  MD-­‐6  tool  with  161  dies.  The  crew  then  completed  transfer  of  wire  to  the  new  pole  and  contacted  the  troubleman,  gaining  permission  to  re-­‐energize  the  Galahad  16kV  circuit.      No  injuries  were  reported.              

10/18/15 Outside  Crew CCCIConductor  Control

CCCI  -­‐  On  September  18,  2015  -­‐  Santa  Barbara  -­‐  A  contract  crew  was  tasked  to  replace  a  deteriorated  pole  in  the  Santa  Barbara  District.  The  crew  had  completed  all  primary  work  and  was  in  the  process  of  transferring  a  span  guy.  The  span  guy  went  from  the  phone  level  of  the  pole  the  crew  was  replacing  to  an  angled  pole  between  the  V-­‐brace  and  the  primary  arm.    The  span  guy  was  existing  and  is  unnecessary  in  the  construction  of  the  pole  on  either  side.  The  primary  did  not  follow  the  span  guy;  it  went  to  a  line  and  buck  first,  and  then  the  buck  fed  that  angle  pole.      The  secondary  triplex  did  follow  from  the  crew's  pole  to  the  angle  pole.    In  the  process  of  transferring  the  span  guy  the    foreman  and  crew  heard  the  unmistakable  noise  of  a  phase-­‐to-­‐phase  or  phase-­‐to-­‐ground  contact.  They  were    not  sure  what  had  happened.  The  foreman  received  a  call  from  the  Sub  to  see  if  everything  was  OK  and  he  replied  "yes,"  but  was  unclear  of  what  had  happened.    They  knew  that  the  span  guy  passed  under  the  primary  wire  at  the  angle  pole  and  figured  it  had  to  have  made  contact  there,  since  it  is  the  only  place  where  the  span  guy  is  near  the  conductor.    The  crew  immediately  stopped  what  they  were  doing  and  went  down  to  this  angle  pole  to  investigate  what  had  caused  the  unplanned  outage.  They  knew  it  was  a  phase-­‐to-­‐ground  contact  because  the  troubleman  said  it  would  most  likely  be.  This  was  due  to  the  fact  that  the  RAR  0611  had  operated.  The  crew  was  working  behind  Branch  Line  Fusing,  which  was  in  front  of  the  Automatic  Re-­‐closure,  and  if  it  had  been  a  phase-­‐to-­‐phase  contact,  it  would  have  opened  the    Branch  Line  Fusing  not  the  RAR.    During  the  investigation  the  crew  found  that  the  field  side  phase  on  the  angle  pole  already  had  an  armor  rod  installed  because  of  previous  contact  with  the  span  guy.  The  crew  found  a  contact  mark  on  the  span  guy  and  armor  rod.  Further  investigation  revealed  a  contact  mark  on  the  triplex  and  the  span    guy.  The  span  guy  was  not  backing  up  anything  and  is  unnecessary.  It  also  had  excessive  slack  in  it  because  it  was  not  under  strain.  There  appeared  to  be  2-­‐  to  3-­‐foot  gap  between  the  span  guy  and  the  primary.  When  the  lineman  came  up  on  the  span  guy  to  transfer  it  to  the  new  pole  it  made  contact  with  the  primary  at  the  angle  pole  and  with  the  secondary  about  mid-­‐span.  This  was  due  to  the  span  guy  going    from  the  phone  level  at  the  pole  the  crew  changed  to  the  primary  level  at  the  angle  pole.        

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/4/15 Outside  Crew CCCI Conductor  Control

CCCI  -­‐  On  November  4,  2015  -­‐  Santa  Barbara  -­‐  A  contract  crew  was  tasked  with  extending  a  no  access  secondary  riser  while  the  transformer  stayed  hot.  The  secondary  leads  were  approximately  12  feet  from  the  existing  riser  and  the  other  house’s  service.  The  leads  were  temporary.  After  the  crew  disconnected  one  lead  from  the  secondary  riser  and  removed  the  connector,  the  hot  leg  and  neutral  made  contact,  causing  the  BLF49304  to  open  up.  Crew  called  the  DOC  and  switching  center,  and  asked  for  a  troubleman  to  be  dispatched  to  their  location.  The  crew  also  called  their  foreman  and  project  general  supervisor.  The  8  amp  transformer  did  not  blow,  but  the  25  amp  SMUS  branch  line  fuse  did,  taking  out  2  transformers  and  5  customers.  The  troubleman  arrived  and  closed  fuses  back  in,  for  a  total  outage  time  of  30  minutes.  The  troubleman  said  the  fusing  scheme  in  the  area  is  wrong  and    would  write  up  an  R/O  to  have  it  fixed.    

11/6/15 Outside  Crew CCCI Observation

CCCI  -­‐  On  November  6,  2015  -­‐  Montebello  -­‐  A  contractor  crew  was  tasked  to  replace  a  pole.  The  pole  had  one  transmission  circuit,  a  16kV  circuit  on  alley  arms,  and  two  4kV  circuits  on  alley  arms.  The  pole  also  had  open  wire  secondary’s  on  the  alley  arms.  The  crew  had  an  outage  on  all  three  circuits  and  a  outage  on  the  transformer  that  fed  the  secondary's  to  the  pole  being  replaced.  As  the  lineman  in  the  bucket  was  removing  some  alley  arms  from  the  old  pole,  he  snagged  one  of  the  wires  from  the  secondary's  on  the  Lineman  Bucket  Rescue  device  that  is  mounted  on  the  boom  of  the  bucket.  As  he  was  exiting  the  work  location  the  wire  was  pulled  with  the  bucket  and  then  it  came  off  shaking  the  wires  to  the  west  of  the  work  location.  On  the  pole  to  the  west  the  open  wire  secondary's  was  energized  the  other  side  of  the  double  alley  arms.    Within  the  energized  span  of  open  wire  there    was  a  wizzer  service  that  had  taps  to  the  open    wire  secondary's.  With  the  shock  of  the  wire    from  coming  off  the  bucket,  the  wizzer  taps  got  together  and  the  neutral  opened  up.  The  foreman  called  the  DOC  for  a  emergency  outage    on  the  transformer  and  made  repairs.  No  injuries  or  damage  was  reported.      

11/9/15 Outside  Crew CCCITraffic  Control/  Observation

CCCI  -­‐  On  November  9,  2015  -­‐  Ontario  -­‐  A  contractor  crew  was  tasked  to  replace  a  deteriorated  pole  in  Ontario.  The  crew  had  suspended  the  existing  omni-­‐rupter  switch  to  the  jib  on  the  material  handler  bucket  and  topped  the  pole.  After  3  to  4  hours  of  work,  a  large  truck  passed  under  the  phone/com  line  that  is  connected  to  the  existing  pole  and  snagged  it.  This  caused  a  phase  and  a  neutral  make  contact,  resulting  in  the  Creekside  12kV  to  lock  out.    No  injuries  were  reported.                                                                                                                                                                                                          

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/10/15 Outside  Crew CCCIInadequate  Attention/    Process

 CCCI  -­‐  On  November  10,  2015  -­‐  San  Joaquin  -­‐  At  approximately  11:56  p.m.,  a  contractor  crew  had  completed  changing  out  a  deteriorated  pole  with  a  new  pole  that  had  an  omni-­‐switch,  and  was  in  the  process  of  removing  the    deteriorated  pole  top.  They  had  grabbed  the  pole  top  with  the  jib  on  the  bucket  truck  and  connected  the  winch  line  to  the  pole.  A  lineman  was  below  in  a  squirt  bucket  and  was  making  the  cut.  As  the  lineman  was  cutting  the  pole  top,  the  saw  got  caught  in  a  bind  and  the  lineman  in  the  bucket  truck  rotated  the  boom  to  free  up  the  saw.  As  he  did  this,  the  pole  top/bucket  had  too  much  tension  on  it,  causing  it  to  jump  up.  As  it  broke  free,  the  top  of  the  pole  contacted  the  center  phase  and  the  road  phase.  The  result  was  the  circuit  being  interrupted  with  no  injuries.  The  crew  stopped  work  immediately,  making  sure  that  everyone  was  OK  and  then  contacted  Rector  Substation,  the  SCE  Troubleman,  and  ACC  Supervisors.      No  injuries  were  reported.

11/11/15 Outside  Crew CCCI Improper  Transformer

CCCI  -­‐  On  November  11,  2015  -­‐    Ontario  -­‐  Contract  crews  had  a  mainline  clearance  to  replace  old  4  wire  primary  and  install  new  336AK.  When  new  primary  was  in  and  energized,  the  crew  was  in  the  process  of  picking  up  load.  When  energizing  480V  bank,  a    "firecracker"  tool  was  not  installed  at  the    panel,  causing  the  meter  to  burn  up.  The  panel  was  servicing  a  nursery  and  small  trailer.    Crew  notified  the  SCE  PGS,  contacted  an  electrician  and  hooked  up  a  temporary    generator  to  provide  the  customer  with  temporary  power.      No  injuries  were  reported.

11/11/15 Outside  Crew CCCI Soil  Conditions

CCCI  -­‐  On  November  11,  2015  -­‐  San  Joaquin  -­‐  A  contract  crew  was  assigned  to  replace  a  70    foot  pole  with  an  80  foot  pole.  There  was  one  69kV  circuit  and  two  12kV  circuits  on  the  old  pole,  with  a  primary  riser.  The  circuit  in  the  riser  was  de-­‐energized.  When  the  hole  was  at  the  required  10  foot  depth,  the  soft  dirt  sloughed  off  and  allowed  the  existing  pole,      which  was  set  at  a  depth  of  8  to  8.5  feet,  to  fall  into  the  new  hole  and  slip  to  the  side  a  few  inches,  causing  very  slight  damage  to  the  insulation  on  the  cable  and  the  PVC  riser  to  separate  at  a  point  approximately  2  feet  above  ground  level.  There  was  no  interruption  of    power.  The  crew  stabilized  the  butt  of  the  pole,  and  made  sure  the  12kV  cable  in  the  riser  was  still  operational.  Although  the  cable  was  in-­‐tact  with  only  a  small  cut  in  the  insulation,  the  crew  decided  to  install  a    temporary  splice  and  schedule  time  to  return  and  make  permanent  repairs.    When  digging  adjacent  to  an  existing  pole,  and  soil  conditions  are  such  that  there  is  a  risk  of  the  pole  shifting,  measures    should  be  taken  to  stabilize  the  pole    during  the  excavation.  In  this  instance,    there  were  no  indications  that  soil  conditions  were  not  stable.        No  injuries  were  reported.      

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/11/15 Outside  Crew CCCI Improper  Splice

CCCI  -­‐  On  November  11,  2015  -­‐  Covina  -­‐  A  contract  crew  was  tasked  with  replacing  a  75  foot  transmission  pole.  The  transmission  was  constructed  with  vertical  arms  and  the  Bender  12kV  was  double  dead-­‐ended  opposite  the  transmission.  The  pole  also  had  the  Jarvis  12kV  as  under  build  in  horizontal  construction.  The  crew  had  a  switching  program  on  both  the  Bender  12kV  and  the  Jarvis  12kV.    To  accomplish  the  switching  program  and  take  a  clearance,  the  switching  program  called  out  to  install  mid-­‐span  isolators  on  the  Bender  12kV,  one  span  to  the  East  at  another  pole.  The  work  order  map  identified  the  wire  size  as  4/O  copper  on  the  Bender  12kV.  The  pole  was  replaced  and  after  the  crew  completed  their  work,  they  began  to  switch  back  both  circuits.    The  crew  closed  in  the  mid-­‐span  isolators  on  the  Bender  12kV  by  installing  a  4/O  splice  in  each  of  the  top  two  phases  and  a  2/O  splice  in  the  bottom  phase.  All  load  was  restored.  About  an  hour  later  the  top  two  phases  pulled  out  of  the  splices  and  fell  into  the  Jarvis  12kV,    locking  out  both  circuits.  The  contractor  dispatched  a  crew  to  make  repairs  and  all  load  was  restored  on  both  circuits  later  that  evening.  No  injuries  were  reported.

11/29/15 Outside  Crew CCCIConductor  

Control/Strain

CCCI  -­‐  On  November  29,  2015  -­‐  Monrovia  -­‐  A  subcontract  crew  was  tasked  with  replacing  a  triple-­‐circuit  pole.  The  crew  installed  isolators  on  the  Laporte  16kV  line  one  span  to  the  west  of  their  work  location.  Prior  to  installing  grounds,  the  crew  performed  a  visual  inspection  of  the  cross  arm,  then  proceeded  the  install.  The  crew  was  issued  clearance  and  began  their  pole  change  out.  The  pole  was  replaced  without  issues.  At  approximately  11:15  a.m.,  the  crew  heard  a  noise  and  saw  that  the  cross  arm  one  span  to  the  west  had  broken  on  the  back  side  of  their  grounds  and  isolators.  The  broken  arm  brought  the  Laporte  16kV  down  into  the  underbuild  Rowland  4kV,  causing  both  circuits  to  lock  out.    No  injuries  were  reported.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

2/18/15 Outside  CrewPotential  Significant  Incident

 Load  Securement

Potential  Significant  Accident  -­‐  On  February  18  2015;  A  Contractor  flatbed  truck  was  transporting  partially  empty  wire  reels  from  Gould  Substation  Yard  to  the  Vincent  Material  Yard.  On  Angeles  Forest  Highway  mile  marker  18.0  one  of  the  wire  reels  slid  sideways  on  the  steel  bed  and  partially  fell  off  the  truck.  The  driver  was  able  to  pull  over  at  a  safe  place  off  the  highway.  A  transport  truck  delivered  a  forklift  from  Vincent  to  assist  in  loading  the  wire  reels  back  on  the  flatbed  truck.  While  repositioning  the  wire  reels,  one  of  the  reels  slid  off  the  truck  into  traffic  lanes.  Fortunately  a  chain  was  attached  to  the  reel  and  stopped  it  before  it  rolled  into  oncoming  traffic.  The  reels  had  not  been  rigged  correctly,  which  caused  the  center  reel  to  slide  sideways  off  the  truck.

5/12/15 Outside  Crew Dig  in Mismarked  Utility  Service

Gas  Dig  in  -­‐  on  May  12-­‐2015  -­‐  Ontario  District  -­‐  A  contractor  crew  was  assigned  to  remove  and  replace  a  deteriorated  pole  on  the  Texfi  12kV  circuit.  All  USA  marks  were  noted  and  remarked  as  needed  to  avoid  any  damage  to  existing  utilities.  As  the  crew  was  installing  a  new  screw  anchor,  they  struck  and  damaged  a  mismarked  gas  service  line.  The  foreman  immediately  called  the  gas  company,  which  responded  and  dispatched  a  crew  to  the  location  to  make  repairs.  When  the  gas  company  crew  arrived,  they  determined  the  line  was  a  stub  that  was  active  but  not  in  use  and  made  the  repairs.      Per  underground  construction  requirements,  you  must  hand  expose,  to  the  point  of  no  conflict,  24  inches  on  either  side  of  the  underground  facility  so  you  know  its  exact  location  before  using  power  equipment  

6/8/15 Outside  Crew Vehicle  Incident Operator  Error

Property  Damage  on  June  8,  2015  -­‐  A  Contractor  on  the  Chino  Underground  Project  was  driving  a  forklift  from  Vault  Cluster  12  to  VC  11  on  public  roads.  The  driver  of  the  forklift  was  making  a  right  turn  from  Morning  field  Dr.  onto  Lost  Trail  and  struck  a  third-­‐party  vehicle  on  the  left  rear  quarter  panel  with  the  right  front  tire  of  the  fork  lift.  The  third-­‐party  vehicle  was  parked  on  the  correct  street  side.  It  was  towed  to  an  unknown  facility  and  a  police  report  was  made.

6/19/15 Outside  Crew Close  Call Operator  Error

Close  Call  –  on  June  19,  2015  -­‐  A  contractor  crew  was  tasked  with  unloading  36-­‐inch  casing  from|  a  flatbed  trailer.  An  operator  was  using  a  forklift  to  unload  the  third  piece  of  36-­‐inch  casing  from  the  top  of  the  stack  on  the  trailer.  There  were  two  spotters  keeping  the  area  clear  for  the  pick  when  the  casing  fell  from  the  top  of  the  trailer  to  the  opposite  side  of  the  forklift.  No  injuries.

6/23/15 Groundman Strain Tool  Positioning

Sprain  –  on  June  23,  2015  -­‐  A  groundman  working  on  a  contractor  crew  on  the  Chino  Hills  Underground  Project  was  carrying  a  shoring  jack  and  had  it  resting  on  his  shoulder.  When  he  set  one  end  of  the  shoring  jack  down  on  the  ground,  the  other  end  was  still  on  his  shoulder.  The  shoring  jack  is  about  6  feet  long  and  weighs  approximately  45  pounds.  The  weight  of  the  jack  and  its  position  caused  a  strain/sprain  to  the  groundman's  right  shoulder.  The  groundman  notified  his  supervisor.  The  groundman  was  treated  on  site  and  released  back  to  work.

Contractor  Other  Incidents

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

6/23/15 Outside  CrewProperty  Damage

Improper  Work  Method

Property  Damage  –  on  June  23,  2015  -­‐  A  contractor  journeyman-­‐lineman  in  the  San  Joaquin  District  was  lowering  idle  lashed  copper  cable  and  messenger  from  bucket  truck  using  a  hand  line  and  grip  down  to  the  groundman.  The  grip  slipped  from  the  messenger,  causing  the  cable  to  strike  the  front  windshield  of  contractor's  boom  truck.  The  front  windshield  cracked  and  shattered.  

6/30/15 Outside  Crew Property  Damage

Rope  Failure

Property  Damage  -­‐  June  30,  2015  –  A  contractor  crew  in  the  Santa  Ana  District  was  in  the  process  of  removing  failed  200  amp  cable.  The  crew  proceeded  to  pull  the  cable  out  of  the  transformer  using  the  line  truck  as  an  anchor  and  a  snatch  block  attached  the  rear  of  the  line  truck.  They  wove  the  cable  through  the  block  and  attached  it  to  a  pickup  truck.  The  snatch  block  attached  to  the  line  truck  was  rigged  using  1/2-­‐inch  poly  rope.  As  the  pickup  truck  was  taking  up  the  cable  and  slowly  driving  down  the  street,  the  rope  failed  and  shattered.  As  a  result  of  the  rope  failure,  the  snatch  block  launched  in  the  air  and  smashed  into  the  roof  of  a  nearby  house  170  feet  away.  The  block  then  ricocheted  to  the  next  house.  Damage  to  both  rooftops  was  significant.  No  injuries  were  reported.    

7/9/15 Outside  Crew Injury AnkleInjury  -­‐  On  July  9,  2015  -­‐  Monterey  -­‐  Climbing  down  bucket  truck,  misjudged  elevation  due  to  outriggers,  turned  left  ankle.  Examined  at  clinic,  PT  ordered  and  placed  on  light  duty.

7/29/15 Outside  Crew Insect  Bite Bee  Sting

Insect  Bite  -­‐  July  29,  2015  –  A  contractor  crew  in  the  Ontario  District  began  trenching  by  hand  in  theshrubs  behind  curb  when  the  crew  encountered  a  beehive.  One  of  the  workers  was  stung  by  a  bee  on  the  right  side  of  his  neck.  He  experienced  no  reaction  to  the  sting  at  that  time.  The  crew  foreman  immediately  removed  crew  from  the  work  area  and  notified  the  SCE  representative.  The  work  site  was  shut  down  until  the  bees  were  removed.

8/2/15 Outside  Crew Significant  Injury Loss  of  Control

Significant  Injury  August  2,  2015  –  A  contractor  crew  in  the  Ontario  District  was  in  the  process  of  extending  the  Kelly  bar  on  the  Auger  to  lengthen  and  gain  more  depth.  As  the  employee  went  to  tighten  the  bolt,  he  bobbled  the  wrench,  and  the  weight  of  the  wrench  fell  into  his  teeth,  chipping  the  two  front  teeth.  The  crew  notified  the  SCE  representative.  The  injured  worker  was  taken  to  the  dentist  to  be  evaluated.

8/2/15 Outside  Crew Injury Chipped  Tooth Significant  Injury  -­‐  on  August  2,  2015  –  Ontario  -­‐  Employee  tightening  bolt  with  wrench,  it  slipped  and  struck  mouth/2  front  teeth,  causing  teeth  to  chip.  Dental  work  only,  returned  to  work.

8/4/15 Outside  Crew Significant  Injury Conductor  Break

Significant  Injury  August  4,  2015  –  A  contractor  crew  in  the  Valencia  District  was  pulling  out  copper  conductor  and  pulling  in  rope  from  one  tubular  steel  pole  (TSP)  to  another.  Toward  the  end  of  the  pull,  the  line  had  an  old  section  that  had  copper  splices  and  preforms  in  it.  When  the  spliced  section  came  through  the  guide  on  the  puller,  the  wire  broke.  The  rope  held  at  the  second  TSP.  No  injuries  or  damage  was  reported.  The  wire  did  fall  to  the  ground.  The  crew  inspected  the  wire  and  discovered  that  the  wire  ends  were  oxidized,  and  that  wire  had  been  broken.

8/9/15 Outside  Crew Injury FallInjury  -­‐  On  August  9,  2015  -­‐  Monrovia  -­‐  Climbing  up  to  boom  of  digger  truck,  stepped  on  steel  bar  which  gave  way  and  broke,  causing  employee  to  fall  from  truck,  approx.  8ft  to  ground.  Examined  at  clinic,  placed  on  mod  duty.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

8/22/15 ApprenticeProperty  

Damage/Close  Call

Vehicle

Property  Damage  August  22,  2015  -­‐  While  driving  a  digger  derrick  an  Apprentice  Lineman  working  in  the  Whittier  District  felt  a  jolt  and  noticed  his  pole  trailer  had  become  disconnected  from  the  power  unit.  The  pole  trailer  contained  cut  sections  of  pole  and  was  not  extended  at  the  time  of  the  event.  The  trailer  came  to  rest  in  the  side  lawn  of  a  commercial  business.  The  event  caused  damage  to  a  gas  meter  located  in  the  property.  There  were  no  injuries  associated  with  this  event.            

8/25/15 Outside  Crew Property  Damage

Phone  Cable

Property  Damage  August  25,  2015  -­‐  A  contractor  crew  in  the  San  Joaquin  District  was  assigned  to  continue  working  on  the  Caribbean  12kV  project.  A  tailboard  was  given|  so  that  all  crew  members  understood  the  task,  hazards,  and  the  methods  to  mitigate  any  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  and  the  public.  While  the  crew  was  excavating  with  a  backhoe  the  operator  damaged  a  marked  Verizon  phone  cable.  The  crew  foreman  notified  Dig-­‐Alert  of  the  damage  and  Dig-­‐Alert  dispatched  a  Verizon  repair  crew  to  respond  and  make  the  necessary  repairs.  After  the  repairs  were  made  the  crew  finished  the  day  without  any  further  incidents.                                                                

8/26/15 Outside  CrewProperty  Damage No  Observation

Property  Damage  -­‐  On  August  26,  2015  -­‐  A  contractor  crew  in  the  Redlands  District  was  assigned  to  work  on  an  M&M  project  on  the  Urbita  12kV  circuit.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards,  and  methods  to  mitigate  any  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  and  the  public.  While  the  crew  was  excavating  with  a  backhoe  the  operator  hit  and  damaged  an  unmarked  1-­‐inch  plastic  water  service  stub.  The  crew  foreman  notified  Dig-­‐Alert  and  Dig-­‐Alert  dispatched  a  repair  crew  from  the  City  of  Grand  Terrace  Water  District  to  respond  and  make  the  necessary  repairs.  After  the  repairs  were  made  the  crew  finished  the  day  without  any  further  incidents

8/27/15 Outside  Crew Close  Call Cable  Marking

Close  Call  -­‐  On  August  27,  2015  -­‐  A  contract  crew  in  the  Ontario  District  was  removing  control  cable.  They  tested  all  the  wire  before  removing  or  cutting  cable.  The  crew  was  in  the  cable  trench  removing  green-­‐taped  wire.  They  cut  off  the  carrots  were  they  could  test  the  wires  and  the  cable  arced.  The  crew  followed  the  cable  without  cutting  it  and  found  that  it  was  still  landed  on  the  AC  cabinet.  The  crew  disconnected  and  removed  the  cable.  The  cable  the  crew  cut  was  green-­‐taped,  indicating  the  cable  had  already  been  tested  dead  by  another  party.  Since  the  other  end  of  the  cable  was  still  connected  to  the  A04  AC  panel,  the  cable  should  have  been  wrapped  in  both  red  and  green  tape.    

8/27/15 Outside  Crew Close  CallConductor  Control

Close  Call  -­‐  On  August  27,  2018  -­‐  A  crew  set  up  a  bucket  at  a  TSP  tower  in  the  Whitter  District.  The  crewmembers  tested  and  ground  the  Sunshine  66kV  circuit.  They  broke  the  dead-­‐end  on  the  Sunshine  66kV  and  released  the  wire  from  the  existing  structure  and  let  all  three  phases  float.  The  arms  were  installed  and  the  crew  began  transferring  the  wire.  A  splice  sleeve  located  in  an  inaccessible  location  failed  and  the  wire  separated.  No  injuries  or  damages  were  reported.  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

8/30/15 Outside  Crew Injury HeatInjury  -­‐  On  August  30,  2015  -­‐  El  Monte  -­‐  Working  under  hot  conditions,  experienced  nausea  and  vomiting.  Taken  to  local  hospital,  IV  fluids  kept  overnight  for  observation.

9/2/15 Outside  Crew Close  Call Switching

Close  Call  -­‐  On  September  2,  2015  -­‐  Wildomar  -­‐  A  contractor  crew  was  in  the  process  of  testing  the      line  de-­‐energized  after  the  troublemen  (TM)    completed  their  switching  on  the  Babylon  12kV.  The      TM's  switching  procedure  consisted  of  clearing  a  section  of  the  Babylon  12kV  from  PS1649  to  open          position  2  of  PME  5182  to  replace  a  riser  pole.  The  contractor  crew  tested  the  line  to  validate  the  line  was  de-­‐energized  but  instead  found  the  line  to  still  be  energized.  At  this  time  the  crew  stopped  their  work  and  informed  the  substation  operator  and  the  troublemen  of  the  situation.  The  TM  checked  PME  5182,  and  found  that  position  2  of  the  switch  blades  were  closed;  however,  the  switch  position  indicator  showed  closed.  Earlier  when  the  TMs  were  switching  the  line  de-­‐energized,  the  TM  verified  the  switch  blades  were  open  and  the  indicator  showed  open.  A  note  was  placed  on  OMS  not  to  operate  this  switch,  which  is  being  scheduled  for  replacement.

9/12/15 Outside  LinemanMedical  Condition Diabetic  Shock

Medical  Condition  -­‐  On  September  12,  2015  -­‐  Covina  -­‐  A  contractor  lineman  went  into  diabetic  shock  while  on  a  job  site.  Another  lineman  on  the  crew  administered  medication  by  syringe,  which  the  two  linemen  had  discussed  previously  if  such  an  incident  occurred.  Afterward,  the  worker  was  transported  to  a  nearby  hospital  where  he  was  treated  and  released  after  two  hours.    

9/18/15 Outside  Crew Vehicle  Accident Civilian  Collision

Vehicle  Accident  -­‐  On  September  18,  2015  -­‐  Yucca  Valley  -­‐    A  contractor  crew  was  trailering  two  45  foot  poles  to  a  job  site.  At  approximately  7:30  a.m.,  a    privately  owned  flat-­‐bed  pick-­‐up  truck,  traveling  at  a  high  rate  of  speed,  ran  into  the  butt  end  of  the  poles,  resulting  in  substantial  damage  to  the  private  vehicle  and  damage  to  the  contractor's  trailer  and  truck.  There  were  no  injuries.                      California  Highway  Patrol  officers  on  the  scene  determined  fault  to  be  with  the  driver  of  the              flatbed  pick-­‐up.                                                                          

9/18/15 Outside  Lineman Injury Chipped  Tooth

Injury  -­‐  On  September  18,  2015  -­‐  Valencia  -­‐  A  contractor  lineman  was  inside  a  bucket  positioned  on  the  ground.  The  employee  was  moving  the  job  to  pick  up  a  load.  As  the  jib  swung,  the  hook  on  the  jib  struck  the  employee  in  the  mouth,  chipping  his  front  tooth.  Crew  supervision  was  immediately  notified.  The  crew  stopped  worked,  examined  the  employee  and  sent  him  back  to  the  yard,  so  he  could  leave  to  see  the  dentist  for  an  evaluation.                  

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

10/8/15 Outside  Crew Operator  ErrorLoad  

Securement

Operator  Error  -­‐  On  October  8,  2015  -­‐  Palm  Springs  -­‐  A  contractor  crew  was  assigned  to  continue  working    on  the  Las  Palmas  4kV  project.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards,  and  the  methods  to  mitigate  hazards.  All    USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as    to  protect  the  crew  as  well  as  the  public.  While  the  crew  was  excavating  with  a  backhoe,  they  came  across  a  large  boulder  in  their  trench  line  that  needed  to  be  removed.  While  the  operator  was  attempting  to    remove  the  boulder  with  the  backhoe,  it  slipped  out    of  the  backhoe’s  bucket  and  fell  onto  an  already    exposed  and  located  CATV  conduit,  damaging  it  and  the  cable  inside.    The  crew  foreman  notified  Dig  Alert  of  the  damage,  and  Dig-­‐Alert  dispatched  a  Time  Warner  Cable  repair  crew  to  respond  and  make  the  necessary  repairs.    After  the  boulder  was  removed  and  repairs  were  made  the  crew  finished  the  day  without  any  further  incidents.  

10/14/15 Outside  Crew Vehicle  Incident Civilian  Collision

Vehicle  Incident  -­‐  On  October  14,  2015  -­‐  Covina  -­‐  A  contractor  hole-­‐digging  crew  was  traveling                  northbound  on  the  71  freeway  when  they  encountered  traffic.  The  contractor  vehicle  was  slowing  for  traffic  when  they  were  rear-­‐ended  by  a  car.  The  car  hit  an  air  compressor  that  the  truck  was  towing.  No  injuries  were  reported.  At  the  time  of  this  report  the  car  that  rear-­‐ended  the  air  compressor  has  been  taken  away  by  a  tow  truck  and  the  people  have  left  the  scene.  The  crew  secured  the  accident  area,  exchanged  information,  and  called  California  Highway  Patrol.  

10/17/15 Outside  Crew Dig  in Phone  Cable

Dig  in  -­‐  On  October  17,  2015  -­‐  Foothill  -­‐  A  contractor  crew  was  assigned  to  work  on  an  M&M  project  in  Bloomington  on  the  Flatcar  12kV  circuit.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards,  and  the  methods  to  mitigate  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  as  well  as  the  public.  As  the  crew  was  digging  around  a  BURD  structure  to  facilitate  its  replacement,  they  unknowingly  damaged  a  phone  service  cable.  The  SCE    inspector  was  later  made  aware  of  the  damage,  and  notified  the  foreman  on  October  17.    The  foreman  notified  AT&T  of  the  damage  and  had  the  contractor  crew  excavate  to  allow  the  AT&T  crew  to  make  the  necessary  repairs.  The  AT&T  crew  made  the  required  repairs  and  the  contractor  had  no  further  incidents.                                                                                        

10/19/15 Outside  Crew Dig  in Secondary  Cable

Dig  in  -­‐  On  October  19,  2015  -­‐  Redlands  -­‐  A  contractor  crew  was  assigned  to  pre-­‐dig  a  BURD  structure  on  the  Irvington  12kV  in  San  Bernardino.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards,  and  the  methods  to  mitigate  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the    existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  as  well  as  the  public.  While  the  crew  was  pre-­‐digging  the  BURD  enclosure,  using  shovels,  one  of  the  crew  members  inadvertently  struck  and  damaged  a  direct  buried  SCE  secondary  cable.  The  foreman  called  the  SCE  emergency  number  to  have  an  SCE  repair  crew  respond  and  perform  the  necessary  repairs.  A  short  time  later,  an  SCE  troubleman  responded,  made  the  necessary  repairs  and  the  contractor  crew  finished  the  day  without  any  further  incidents.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

10/20/15 Outside  Crew Dig  in Gas  Line

Dig  in  -­‐  On  October  20,  2015  -­‐  Palm  Springs  -­‐  A  contractor  crew  was  assigned  to  work  on  an  M&M            project  in  Indian  Wells  on  the  Ton  12kV  circuit.  A    tailboard  was  given  so  that  all  crew  members                  understood  the  task,  hazards,  and  the  methods  to  mitigate  hazards.  All  USA  marks  were  noted  and            re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  as    well  as  the  public.  While  the  crew  was  pot  holing  to  verify  the  exact  location  of  a  marked  half-­‐inch  plastic  gas  service  belonging  to  SoCalGas,  they  inadvertently  damaged  it  with  a  shovel.      The  foreman  notified  Dig-­‐Alert  of  the  damage  and          Dig-­‐Alert  dispatched  a  repair  crew  from  SoCalGas  to  respond  and  make  the  necessary  repairs.  After  the  repairs  were  made  the  crew  finished  the  day  without  any  further  incidents.  

10/26/15 Outside  Crew Dig  in Mismarked  Utility  Service

Dig  In  -­‐  On  October  26,  2015  -­‐  Foothill  -­‐    A  contractor  crew  was  assigned  to  work  on  an  M&M  project  on  the  Citrow  12kV  circuit  in  Fontana.  A    tailboard  was  given  so  that  all  crew  members                  understood  the  task,  hazards,  and  the  methods  to  mitigate  hazards.  All  USA  marks  were  noted  and          re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  as    well  as  the  public.  While  the  crew  was  digging  an  anchor  hole  for  an  SCE  crew,  using  a  backhoe,  the    operator  struck  and  damaged  an  unmarked  cable.    The  foreman  notified  Dig-­‐Alert  and  Dig-­‐Alert  dispatched  a  “Time  Warner  Cable”  repair  crew  to  respond  and  make  the  necessary  repairs.  After  the  repairs  were  made,  the  crew  finished  the  day  without  any  further  incidents.      

10/27/15 Outside  Crew Vehicle  Accident No  Observation

Vehicle  Accident  on  October  27,  2015  -­‐  Montebello  -­‐  A  contractor  crew  was  performing  work.    Traffic  control  was  moving  traffic  over  to  the  left.    A  backhoe  operator  went  to  pick  up  dirt  and  had  the  back  of  the  backhoe  in  traffic.    A  flagger  was  being  used,  but  he  let  traffic  go  and  the  backhoe  was  hit.

11/2/15 Outside  Crew Vehicle  Accident Civilian  Collision

Vehicle  Accident  on  November  2,  2015  -­‐  A  contractor  crew  was  in  a  digger  truck  heading  to  a  job.    The  truck  was  going  west  on  Ave  24.    While  they  were  stopped  at  the  stop  sign  a  car  was  traveling  east  (grey)  had  stopped  at  the  stop  sign  across  from  them.    When  the  car  proceeded  through  the  intersection  it  hit  another  car  (red)  that  was  traveling  north,  without  a  stop  sign,  causing  the  red  car  traveling  north  to  ricochet  into  the  front  end  of  the  digger  truck  at  the  stop  sign.    The  person  who  hit  the  car  and  hit  the  front  of  the  digger  truck  ended  up  going  to  the  hospital  with  minor  injuries.    There  were  no  injuries  to  the  driver  of  the  digger  truck.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/3/15 Outside  Crew Vehicle  Accident Civilian  Collision

Vehicle  Accident  -­‐  November  3,  2015  -­‐  A  contractor  crew  parked  a  line  truck  on  the  side  of  the  road  in  a  residential  area.  A  trailer  carrying  to  distribution  poles  was  hitched  to  the  truck.  The  groundman  was  unloading  cones  and  setting  traffic  control.      An  apprentice  was  located  on  the  curb  side  of  the  trailer  unstrapping  the  poles.  Within  a  few  minutes  of  the  line  truck  being  parked,  the  apprentice  saw  a  car  come  toward  the  trailer  and  called  out  to  the  groundman.  Both  members  were  able  to  get  out  of  the  way  as  the  third-­‐party  vehicle  collided  with  the  butt  of  the  pole  located  on  the  trailer.    The  pole  went  through  the  windshield  of  the  vehicle.  One  of  the  occupants  was  taken  to  the  hospital  for  observation.  California  Highway  Patrol  was  called  on  site  and  created  a  collision  report.                                                                                                                                                                                                            

11/6/15 Outside  Crew Dig  In Gas  Line

Dig  in  -­‐  On  November  6,  2015  -­‐  San  Joaquin  -­‐  A  contractor  crew  was  hand  digging  in  an  alley      for  a  pole  set  and  in  the  process  they  struck  a  gas  line.  The  gas  company  was  called  out  and  the  crew  ceased  work  and  evacuated  the  area.    The  gas  company’s  first  responder  showed  up  to  close  off  the  area  and  then  contacted  a  crew  to  come  shut  off  the  gas  and  repair  the  line.  Everyone  is  fine  and  there  were  no  injuries.                                                                                                                                                      

11/10/15 Outside  Crew Dig  in Phone  Cable

Dig  in  -­‐  On  November  10,  2015  -­‐    Saddleback  -­‐  A  contractor  crew  was  assigned  to  an  ECO  on  the  Chrome  12kV  to  replace  a  damaged  hand  hole.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards  and  methods  to  be  utilized  to  mitigate  any    hazards.  All  USA  marks  were  noted  and    re-­‐marked  as  needed  to  avoid  any  damage  to  the    existing  utilities.  Traffic  Control  was  established  per  the  WATCH  manual  so  as  to  protect  the  crew  as  well  as  the  public.  As  the  crew  was  hand  digging  with  shovels,  a  crew  member  inadvertently  struck  and  damaged  an    AT&T  phone  service.  The  crew  foreman  contacted  AT&T,  and  an  AT&T  crew  was  dispatched  to  make  the  required  repairs.  After  the  phone  cable  was  restored  to  service,  the  PAR  crew  continued  to  work  without  any  further  incidents.    No  injuries  were  reported.        

11/16/15 Outside  Crew Property  Damage

Improper  Work  Method

Property  Damage  -­‐  On  November  16,  2015    -­‐  Palm  Springs  -­‐  A  contractor  crew  was  excavating  for  mainline  conduit  installation  after  creating  potholes  and  exposing  USA  field  marked  utilities  in  conflict  with  excavation.  While  digging  with  a  backhoe,  the  crew  struck  an  unmarked  reclaimed  water  main  crossing  the  excavation.  Coachella  Valley  Water  Co.  (CVW)  was  notified  and  responded  to  the  damage.  CVW  determined  that  the  water  main  belonged  to  Desert  Greens  Golf  Course  (DGGC).  DGGC  maintenance  personnel  responded  and  shut  off  the  main.  The  contractor  crew  lost  considerable  production  time  while  mitigating  water  damage  to  excavation  and  flooding  to  surrounding  area.  What  can  we  learn  from  this?    On  future  projects  that  take  place  on  private  property,  the  Property  Manager,  Maintenance  Engineer,  and  the  owner,  if  possible,  should  be  present  at  the  pre-­‐construction  meeting.  This  will  allow  the  contractor  to  explain  the  project  details  and  ask  questions  about  underground  facilities  or  hazards  that  may  be  unidentified  on  drawings  or  with  USA.  No  injuries  were  reported.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

11/16/15 Outside  Crew Property  Damage

Equipment  Failure

Property  Damage  -­‐  On  November  16,  2015  -­‐  Ontario  -­‐  A  contractor  crew  had  installed  new  336  AL  conductor  and  re-­‐energized  the  circuit.  Upon  picking  up  load  at  a  location  of  a  480V  panel,  bad  wiring  caused  a  phase-­‐to-­‐phase  and  the  panel  failed.  The  crew  contacted  SCE  PGS  and  trouble  men  to  assess  the  situation.  With  the  support  of  SCE,  the  panel  wiring  was  deemed  to  have  failed.  New  parts  were  installed  and  the  customer  was  re-­‐energized.  What  can  we  learn  from  this?  Be  aware  of  customer  equipment  conditions  and  take  extra  steps  to  assess  panel  conditions  before  energizing.  The  crew  reported  the  utilization  of  a  "firecracker"  to  limit  circulating  current.    No  injuries  were  reported.

11/21/15 Outside  Crew Dig  in Mismarked  Utility  Service

Dig  in  -­‐  On  November  21,  2015  -­‐  Arrowhead  -­‐  A  subcontractor  crew  was  assigned  to  work  on  an  ECO  on  the  Rowco  12kV  circuit.  A  tailboard  was  given  so  that  all  crew  members  understood  the  task,  hazards,  and  the  methods  to  mitigate  any  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established.  While  the  crew  was  performing  a  directional  bore,  they  struck  and  damaged  an  unmarked  1-­‐inch  plastic  water  service  with  their  bore  bit.  The  foreman  notified  DigAlert,  and  DigAlert  dispatched  a  Running  Springs  Water  District  repair  crew  to  respond  and  make  the  necessary  repairs.  After  the  repairs  were  made,  the  crew  finished  the  day  without  any  further  incidents.

11/21/15 Outside  Crew Dig  in Phone  Cable

Dig  In  -­‐  On  November  21,  2015  -­‐  Arrowhead  -­‐  A  contract  crew  was  assigned  to  work  on  an  ECOon  the  Rowco  12kV  circuit.  A  tailboard  was  given  so  that  all  crew  members  understood  thetask,  hazards  and  the  methods  to  mitigate  any  hazards.  All  USA  marks  were  noted  and  re-­‐marked  as  needed  to  avoid  any  damage  to  the  existing  utilities.  Traffic  Control  was  established.  While  the  crew  was  potholing  a  marked  Verizon  phone  cable  to  verify  its  exact  location,  they  inadvertently  nicked  and  damaged  it  with  a  shovel.  The  crew  foreman  notified  DigAlert  of  the  damage,  and  DigAlert  dispatched  a  Verizon  repair  crew  to  respond  and  make  the  necessary  repairs.  The  necessary  repairs  were  made.

11/23/15 Outside  Crew Close  Call Load  Securement

Close  Call  -­‐  On  November  23,  2015  -­‐  Catalina  -­‐  A  scissor  lift  was  being  transported  from  the  freight  yard  to  the  job  site  using  a  forklift.  A  rough  patch  of  road  caused  the  forklift  tolose  control  of  the  load.  What  can  we  learn  from  this?  The  forks  could  have  been  secured  together  to  prevent  the  scissor  lift  from  falling.    No  injuries  were  reported.

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

9/12/14 IOU-­‐E  Lineman Significant  InjuryPartial  

Amputation  Fingers

Significant  Injury  –  On  September  12  2014,  A  IOU-­‐E  worker  had  his  fingertip  amputated  after  sustaining  an  injury  while  in  the  process  of  pulling  cable.  The  worker’s  hand  was  placed  in  the  bite  of  a  capstan.  The  worker  inadvertently  pushed  the  lever  of  the  capstan  while  reaching  across  to  unwind  mule  tape  that  had  accumulated  in  the  capstan.  This  activated  the  capstan  and  caused  it  to  tighten  the  line,  pulling  the  mule  tape  tight  across  the  worker’s  left  index  finger  causing  partial  amputation.

11/5/14 IOU-­‐E  Lineman Significant  Injury BurnSignificant  Injury  -­‐  11-­‐5-­‐2014,  Primary  flash  occurred  and  burns  suffered  when  linemen  removed  an  energized  12kV  elbow  without  testing  or  grounding    EMS  called  and  employee  transported  to  hospital  for  treatment  for  burn  injuries

11/16/14IOU-­‐E  Lineman  /  Hot  Apprentice Significant  Injury Burn

Significant  Injury  -­‐  11-­‐16-­‐2014,  Two  workers  were  involved  in  an  electrical  flash  incident  while  working  inside  an  underground  structure  in  the  City  of  La  Puente.  Preliminary  information  indicates  that  a  journeyman-­‐lineman  and  hot  apprentice,  installed  600-­‐amp  components  onto  a  gas  switch  on  the  Coupler  12kV  circuit,  and  were  in  the  process  of  removing  a  200-­‐amp  elbow  on  an  adjacent  position  when  a  flash  occurred  resulting  in  burns  injuries

11/16/14 IOU-­‐E  Crew CCCI Boom  Contact

CCCI  -­‐    On  November  16,  A  IOU-­‐E  four-­‐man  crew  was  working  on  an  ongoing  project  on  the  91  Freeway.  They  were  in  the  process  of  taking  a  fixed  capacitor  bank  offline  for  a  switching  procedure  when  the  boom  made  contact  with  a  conductor,  causing  an  electrical  flash  and  the  Promenade  12kV  to  lock  out.  No  injuries  were  reported.  Preliminary  information  indicates  that  the  bucket  truck  had  been  moved  into  position  for  the  work  to  be  completed.  The  lineman  inside  the  bucket  uncradled  the  bucket  and  began  ascending  when  the  knuckle  of  the  boom  made  contact  with  one  or  multiple  conductors.  Two  conductors  on  the  contacted  span  were  burnt  to  the  ground.  

1/7/15 SCE  T&D Significant  Injury FractureSignificant  Injury  -­‐  On  January  7,  2015  -­‐  Worker  was  off-­‐loading  an  underground  oil  switch  when  the  load  shifted  hitting  his  leg  and  knocking  him  off  the  trailer  resulting  in  a  broken  leg  and  head  injuries.

3/3/15 IOU-­‐E  Lineman Significant  InjuryPartial  

Amputation  Fingers

Significant  Injury  –March  3,  an  IOU-­‐E  distribution  lineman  from  the  Victorville  District,  sustained  a  serious  injury  to  his  left  hand  while  working  on  a  job  to  replace  a  deteriorated  dead-­‐end  pole.  After  replacing  the  pole,  upgrading  the  transformer,  transferring  conductors,  and  restoring  load,  the  crew  proceeded  to  remove  the  old  pole.  A  pole  jack  and  boom  were  employed  to  pull  the  old  pole  out  of  the  ground.  Preliminary  information  indicates  two  of  the  lineman’s  fingers  on  his  left  hand  were  caught  in  a  pinch  point  on  the  pole  jack.  He  was  wearing  gloves  at  the  time  of  the  incident.

4/21/15 IOU-­‐E  CrewSafety  

Consideration Heat  Scan

Safety  Consideration  –  4-­‐21-­‐2015  -­‐  Following  a  UDI  vault  inspection,  600  amp  components  failed  30  minutes  later  and  just  about  24  hours  after  that,  Equipment  components  failed  again  on  a  BURD  transformer  in  the  same  structure.  Approximately  8  feet  of  water  had  been  pumped  prior  to  the  UDI  inspection.  No  visible  defects  were  noticed  during  inspection  or  first  repair.  The  crew  that  worked  the  second  repair  order  completely  de-­‐energized  the  vault  before  proceeding  with  work.

Customer  Accidents/Incidents

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Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

5/11/15 IOU-­‐E  Crew Safety  Consideration

Significant  Injury

Significant  Injury  -­‐  May  11  2015,  a  Transmission  employee  was  seriously  injured  after  sustaining  a  rattlesnake  bite.  A  heavy  equipment  operator,  was  working  on  a  transmission  project  in  Porter  Ranch  related  to  the  new  Natural  Substation.  Preliminary  information  indicates  the  employee  was  moving  road  marking  stakes  from  a  bundled  pile,  which  reportedly  concealed  the  snake.  Once  disturbed,  the  snake  reacted  and  bit  the  employee  on  his  right  hand.  His  co-­‐worker  on  the  job  immediately  called  911  and  notified  supervision.  The  employee  was  transported  by  ambulance  to  Northridge  Hospital  Medical  Center  where  he  currently  is  in  the  Intensive  Care  Unit  under  close  observation

5/26/15 IOU-­‐E  Crew Significant  Injury Fracture

Significant  Injury  -­‐  On  May  26  2015  -­‐    a  Transmission  lineman  from  San  Joaquin,  was  seriously  injured  after  falling  from  a  bucket  truck.  The  employee  was  working  on  a  patrol  crew  tasked  with  removing  a  tarp  that  had  blown  into  the  Dairymans-­‐Protein  66kV  line  in  Tulare.  Preliminary  information  indicates  the  employee  was  removing  the  cover  from  the  cradled  bucket  when  he  lost  his  footing  and  fell  off  the  truck.  The  crew  immediately  called  911,  and  the  employee  was  transported  by  ambulance  to  Kaweah  Delta  Hospital  in  Visalia.  He  currently  is  at  the  hospital  receiving  treatment  for  his  injuries.  

5/13/15 SCE  T&D Significant  Injury Snake  Bite

Significant  Injury  -­‐  On  May  11,  2015  -­‐  A  Transmission  employee  was  seriously  injured  after  sustaining  a  rattlesnake  bite.    A  heavy  equipment  operator,  was  working  on  a  transmission  project  in  Porter  Ranch  related  to  the  new  Natural  Substation.  Preliminary  information  indicates  the  employee  was  moving  road  marking  stakes  from  a  bundled  pile,  which  reportedly  concealed  the  snake.  Once  disturbed,  the  snake  reacted  and  bit  the  employee  on  his  right  hand.  His  co-­‐worker  on  the  job  immediately  called  911  and  notified  supervision.  The  employee  was  transported  by  ambulance  to  Northridge  Hospital  Medical  Center  where  he  currently  is  in  the  Intensive  Care  Unit  under  close  observation.

6/2/15 2nd  Employee Vehicle  Incident Head

Significant  Injury  6/2/2015  -­‐  An  employee  was  driving  back  to  the  service  center  after  completing  his  work  for  the  day.  While  en  route,  the  employee  lost  consciousness,  causing  the  vehicle  to  veer  off  the  highway.  It  rolled  over  several  times  and  landed  on  the  opposite  side  of  the  highway.  The  employee  was  taken  to  the  hospital  and  has  since  been  released  and  is  now  at  home  recovering.

6/6/15 1st  Lineman Vehicle  Incident Ribs

Significant  Injury  6/6/2015  -­‐  A  lineman  was  injured  the  boom  truck  he  was  driving  struck  a  cluster  of  rocks  and  rolled  onto  its  side.  The  lineman  was  driving  down  Highway  74  toward  Hemet  after  finishing  work  on  a  pole  that  had  been  hit  by  a  car.  While  approaching  the  base  of  a  hill,  his  boom  truck  veered  to  the  right  and  struck  the  rocks.  Though  it  was  tipped  on  its  side,  the  lineman  was  able  to  exit  the  vehicle  and  initially  said  he  felt  fine.  However,  he  later  said  he  was  suffering  from  pain  in  his  ribs  and  an  ambulance  was  called.  He  was  taken  to  a  nearby  hospital  where  he  was  treated  and  released.

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12/3/15 Page  36

Date  Of  Incident Occupation Type  of  Incident

Body  Part  /    Root  Cause Description

8/6/15 Transmission  Lineman

Significant  Injury Fracture  /  Head

Significant  Injury  August  6,  2015  –  A  SCE  Transmission  lineman  from  the  Orange  Grid,  was  injured  when  he  fell  from  a  transmission  line  truck.  Thankfully,  he  was  not  seriously  hurt,  but  he  suffered  a  head  wound  and  fractured  wrist.  He  is  doing  well  and  recovering  at  home.  The  incident  is  currently  under  investigation.  Preliminary  information  indicates  the  lineman  was  walking  across  the  top  of  the  truck  tool  bins  to  retrieve  shovels  when  he  lost  his  footing.  Transmission  Grid  managers  are  gathering  their  field  employees  to  talk  about  what  happened  and  pinpoint  solutions  to  prevent  truck  falls.  However,  we  stand  together  as  we  call  your  attention  to  this  hazard.

8/17/15 Transmission  Lineman

Significant  Injury Fracture

Significant  Injury  August  17,  2015  –  A  SCE  Transmission  lineman  from  the  Metro  East  Grid,  was  seriously  injured  while  working  on  a  fire  restoration  job  in  Montebello.    He  sustained  multiple  fractures  to  his  right  lower  leg  and  is  currently  receiving  medical  care  at  Cedars-­‐Sinai  Medical  Center.    The  Lineman  was  on  a  crew  in  charge  of  removing  the  existing  66kV  wood  poles  that  were  damaged  by  the  fire,  and  framing,  digging,  and  setting  new  poles.    The  Lineman's  specific  task  was  to  frame  the  head  on  a  new  wood  pole.    Preliminary  information  indicates  he  was  in  the  process  of  rotating  the  pole  with  a  cant  hook  -­‐  a  traditional  logging  tool  used  for  handling  and  turning  wood  logs  -­‐  when  the  handle  of  the  hook  failed  and  broke,  causing  him  to  fall  back  and  injure  his  right  leg  and  ankle.    His  co-­‐workers  rushed  to  has  aid  and  called  911.

8/26/15 Traffic  Control Traffic  Control Motorcycle

Traffic  Control  August  26,  2015  -­‐  A  contract  worker  in  the  Covina  District  had  control  of  stopped  traffic.  A  driver  who  was  involved  in  an  altercation  earlier  drove  past  the  job  site  and  exited  his  vehicle  to  approach  a  motorcyclist,  who  had  broken  the  driver's  side  mirror.  As  the  motorcyclist  was  approached,  he  fled  the  scene  but  lost  control  of  his  motorcycle.  In  doing  so,  he  struck  the  contract  worker  managing  the  traffic.  The  worker  was  attended  to  in  Ontario  by  U.S.  Healthworks  and  a  preventative  tetanus  shot  was  given  to  the  employee  due  to  a  minor  cut  sustained  by  the  collision.

10/13/15 SCE  Crew Close  Call Snake      Close  Call  on  October  13,  2015  -­‐  An  SCE  employee  found  a  Mojave  Green  rattlesnake  inside  an  SCE  vault  located  inside  the  substation.    SCE  Environmental  was  called  and  a  biologist  was  dispatched  to  remove  and  relocate  the  rattlesnake.    No  injuries  occurred.

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Page  1  of  1  December  2,  2015  

Monthly  Supervisor  Staff  Meeting  Construction  Services  (CS)  Safety  Report  

Through  October  2015    

CS  -­  MVI’s/OSHA  InjuriesCS has One CMVI and No OSHA-Recordable injuries.    Incident  and  Injury  Rates      

1.   Construction Services is counting 13 Incidents. 1.   1/15 – C222, Temporary jumper failed causing outage 2.   2/11 – C442, while crimping connector wire falls to ground. 3.   2/11 – Fuerte Dr., operator hit marked gas main. 4.   2/17 – Fuerte Dr., operator hit marked gas main. 5.   3/30 – MT1, while transferring load crew crosses phases. 6.   4/18 – C239, crew dropped new cross-arm on conductors. 7.   5/15 – C44, crew put 2 phases on same feed-thru. 8.   5/16 – C386, crew dropped jumper tail causing ph to ph outage. 9.   6/2 – Chula Vista 400 psi gas blow in. 10.   6/25 – C222, while applying primary cover wire slipped out of shoe. 11.   7/2 – C781, while chipping for intercept SBL hits energized 12kV conductor. 12.   8/18 – Greenfield Dr., while welding Mueller fitting EE burned through 8” pipe. 13.   9/8 – C222, Crew cut wrong over the arm jumper causing outage.

2.   Contractor Incidents Under Investigation or Review:

11/24 – Fatality due to EE hit by car.

3.   Contractor Injury/Interruption Rates: 1.   Outage Rate (October): 1.90 (Target 1.02) 2.   Injury Rate (October): 2.34 (Target 2.46)

List  of  Injuries    

1. 1/23 Foot, puncture, fracture when hit by board with spike in it. 2. 2/24 Finger, employee lacerated pinkie when cutting zip tie toward self. 3. 3/4 Finger(s), fracture, crushed in shoring jack. 4. 3/17 Hand, while skinning cable EE cut himself with knife. 5. 3/19 Finger, inflammation, while pole brushing EE was punctured by cactus thorn. 6. 3/26 Calf, strained while avoiding lunging dog. 7. 4/2 Finger, laceration when smashed between block wall and log EE was carrying. 8. 4/8 Arm, laceration and fracture when EE is hit by snapped rope. 9. 4/9 Torso, while trimming palm EE is engulfed in palm fronds. 10. 4/9 Knee, sprain when stepping off truck, Modified Duty, no LTI. 11. 4/18 Toe, fracture when 10” rock rolled down hill and hit toe. 12. 5/21 Knee, laceration when chainsaw cut thru chaps. 13. 6/10 Hand, Hip, burns from induction incident. 14. 6/10 Hand, while skinning cable EE cuts self on palm, 14 stitches. 15. 9/8 Finger, laceration and fracture to pinky when caught between pole saw and edge of bucket. 16. 9/25 Ankle, sprain when jumping into shallow trench. 17. 11/24 Fatality, tree trimmer was hit by a car while clearing trimmed branches.

 

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Event  Number

Date  of  Incident Region Division Circuit Description  of  Event

Type  (momentary  or  sustained)

Customers  Impacted

Inadequate  control    (phases  getting  together)

Wire  on  Ground

Incident/ACE  

Reports

Primary  or  Secondary OH/UG Work  type Error  Category

2015-­3 3/06/2015  @  3:15  pm

CV Kern N/A crew  dug  into  Fiber  optic  12  count  without  valid  USA N/A O no no yes Telephone UG AG Dig-­In

2015-­4 3/10/2015  @  2:30  pm

NO Ukiah Philo  1101Apprentice  Terminated  secondary  Bus  Tube  Leads  to  Service  improperly  causing  a  phase  to  phase  secondary  condition  which  blew  out  fuses  on  XFMR  bank  -­‐  1  pole  N/E

N/A 0 no no yes Secondary OH Residential Incorrect  Connection

2015-­5 5/26/2015  @  12:20  pm

CV Kern N/ACrew  dropped  new  conductor  on  a  hot  customer  crossing  (McPherson  Oil)  burning  customer  line  down

N/A 1 yes yes Yes Primary OH Reconductor Wire  Down

2015-­6 5/17/2015  @  11:00  am

NR Sonoma Silverado  2102Helicopter  set  poloe  on  top  of  #6  CU  breaking  wire  and  causing  an  outage

N/A 48 no yes Primary OH Wire  Down

2015-­7 4/22/2015  @  12:45  pm

NR Sonoma/Santa  Rosa

Molino  1101  While  moving  energized  conductor  crew  let  top  phase  touch  a  buck  phase  causing  a  x  phase  blowing  a  line  fuse

N/A yes no yes Primary OH Pole  Replacement Inadequate  control

2015-­8 4/20/2015  @  10:15  AM

CC SLO Paso  1101While  removing  a  switch  crew  removed  switch  handle  and  switch  fell  closed  causing  a  circuit  interuption

N/A 0 no no yes Primary OH Reclosure  removal ?

2015-­9 4/2/2015  @  10:34  AM

CV Fresno Caruthers  1105While  dead  ending  wire  crew  lost  controla  of  a  tail  into  an  energized  circuit

N/A ? yes yes yes Primary OH ? Inadequate  control

2015-­10 3/10/2015  @  15:00  PM

NR SonomaUnderarm  service  bus  hooked  to  both  hotlegs  of  open  wire  secondary  causing  a  cross  phase

N/A ? no no yes Secondary OH service Incorrect  Connection

2015-­11 6/7/2015  @    09:47AM

CV Yosemite Gustine  1102Crew  shook  pole  while  digging  next  to  it  and  brought  #6  Cu  down

S 44 ? Yes yes Primary OH Pole  Replacement Wire  Down

2015-­12 20-­Jun CC San  Jose El  Patio  1104While  installing  a  Scada-­‐  Mate  Switch  crew  failed  to  verify  it  was  closed  dropping  load  when  removing  a  temp  jumper.

S 1 No No Yes Primary OH Switch  Replacement

Human  Performance

2015-­13 21-­Jun CV Yosemite DairyLand  1109Crew  opened  jumpers  on  tap,  when  re-­‐connecting  they  did  not  connect  back  the  same  resulting  in    an  out  of  phase  condition  damage  a  3  phase  pump  

N/A 5 no no yes Primary OH Ag Incorrect  Connection

2015-­14 Aug.  3 NR Humbolt Harris  1108While  transferring  center  phase  of  vertical  construction  crew  made  contact  with  top  phase  which  had  already  been  transferred  to  the  new  pole  causing  a  cross  phase.

yes no yes Primary OH Pole  Replacement Inadequate  control

2015-­15 3-­Oct CC San  carlos Redwood  City  410

While  transfering  secondary  primary  sliped  through  ties  causing  seconday  and  primary  to  to  contact  each  other  causing  a  cross  phase.

Sustained 383 yes no yes Primary OH pole  Replacement Inadequate  control

2015-­16 22-­Oct NR Sacramento B  1101While  building  an  elbow  lineman  did  not  install  the  pin  in  the  elbow

61 no no yes Primary UG 56 Poor  Workmanship

2015-­17 30-­Oct NR sacramento Peabody  2113 Crew  mistakenly  spliced  new  cable  to  abandoned  cable   208 no no Yes Primary UG 56 Poor  Workmanship

2015-­18 26-­Oct CC San  Jose Mabury  1102Tail  of  conductor  made  contact  with  extension  link  causing  a  x  phase

1997 yes no Yes Primary OH Pole  Replacement Inadequate  control

PG&E  -­  2015  Contractor  Work  Procedure  Errors

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J.R.T.C. Accident Report

CRLlfDRnlR • nEVRDR

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lnjured's Name ---""""M=a=tt"""'h-=-ew-'-'--'-H""""i""-11 ____________ _

Birth Date 7/27/84 Classification Apprentice Lineman

Date of Injury 8/14/2015 Weather ___ C.=.......le-=a __ r-_____ w'"""'a""""rm-'-'--___ _

Location 9846 Limonite Avenue - Riverside, CA 92509

4. Present Employer_.;...:N"-'-/A-'-------�------------

5.

6. Others Present (name and classification) --'P=--=at;:.;..ri=c"""k-=B'-'-la=n"-'-c=o:;.J.,....;.I :..:..n s=t:.:..:ru=c=to=r'--_

7. Description of Accident (be specific) Matthew was practicing climbing

exercises on a wood pole. While descending, he moved his left arm and

felt a pop in his left shoulder, causing pain from his neck down through his

left shoulder and arm to his elbow.

8. What has been done to prevent recurrence of accident? Further

instruction given to Matthew on better climbing techniques and pole

climbing procedures.

9. Extent of Injury (cut, broken bone, etc.) Pain from his neck through his

left shoulder and arm to his elbow.

10. Treatment sent to urgent care

First Aid __ Doctor ___ Hospitalized ___ Time Lost (days) __ _ Permanent Injury Partial Total Fatal __ _

11. Report made by Armando Mendez Title Director Address: 9846 Limonite Ave. Riverside, CA 92509 Phone: 951/685-8658

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12. Method of Payment NIA - refer to Mass Benefits area code 951

Knowledge of Power is Powerful Knowledge

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P: 685-VOU {8658)

F: 685-WIRE (9473)

www.calncvjatc.org Exhibit B

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