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a .. . .. - * .. ....a. _ . .__ .. _ _ . . ... . . . . . ,. ~ . - ! . .i * . ' , . . U. S. ATOMIC ENERGY CO:f!ISSION DIRECTORATE OF REGULSTORY OPERATIO:;S REGION I R0 Inspection Report No.: 50-289/74-06 Docket No.: 50-289 Licensee: Metropolitan Edison Company License No.: CPPR-40 P.O. Box 542 Priority: a Reading, Pennsylvania Category: B (Three Mile Island - Unit 1) t 'o . Location: Middletown, Dauphin County, Pe'nnsylvania Type of Licensee: PWR 871 MWe (B+W) ,- ^ , 1 Type of Inspection: Routine, Unannounced Dates of Inspection: February 19-21, 1974 Dates of Previous Inspection: February 12-15, 1974 Reporting Inspector: L d"hv , ;-3 f 7 t/ Seth A. tolscam, neactor inspecm / / Date . I Acco=panying Inspectors: ,,,,,g Date - . Date - . i , Other Accompanying Personnel: None Date : [ fife - (1- / ' *D M M Jad Reviewed By: R. F. Heishman, Reactor Inspector Date I L. I - - . . . . _ . . . .

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Page 1: (Three Mile Island - Unit 1)

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U. S. ATOMIC ENERGY CO:f!ISSION

DIRECTORATE OF REGULSTORY OPERATIO:;S

REGION I

R0 Inspection Report No.: 50-289/74-06 Docket No.: 50-289

Licensee: Metropolitan Edison Company License No.: CPPR-40

P.O. Box 542 Priority:

a

Reading, Pennsylvania Category: B

(Three Mile Island - Unit 1)t 'o .

Location: Middletown, Dauphin County, Pe'nnsylvania

Type of Licensee: PWR 871 MWe (B+W),- ^ ,

1

Type of Inspection: Routine, Unannounced

Dates of Inspection: February 19-21, 1974

Dates of Previous Inspection: February 12-15, 1974

Reporting Inspector: L d"hv , ;-3 f 7 t/Seth A. tolscam, neactor inspecm / / Date

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I Acco=panying Inspectors: ,,,,,gDate-

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Other Accompanying Personnel: None

Date:

[ fife - (1-/

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*D M M JadReviewed By:R. F. Heishman, Reactor Inspector Date

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(~ SUK ARY OF FINDINGS

Enforcement Action

Nonet

Licensee Action on Previously Identified Enforcement Matters

A. A task force was formed by the licensee to identify cabling dis-crepancies and to insure their correction. The inspector 's re-audit show-ed cabling to be in conformance with pull cards and drawings.,.

i This item is resolved. (Details, Paragraph 2)l

: Unusual Occurrences,.

| None identified|

Design Changesj ,

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None identified -

t' Other Significant Findingsj.

' 'A. Current Findings'

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l. The inspector examined the handling and inspection of nuclear'

fuel. No deficiencies were identified. (Details, Paragraph 3)'

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2. The licensee stated that the containment structural integrity;

test (SIT) was re-scheduled to start on March 4, 1974. Fuelloading was re-scheduled to start March 28, 1974. (Management

|Interview, Paragraph A)

B. Status of Previous 1v Reported Unresolved Items'

1. The following items were resolved during the inspection:.

Handling and inspection of nuclear fuel. (Details,a.

| Paragraph 3)}

b. Bent thermocouple guide tubes. (Dett. .s, Paragraph 4)i

c. Core flood tank valve malfunction. (Details , Paragraph 5)|

i d. QA program breakdown on electrical equipment inspectionand testing. (Details , Paragraph 6)

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,e. Welding filler electrodes for major components. (Details,

Paragraph 7)

f. Coolant bleed tank welder identification. (Details,Paragraph 8)

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Management Interview

A management interview was held at the site on February 21, 1974 withthe following personnel in attendance:

General Public Utilities Service Corporation (GPUSC)

Mr. R. A. Burns, Assistant Project Manager

* Mr. W. T. Gunn, Project Site ManagerMr. J. A. Renshaw, Project EngineerMr. D. H. Reppert, Safety & Licensing Health PhysicistMr. G. L. Roshy, Auditor,

.

Mr. M. J. Stromberg, Site Quality Assurance Auditor

Gilbert Associates (GAI)s

.- Mr. G. R. Joseph, Quality Assurance Assistant Program Manager

Mr. P. J. Shipper, Project Electrical Engineer

United Engineers & Constructors (UE&C),

Mr. V. E. Cichocki, Construction QA/QC Coordinating SuperintendentMr. R. L. Hawkins, Construction QA/QC Coordinator

' Mr. B. E. O'Connor, Quality Control Documents

The following items were discussed:

A. In response to the inspector's questions concerning schedulesthe licensee stated that the containment structural integritytest (SIT) had been re-scheduled to start March 4, 1974, with*

fuel loading re-scheduled to start March 28, 1974. The licenseeagreed to notify the inspector of any change in the SIT schedule.

B. The inspector stated that the following items had been resolvedat this inspection:.

1. Cable routing discrepancies (Details, Paragraph 2)

2. Inspection of nuclear fuel (Details, Paragraph 3)~

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( )I 3. Bant ther=occuple guide tubes (Details, Paragraph 4)i_

4. Core flood tank valves malfunction (Details, Paragraph 5)

I5. QA program breakdown on electrical equipment inspection and:

| testing (Detai'.s, Paragraph 6)

6. Welding filler electrodes for major components (Details, ,

! Paragraph 7),

I7. Coolant bleed tank welder identification (Details, Paragraph 8)'

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The licensee acknowledged this information, and stated that every effort

| would be expended to resolve the remaining outstanding items withintha next week.

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DETAILStw.

1. Persons Contacted

General Public Utilities Service Corporation (GPUSC)

Mr. J. Barton, Manager, Startup & TestMr. R. A. Burns, Assistant Project ManagerMr. I. Feinberg, Electrical EngineerMr. R. F. Fenti, Shif t EngineerMr. W. T. Gunn, Project Site Manager

.

Mr. S. Levin, Proj ect Engineer, Unit 1Mr. P. Levine, Quality Assurance EngineerMr. J. A. Renshaw, Proj ect EngineerMr. D. H. Reppert, Safety & Licensing Health Physicist

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Mr. G. L. Roshy, Auditor-

Mr. M. J. Stromberg, Site Quality Assurance Auditor,

.

Mr. J. E. Wright, Quality Assurance Manager ,

Gilbert Associates (GAI)

( Mr. G. R. Joseph, Quality Assurance Assistant Program Manager

Mr. P. J. Shipper, Project Electrical Engineer

United-Engineers & Constructors (UE&C)

Mr. V. E. Cichocki, Construction QA/QC Coordinating Superintendent

-Mr. R. H. Hawkins, Construction QA/QC Coordinator

Mr. D. C. Lambert, Field Supervisor, Quality ControlMr. B. E. O'Connor, Quality Control Documents

2. Safeguards Cabline Discrepancies'

*

During a previous inspection the inspector found numerous instanceswhere cables including safeguards, were not routed in accordance

The licenseewith the . pull cards, computer printouts or drawings.had since formed a special task force to verify all cabling,identification and routing, and to make corrections where necessary.

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The inspector re-audited the safeguards cables in several systems' '

ar.1 no deficiencies were identified. This item is resolved.

3. Handline and Inspection of Nuclear Fuel|

| The inspector examined the handling and inspection of nuclear fuel,I

together with associated documentation. The following items were' included:, ,

a. Vendor inspection program.

b. Document control (1F1-201)

Tool and gage control (lF1-205)' c.

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d. Cleaning and cleanliness (1F1-206)

Radiological control (1F1-203)' e.'

f. Receipt inspection fit-up and storage (lFP-603).

g. Separation of deficient material'

h. Handling equipment test certification

1. Personnel and materia'l control4

't j. Assqmbly of control rods into fuel elements.

ik. Accounting records

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1 1. Shift logs,;

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Fuel purchase documentation, change orders and vendor; m.quality certification.

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No deficiencies were identified. This item is resolved.!'

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4. Bent Thermocouple Guide Tubes.

The guide tubes on the veat valve ther=ocouples had previously been

|bv.nt when'the reactor vessel head was installed. The licensee hassince determined that these thermocouples would not be required;

for the expected power levels. The thermocouples and guide tubeshave been removed. This item is resolved.

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5. Core Flood Tank Valves Malfunction

. The inspector examined Babcock & Wilcox letter of February 20, 19741 to the licensee, and the core flood system valve vendor's letter

to B&W ef September 4, 1973 " Core Flood System Valves." The vendor4 stated that machining errors were the cause of the valve malfunction,

and that the A564, Grade 360 material used wc3 an authorized sub-stitution. This iten is resolved.

6. 0A Program Breakdown on Electrical Eauipment.

The licensee has completed the corrective action on the failure of

an electrical equipment vendor to perform the quality control op-erations required in the vendor's program. The vendor's re-testprogram, dated August 22, 1973, was approved by the licensee anawas completed with no deficiencies being identified. The licensee's-

audit report 73-49, dated December 3, 1973 noted that "the testingi

was conducted as written, and that QC was provided.".

The inspector examined the results of the testing program, involvingi 7 reports, including E9048 and E8958, and no deficiencies were

identified. This item is resolved.

_ 7. Welding Filler Electrode on Maior Comoonents

The welding filler electrodes used on the steam generators were nota

traceable, as this was not a requirement at the time of manufacture.The vendor had prepared Topical Report No. BAW-1402, dated January1973, which provided the data necessary to justify the use of certain

. lots of weld filler material which had incomplete documentation ofmechanical properties. This iten is resolved.

i 8. Coolant Bleed Tank Welder Identification-

t

At a previous inspection, it was found that welder identification wasnot available for the welding on the Reactor Coolant Bleed Tank 1A.

At this inspection, the inspector examined PDM Drawing WL-1, dated.

Sep tember 11,1968 " Reactor Coolant Bleed Tank 1A" which includedthe identification of individual welders for each seam. This itemis resolved.

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