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The 2 nd annual Air-Cooled Condenser User’s Group Meeting WenhuaTian Huiyong He Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China September 28-29, 2010 Pueblo Air-Cooled Condensate Polishing in China

The 2 nd annual Air-Cooled Condenser User’s Group Meeting

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The 2 nd annual Air-Cooled Condenser User’s Group Meeting. Air-Cooled Condensate Polishing in China. WenhuaTian Huiyong He Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China September 28-29, 2010 Pueblo. CONTEXTS. I. Introduction of TPRI - PowerPoint PPT Presentation

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Page 1: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

The 2nd annual Air-Cooled Condenser User’s Group Meeting

WenhuaTian Huiyong He

Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China

September 28-29, 2010 Pueblo

Air-Cooled Condensate Polishing in China

Page 2: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

CONTEXTS

I. Introduction of TPRI

II. Developments of ACCs in China

III. Carbon Dioxide in ACCs

IV. DO Controlling in ACCs

V. Case of Indirect ACCs

Page 3: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Introduction of TPRI

Page 4: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Developments of ACCs in China

Page 5: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Outline The distribution of coal and water resources in China is asymmetric; coal-rich regions typically lack water and vice versa Because of its significant water-saving advantage, ACC is suitable for drought-prone regions in northern China. So the government of China required that all the new built coal power plants should be used ACCs in drought-prone regions after 2002 The use of ACCs has increased rapidly in China within the past five years

Page 6: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Development of ACCs The total capacity of ACCs was about 24,000MW by 2007

The percentage of ACCs was 4.3%(Total capacity of coal power plant was 554,000 MW)The number of constructing sub-critical ACC plants was 47, and the capacity was 46,000 MW (2008 ~ 2009)

Number o f units

Capacity(MW) Total Capacity(MW)

23 600 13,800

25 300 7,600

11 200 2,200

Page 7: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

It is estimated that the total capacity will reach 1,200,000MW until 2015 in China Capacity of coal power plant will be 820,000MW Capacity of ACCs will surpass 100,000MW and occupy 12%

Foreground

Page 8: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Direct ACCs were the majority, occupied 93% in 2007 Indirect ACCs developed rapidly after 2008. Up to now, the operation capacity is 4,200MW, and other units with 16,800MW capacity is constructing

Ratio of Direct & Indirect

Page 9: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

The percentage of different CPP(2009)

Page 10: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Direct ACCs were the majority, occupied 93% in 2007 Indirect ACCs developed rapidly after 2008. Up to now, the operation capacity is 4,200MW, and other units with 16,800MW capacity is constructing

Ratio of Direct & Indirect

Page 11: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Dalater Power Plant ( 4×600MW,Inner Mogolia)

Page 12: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Powdered resin filter

Page 13: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Datang Tuoketuo Power PlantDatang Tuoketuo Power Plant( ( 4×600MW,Inner Mogolia4×600MW,Inner Mogolia ) )

Page 14: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Unit 5 high-speed cation bedUnit 5 high-speed cation bed

Page 15: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Separated bed in Jingjie power plant eparated bed in Jingjie power plant (( 4×600MW,4×600MW,ShaanxiShaanxi ))

Page 16: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Carbon Dioxide in ACCs

Page 17: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Analyzer method & Instrument

Because carbon dioxide in high pure water such as condensate is as low as μg/L(ppb) level , it is difficult to sample and determine.

Trace carbon dioxide analyzer(Sentry Co. ) can measure carbon dioxide in high pure water as low as ppb level on-line.

Advantages:

(1) convenient and quick testing process

(2) high accuracy, good repeatability and high sensitivity

Standard:

D 4519-94 ( Reapproved 2005 ) by ASTM

Page 18: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Trace carbon dioxide analyzer(Sentry Co. )

Page 19: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

This test method measures the electrical conductivity of high purity water through a cation exchanger in the hydrogen form, then through an electric reboiler. The effluent was boiled at atmospheric boiling water temperature after acidic (volatile) gas removal. subsequently, it was cooled at 25 . Passage through the cation resin replaces cations ℃(including ammonia and amines)in the water with hydrogen ions. Two conductivity cells located in the instrument provide measurements of the cation conductivity at the incoming sample temperature, and the effluent conductivity at 25 .℃In order to obtain the carbon dioxide, subtract the conductivity of pure water (0.055μS/cm) from the conductivity of the final effluent cell. Then deduct this value from the cation conductivity obtained from the cell immediately after the cation exchanger resin. Use this adjusted conductivity value to look up the concentration of volatiles expressed as a concentration of carbon dioxide in Table.

Determination Methods

Page 20: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Tongchuan Power Plant

(2×600MW,Shaanxi Province)

Powdex of Tongchuan Power Plant

Page 21: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Shangan Power Plant

(2×600MW, Hebei Province)

CA-AN Bed of Shangan Power Plant

Page 22: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Plant Type of unitType of

condensate polishing

DO in condensate( μg/L)

CO2 (μg/L) Fe(μg/L)

pH

Condensate

Effluent of

polishing

Feed water

Condensate

ASubcritical

pressure drum boiler

Powdex 85 30 20 15 15.0 9.4

B

Supercritical Once-

through boiler

Pre-filtration+CA -AN

bed

20 12 3 1 8.0 9.4

Determination Results

At the same pH condition, the higher level of CO2 , the higher level of Fe in the condensate CO2 recycles in plant A, but it is removed in plant B by separated beds in plant B It is important to control the level of CO2 , it will reduce corrosion of metals in ACCs.

Page 23: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

DO Controlling in ACCs

Page 24: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Determination of DO

DO in condense will make iron corroded in ACCs, so the limit DO concentration is 100ppb in China

The operational ACCs in condense often surpass the limit of 100ppb

Page 25: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Zhaoguang Power Plant

(2×300MW+2×600MW,

Shanxi Province)Yushe Power Plant

(2×300MW,Shanxi Province)

Page 26: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Wuxiang Power Plant

(2×600MW,Shanxi Province)

Hejin Power Plant

(2×300MW,Shanxi Province)

Page 27: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Determination results of DO

Power Plant Capacity Start-up timeDO in condensate

( μg/L)Hejin 2×300 2005 70 ~ 106Yushe 2×300 2004.10 85 ~ 237

Zhaoguang 2×300

2005.7 ( #1 unit)

2005.9 ( #2 unit)

#1 unit:20 ~ 55#2 unit:52 ~ 84

Wuxiang 2×600 2006.10 < 30The reason of high DO in condensate:1. Vacuum system is too large that will lead to air leakage in ACCs.2. DO in make-up water is too high. For example, it is 800 ppb in some power plant .

Page 28: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Methods to decrease DO

Strengthen the welding management and improve its quality, try to decrease the air leakage of vacuum

System retrofitting----Case

Power PlantCapacity

Start-up time

Before the retrofitting

After the retrofitting

Wuxiang2×600 MW

2006.10.6

the exhaust unit was installed out of the condensed water tank, make-up water is supply to external condensed water tank

The condensate tank was combined to the exhaust air cooling device. After through the nozzle, the makeup water goes to the throat of exhaust device. It can lead to an increase of the secondary removal of oxygen in returned condensate.

Page 29: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Load

( MW)

Backpressure

( kPa)

Flow of Make up

water ( t/h)

Flow of Condensate( t/h)

Condensate Temperatur

e(℃)

DO( μg/L)

360 21.0 28.9 760.9 61.2 < 0.5

500 23.0 50.7 1045.3 63.2 < 0.5

600 20.5 48.2 1269.4 60.7 1.2

600 19.1 18.8 1240.0 60.0 0.7

DO in condensate after retrofitting

Page 30: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Case of Indirect ACCs

Page 31: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Yangcheng Power Plant is located in Shanxi province in China.

The first stage project are 6×350MW subcritical WCCs , which was completed at 1997.8.

The second stage project are 2×600MW subcritical indirect ACCs named SCAL, which began to construct at 2005.5.18 and completed at 2007.9.

Basic Information

The SCAL ACCs is produced by EGI company(Hungary), and it is more like the combination of Harmon’s no tower system and Heller’s cooling tower.

Page 32: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Features of SCAL indirect ACCs

Cooled water recycles closely during operation, no water consumption

High heat -exchange efficiency The corrosion rate of condenser can be controlled by

adjusting pH in recycled water in order to prolong service cycle time of condenser

Less power consumption The volume of air cooling tower is small Simple system, convenient operation and less capital

construction investment

Page 33: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Unit 7 & 8 of Yangcheng Power Plant are indirect ACCs. 3 sets of powdex are used for each CPP.

Powdex shows good filtration abillity for crud, but its desalination capacity is weak, so steam quality of the units didn’t reach the standard for most of running time.

In order to improve the steam quality, retrofitting of CPP was carried out. 2 high-speed mixed beds were added after powdex

The retrofitting has been successfully completed and put into operation in March 2009, and achieved desired results.

CPP Introduction

Page 34: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Testing Item Unit Standard Value

Min. Max. Qualified Rate

(%)

DO in condensate μg/L 30 10.8 25.1 100

Conductivity in condensate μS/cm 0.3 0.100 0.700 78.0

DO in feed-water μg/L 7 0.1 24.1 92.7

Conductivity in feed water μS/cm 0.2 0.104 1.810 38.0

SiO2 in feed water μg/L 20 3.0 37.8 94.5

Conductivity in boiler water μS/cm 1.5 0.126 2.030 99.7

SiO2 in boiler water μg/L 200 38.6 520 97.6

Conductivity in main steam μS/cm 0.2 0.081 0.657 22.5

SiO2 in main steam μg/L 20 2.9 49 98.0

2007.8-2008.9

SiO2, organism, CO2 and other impurities in condensate couldn’t be removed after powdex. It is just depended on boiler blowdown. This is the main reason of high conductivity in steam.

Steam quality of unit 8 before retrofitting

Page 35: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Testing Item Unit Standard Value

Min. Max. Qualified Rate

(%)

DO in condensate μg/L 30 10.8 22.4 100

Conductivity in condensate μS/cm 0.3 0.120 0.258 100

DO in feed-water μg/L 7 2.8 6.8 100

Conductivity in feed water μS/cm 0.2 0.104 0.195 100

SiO2 in feed water μg/L 20 5.6 12.5 100

Conductivity in boiler water μS/cm 1.5 0.126 0.256 100

SiO2 in boiler water μg/L 200 58.6 125 100

Conductivity in main steam μS/cm 0.2 0.081 0.159 100

SiO2 in main steam μg/L 20 4.8 12.4 100

2009.3

After retrofitting, conductivity in the system decreased clearly. The effluent quality of high speed mixed beds is still good after nearly 1 month operation. It achieved the desired results.

Steam quality of unit 8 after retrofitting

Page 36: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Thanks for your Thanks for your

attentionattention !!

Page 37: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Welcome to ChinaWelcome to China !!

Welcome to XianWelcome to Xian !!

Welcome to TPRIWelcome to TPRI !!

Page 38: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Wenhua Tian : 86-029-

82102246 ( Office)

86-13991302260

Email :[email protected]

Huiyong He : 86-029-

82102570 ( Office)

86-13609111635

Email :[email protected]

Page 39: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Mixed Bed

Cylindrical MB

Page 40: The 2 nd  annual Air-Cooled Condenser User’s Group Meeting

Methods to decrease DO

Strengthen the welding management and improve its quality, try to decrease the air leakage of vacuum

System retrofitting----Case

The condensate tank was combined to the exhaust air The condensate tank was combined to the exhaust air cooling device. After through the nozzle, the makeup cooling device. After through the nozzle, the makeup water goes to the throat of exhaust device. It can lead to water goes to the throat of exhaust device. It can lead to an increase of the secondary removal of oxygen in an increase of the secondary removal of oxygen in returned condensate.returned condensate.