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7/31/2019 Odudimu Certification Scenerio
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Presentation on kiln and Mill Incidents
June 2012
CEMENT
WAPCO Nigeria Ewekoro 1
Name: ODUDIMU, OLUTAYO OLUGBENGA
Plant: EWEKORO 1
Function: CCRO
Experience: 7 yearsBackground: MECHANICAL ENGINEERING
CRO Certification session
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INTRODUCTION
When operating the best designed and most stable plant, theoperator may face an emergency situation once in a while which
requires immediate and drastic action. Quick and appropriate
reaction is extremely important to prevent serious damage to the
kiln and related equipment. In such cases, the Central Control
Room Operator must ignore the normal criteria for stable operation
and concentrate on getting full control of the immediate,
dangerous situation. Most Important in such a situation is of
course that the operator tries to keep his / her head cool.
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CONTENTS
Page
Kiln Scenario1: Clinker Conveyor Stoppage 4 - 12
Kiln Scenario 2: Cold Kiln 13 22
Kiln Scenario 3: Burning Zone Ring Fallout 23 - 31
Mill Scenario1: Limestone Failure / Pile Change over 32 - 37
Mill Scenario 2: VRM fill up 38 - 43
Mill Scenario 3: Mill Feed Belt Stopped 44 - 49
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KILN SCENERIO 1:Clinker Conveyor Stoppage
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Clinker Conveyor Stoppage
On the 22nd December 2011 at 5:30pm, Methods Inspector on
routine inspection noticed three (3) bad rollers on the apron clinkerconveyor and immediately activated the emergency switch to
prevent damage to the conveyor.
The sudden stoppage led to the stoppage of cooler breaker
hammer and cooler drives which eventually force down the kiln
drive to minimum speed (0.36rpm)
One very bad roller was replaced within four minutes, clinker
transport conveyor and cooler drives ran for about 10 minutes to
reduce the materials in the cooler and repositioning for the
remaining two bad rollers, which was completed after another 5
minutes.
CONSEQUENCE
Thermal damage to the cooler components.
KILN SCENERIO 1:Clinker Conveyor Stoppage
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Date 6
KILN SCENERIO 1:Clinker Conveyor Stoppage
Incident Date: 22nd December 2011
Time : 5:30pm to 5:50pm
Shift: Day Shift
BEFORE THE INCIDENT DURING THE INCIDENT
180 Kiln Feed in tph 120
Main Burner Fuel in Nm3/hr 4024 Main Burner Fuel in Nm3/hr 3610
Calciner Fuel in Nm3/hr 6470 Calciner Fuel in Nm3/hr 4176
ID fan damper in % 45 ID fan damper in % 35
Kiln Speed in rpm 3.4 Kiln Speed in rpm 0.36
Cooler Speed in stroke/min 15.1 Cooler Speed in stroke/min 0
Preheater Exit
Temperature in degree 360 Preheater Exit Temperature 405
Cyclone 4 Temperature 845 Cyclone 4 Temperature 850
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Clinker Conveyor StoppageActions taken Significance
Immediate Selection of kiln / Cooler built in
interlocking as in EWE-PRD-K-043
To increase the interlocking time before stopping the kiln
when cooler is not running
kiln feed reduced gradually from 180tph to 120
tph
To prevent poor heat exchange between gas and
material and unstable burning zone as a result of high
volume loading in the kiln. To prevent material over -
spilling from the backend.
Main burner fuel, calciner fuel, ID fan draft were
reduced stepwise
To prevent overheating of the burning zone andmaintain constant free lime, maintain constant
calcination to prevent shift in the burning zone andmaintain constant oxygen and in excess at the kilnbackend and at tower exit.
Continuous shooting of cooler shut blasters / air
cannons
To move the hot materials at the CIS section of thecooler forward and prevent snowman formation in thecooler
Missing bolts on the conveyor replaced by
Mechanical crew
To prevent deformation of the apron conveyor
Clinker Conveyor, clinker breaker hammer andcooler drives stated back as in EWE-PRD-K-029
Kiln speed gradually increased to maintain kiln
speed feed ratio
To maintain constant volume loading
Kiln ramp up starts after stability have beenattained using SOP for ramp up i.e. EWE-PRD-K-032
To optimize the operation.
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Clinker Conveyor Stoppage (Event Trend from ECS)
Kiln Speed
Left Grate
Center Grate
Right Grate
Pressure after ID fan
Hood Pressure
Kiln Feed
Calciner Burner Fuel
Main Burner Fuel
Compartment 1 PressureID fan Damper
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Preheater Outlet Temp
ID fan Damper
Kiln Torque
Cooler Speed
Kiln Feed Flow
Apron Conveyor Current
Kiln Speed Burning Zone Temp
Kiln Hood Temp
Clinker Conveyor Stoppage (Event trend from IP 21)
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ID fan Damper
Cyclone 4 temp
Kiln Feed
ain Burner Gas Flow
Calciner Burner Gas Flow
Pressure after ID fan
Compartment 1 Pres.
Apron Conveyor Current
Clinker Conveyor Stoppage (Event trend from IP 21)
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Clinker Conveyor Stoppage (Event trend from IP 21)Burning Zone Temp
Kiln Speed
Calciner gas Flow
ID fan Damper
ID fan outlet Pressure
Kiln Feed flow
Cooler Centre Grate
Apron Conveyor Current
Cooler Left & Right Grate
Compartment 1 Pres.
Preheater Exit Temp
Kiln Inlet temperature
Compartment 2 Pres.
Kiln Hood Temp.
Cyclone 4 Temperature
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Learning points
Kiln Coach Comment and Recommendation
The operator needs to be highly composed, take fast and good
decisions and be attentive to useful information to be able to tackleany emergency emanating from plant operation
.
Good action to save the kiln. The CRO must be well informed of the
plant SOP and always at alert to manage the emergency condition.
Iduh Lucky (Kiln Coach)
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KILN SCENERIO 2: COLD KILN
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On the 29th May 2012 between 8:10am and 9:20am, there was
increase in the Carbon II Oxide (CO) level at the Preheater Exit ofthe kiln from 0.0 % to 0.05% (500ppm) leading to slight cooling of
the burning zone.
During the first appearance of the CO at the preheater exit, the
Induced Draft fan damper was opened gradually to vent the
system. Then, the feed and the speed were later reduced.
As the material got to the burning zone, there was sharp drop in
the in the secondary air temperature, burning zone temperature
and cooler compartment 1 undergrate pressure.
KILN SCENERIO 2:COLD KILN
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INDICATORS Appearance of CO at the preheater exit analyser
Decrease in the burning zone
Decrease in the NOx level
Decrease in burning zone temperature and secondary airtemperature.
CONSEQUENCES AND DANGER
The presence of CO results from an incomplete combustion with therelease of unburned particles falling into the material load. Theconsequences are:
Local area of reducing condition
Kiln feed end chamber build up
Formation of sulphate ring
Easier SO3 Volatilization
Higher heat consumption.Date 15
KILN SCENERIO 2:COLD KILN
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KILN SCENERIO : COLD KILN
Incident Date: 29th May 2012
Time : 8:20am - 9:00am
Shift: Day Shift of 29th May 2012
BEFORE THE INCIDENT DURING THE INCIDENT
kiln Speed in tph 3.6 kiln Speed 3.3
Kiln Feed in rpm 200 Kiln Feed 185
Cyclone 4 temperature 846 Cyclone 4 temperature 865ID fan damper 81 ID fan damper 85
Calciner Fuel 7621 Calciner Fuel 7539
Main Burner Fuel 4305 Main Burner Fuel 4355
Burning Zone Temperature 1421 Burning Zone Temperature 1178
Preheater Exit CO level in % 0 Preheater Exit CO level in % 0.05
Preheater Exit Oxygen level in % 3.9Preheater Exit Oxygen level in% 4.1
Preheater Exit NOx level in ppm 348 Preheater Exit NOx level in ppm 228
Preheater Exit Temperature 350 Preheater Exit Temperature 354
Compartment 1 Pressure 63 Compartment 1 Pressure 61
Cooler Speed 21.1 Cooler Speed 15.5
Kiln SHC 776.81 Kiln SHC 846.25
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Quality Parameter on 29th May 2012
Date 17
Kiln Feed
TIME LSF % SR % AR % C3SSO3/ALKALIS %
RES(100um)
RES(200um)
8am 100.39 2.64 1.35 75.8 0.52 11.01 2.16
10am
12am 99.37 2.71 1.34 74.02 0.5 11.56 2.16
2am
Clinker
TIME fCao % LSF % LW C3S C2S C3A SO3
8am 2.97 91.14 1.28 44.46 32.66 6.41 0.13
10am 4.42 101.19 1.26 58.66 14.89 6.01 0.14
12am 2.74 98.4 1.31 61.24 15.51 6.18 0.12
2am 2.46 99.45 1.29 59.97 12.06 5.63 0.11
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COLD KILNActions taken Significance
ID fan damper increased gradually from 80% to
86% as in EWE-PRD-K-023E
To improve the efficiency of combustion and clear the
CO formation in the kiln
Kiln Feed and Kiln Speed reduced gradually
from 200tph and 3.6 rpm to 185 tph and 3.3 rpm
respectively.
The reduction in speed was to increase the material
retention time in the kiln and to raise the burning zone
temperature and reduction in the feed was to reduce the
kiln volume loading
Reduced Induced draft fan damper opening To maintain backend temperature, improved the burning
zone temperature .
Slight Increase in main burner fuel rate To raise the burning zone temperature and lowerpercentage oxygen at the inlet
Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth
Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth
Clinker diverted to the clinker dump Not to pollute the clinker in the silo
Kiln ramp up starts after the kiln had heated up
using SOP for ramp up as in EWE-PRD-K- 032
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Burning zone Temp
Compartment 1 Pres
Cooler Speed
Preheater Exit Temp
Cyclone 4 Temp
Preheater Oxygen
Preheater CO
Main Burner Fuel
Calciner Fuel
ID fan Damper
Kiln Speed
Kiln Feed
Kiln SHC
KILN SCENERIO 2:COLD KILN
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KILN SCENERIO 2:COLD KILN
ID fan damper
Kiln inlet Oxygen
Preheater O2
Preheater COPreheater NOx
Kiln Inlet Temp
Kiln Inlet CO
Kiln Inlet NOx
Kiln TorqueKiln Load
Burning Zone Temp
Kiln HoodTemp
Pressure after ID fan
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Learning points
CO presence at the preheater if not properly handled can lead to kiln flush
and lower production rate.
To always maintain stable operating parameter in order to prevent shift in
burning zone.
To always stabilize cooler operation to prevent fluctuation in secondary air(kiln hood) temperature and tertiary air temperature
The operator needs to be highly composed, take fast and good decisions
and be attentive to useful information to be able to tackle any emergency
emanating from plant operation
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Kiln Coach Comment and Recommendation
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KILN SCENERIO 3: BURNING ZONE RING
FALLOUT
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Burning Zone Ring Fallout
On the 17th June 2012 between 8:00pm and 9:00pm, Burning
Zone ring break loose in the kiln leading to slight cooling of theburning zone.
Before the incident, the speed was on maximum speed 3.6 rpm to
allow for the regular flow of material into the cooler as a result of
ring impeding the flow of feed (material) in the kiln. This was done
to achieving high cooler bed for optimal heat recuperation.
As the coating drops, the kiln speed, kiln feed and ID fan damper
were reduced for higher retention time in the kiln, and cooler
speed reduced to maintain constant cooler bed depth for optimal
heat recuperation while the main burner fuel was slightly
increased.
Further reduction in kiln feed was later done to raise the burning
zone temperature.
KILN SCENERIO 3:BURNING ZONE RING FALLOUT
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INDICATORS Sudden change in the kiln drive amperage. There is a steep
increase in the kiln power followed by gradual drop in kiln power.
As power drops, kiln exit NOx and burning zone temperaturedecreases.
Change in shell temperature on the kiln shell temperature scanner
Large lumps observed at the burning zone after few minutes
CONSEQUENCES AND DANGER
Thermal damage to the cooler components.
Overloading of the cooler with unburned feed
Red hot clinker will leave the cooler damaging the upstream equipment
Large pieces may jam the cooler hammer crusher
Large quantities of material in burning zone resulting in cooling of burningzone,
Damage to the cooler drive and grates Date 25
KILN SCENERIO 3:BURNING ZONE RING FALLOUT
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BURNING ZONE RING FALLOUT
Incident Date: 17th June 2012
Time : 8pm - 9:00pm
Shift: Night Shift of 17th June 2012
BEFORE THE INCIDENT DURING THE INCIDENT
Kiln Feed in tph 150 Kiln Feed in tph 135
Main Burner Fuel in Nm3/hr 3895 Main Burner Fuel in Nm3/hr 4015
Calciner Fuel in Nm3/hr 6345 Calciner Fuel in Nm3/hr 5811
ID fan damper in % 75 ID fan damper in % 50
Kiln Speed in rpm 3.6 Kiln Speed in rpm 3.0
Cooler Speed in stroke/min 18 Cooler Speed in stroke/min 14.2
Preheater Exit Temperature 358 Preheater Exit Temperaure 360
Cyclone 4 Temperature 840 Cyclone 4 Temperature 860
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Burning Zone Ring FalloutActions taken Significance
kiln speed was first reduced and later kiln feedas in EWE-PRD-K-044 The reduction in speed was to increase the materialretention time in the kiln and to raise the burning zone
temperature and reduction in the feed was to reduce
the kiln volume loading
Reduced Induced draft fan damper opening To maintain backend temperature, improved the
burning zone temperature .
Slight Increase in main burner fuel rate To raise the burning zone temperature and lowerpercentage oxygen at the inlet
Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth
Patroller called to carried out inspection toensure that there was no damage toequipment and accident on personnel
Kiln ramp up starts after the kiln had heated
up using SOP for ramp up as in EWE-PRD-K-032
B i Z Ri F ll
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Burning Zone Ring Fallout
Kiln Speed
Main burner gas Flow
Kiln Feed
Preheater Analyser NOx
Kiln Torque
ID fan damper
Calciner gas flow
Burning Zone Temp
Preheater Outlet Temp
Cyclone 4 Temp
B i Z Ri F ll t
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Burning Zone Ring Fallout
Kiln inlet NOx
Burning Zone Temp
Preheater Exit Oxygen
Torque
Kiln Feed
Hood Pressure Temp
Cyclone 4 Temp
Calciner Burner Fuel
Main Burner Fuel
Compartment 1 Pressure
Kiln Speed
Central Grate Speed.
Kiln Load
ID fan damper
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Learning points
To always observe burning zone temperature and comparing with it NOxmeasurement, kiln torque and kiln load.
To follow up with laboratory in the examination of the chemistry of the kiln
feed including dust return quantity for possible elimination of ring
formation
To always maintain stable operating parameter in order to prevent shift in
burning zone.
To always stabilize cooler operation to prevent fluctuation in secondary air
(kiln hood) temperature.
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Kiln Coach Comment and Recommendation
Good reaction except for the feed, although, it was due to
the ring. But let us thereafter maintain constant feed to
speed ratio
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MILL SCENERIO 1: Limestone failure /Chute Blockage
MILL SCENERIO 1 Limestone fail re /
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INTRODUCTION
On the 23th December 2011 at 9:30pm, the limestone reclaimer
went on manual trip. The patroller was called to investigate the
cause of the manual trip and make the reclaimer available for mill
operation. It was discovered that there was chute blockage in
reclaimer discharge chute to BC04 belt conveyor.
The de - blocking of the chute was supervised by the Patroller
while other operational controls to prevent incident stoppage on
the mill was carried out at Central Control Room.
CONSEQUENCE
The consequence of feed failure to the mill is excessivevibration which may damage the internal components and the
roller rocker arms.
MILL SCENERIO 1: Limestone failure /Chute Blockage
MILL SCENERIO 1 Limestone failure /
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MILL SCENERIO 1: Limestone failure /Chute Blockage
Incident Date: 23rd December 2011
Time : 9:35pm to 10:05pm
Shift: Night Shift
BEFORE THE INCIDENT DURING THE INCIDENT
Hot Air damper in % 100 Hot Air damper in % 0
Recirculation damper in % 28.6 Recirculation damper in % 96
Raw feed to the mill in Tph 280 Raw feed to the mill in Tph 0
Mill fan Power in Kilowatt 3153 Mill fan Power in Kilowatt 2842
Mill motor Powerin Kilowatt 1536 Mill motor Powerin Kilowatt 110
Mill fan damper in % 58.4 Mill fan damper in % 38.9
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Limestone Failure/ Chute Blockage
Actions taken Significance
Raised the grinding roller as in EWE
PRD
K - 017
To prevent mill vibration as a result of metal to metalcontact between the mill table and the grinding roller
Stop hot gas generator , VRM hot air damper
closed
To prevent overheating of the upstream mill equipment
and damage to the separator bearing and mill fan
impeller and bearing.
Open the mill recirculation damper and slightly
reduced the mill fan damper.
To maintain stable sensible / latent heat in the mill in
preparation for mill start up.
Patroller called to carried out inspection and to
de-block the chute and ensuring that there is
no damage to equipment and accident on
personnel
Grinding Commences and operation stabilized
minutes later as in EWE-PRD-K-006
Limestone Failure / Chute Blockage
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Limestone Failure / Chute Blockage
Mill Motor power
Mill Differential PressureLimestone Hopper Level
Fresh feed to VRM
Mill Vibration Cyclone Differential Pressure
Mill Fan Power
Hot air damper positionRecirculation damper
ot Gas Generator gas flowMill Outlet Temp
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Learning points
The operator needs to be highly attentive to be able to tackle any
emergency emanating from plant operation
Kiln Coach Comment and Recommendation
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MILL SCENERIO 2: MILL FILLED UP
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MILL SCENERIO 2: MILL FILLED UP
Incident Date: 24th December 2011
Time : 9:30pm to 9:50 pm
Shift: Night Shift
BEFORE THE INCIDENT DURING THE INCIDENT
Mill differential Pressure in mbar 90 Mill differential Pressure in mbar 121.8
Feed to the mill in tph 286 Feed to the mill in tph 310
Raw mill outlet Temp. in degree 72.3 Raw mill outlet Temp. in degree 63.5
Mill vibration in mm/s 7.9 Mill vibration in mm/s 6.4
Mill motor power in kilowatt 1537 Mill motor power in kilowatt 2221
Mill Product Elevator Current in % 52 Mill Product Elevator Current in % 56
Cyclone differential Pressure in mbar 6.9 Cyclone differential Pressure in mbar 5.3
Hydraulic Grinding Pressure in barab 860 Hydraulic Grinding Pressure in barab 920
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Mill (VRM) Filled Up
OBSERVATIONS
Increase in mill differential pressure
Increase in VRM mill active power
Decrease in cyclone differential pressure and mill airflow
Decrease in mill outlet temperature (R1M01N5)
Increase in mill reject elevator current (R1J05)
Increase in the mill product elevator current (W1A10)
Mill (VRM) Filled Up
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Mill (VRM) Filled Up
Mill Feed Mill Outlet TempMill Differential Pressure
Mill Motor PowerMill VibrationMill Inlet Temperature
Grinding Pressure
Mill Fan Power
VRM reject elevator Current
Mill Product Elevator Current
Mill (VRM) Fill d U
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Mill (VRM) Filled Up
Actions taken Significance
Grinding roller pressure increased from 860barabs to 920 barabs as in EWE-PRD-K-018
To increase grinding efficiency of the material.
Feed to the mill changed from automatic mode
to manual mode and the feed decreased by 20
tph
To reduced the material coming into the mill.
Mill fan damper opening increased from 52 %
to 62 % with increase in the heat input to the
mill
To reduce VRM internal circulation and lift the material insuspension
Operation later stabilized and feed to the mill
changed from manual mode to automatic
mode.
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Learning points
Reclaiming operation to be stabilized to prevent fluctuation in mill
operation.
The operator needs to be highly composed, take fast and good
decisions and be attentive to useful information to be able to tackle
any emergency emanating from plant operation
Kiln Coach Comment and Recommendation
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MILL SCENERIO 3: MILL FEED BELT STOPPED
MILL SCENERIO 3: MILL FEED BELT STOPPED
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Mill Feed Belt R1J01 Stopped INTRODUCTION
On the 24th April 2012 at 6:00am the mill feed belt conveyor
R1J01 went on manual trip as a result of limestone that activated
the emergency rope leading to the sudden failure of feed into the
mill.
The Separator speed was quickly increased and mill fan damper
lowered to allow materials in suspension to drop on the mill table
since the roller response time when raised was about 90 seconds
which can cause excessive vibration when roller was not fully lifted
up. Also, the heat input into the mill was gradually reduced. The
Patroller called to investigate the cause of the manual trip.
CONSEQUENCE
The consequence of feed failure to the mill is excessivevibration which may damage the internal components and theroller rocker arms.
MILL SCENERIO 3: MILL FEED BELT STOPPED
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MILL SCENERIO 3: MILL FEED BELT STOPPED
Incident Date: 24th April 2012
Time : 6:00am to 6:05 am
Shift: Night Shift
BEFORE THE INCIDENT DURING THE INCIDENT
Mill Differential Pressure inmbar 103.4
Mill Differential Pressure inmbar 66.7
Feed to the mill in tph 358 Feed to the mill in tph 0
Mill outlet temperature indegree 62
Mill outlet temperature indegree 106.4
Mill motor power in kilowatt 1848 Mill motor power in kilowatt 123
Separator Speed in % 73.4 Separator Speed in % 92.6Mill fan damper in % 68 Mill fan damper in % 46.8
Reject Elevator Current in % 42.9 Reject Elevator Current in % 40.2
Hot Air damper position in % 100 Hot Air damper position in % 0
Mill Vibration in mm/s 6.7 Mill Vibration in mm/s 0.9
Recirculation damper in % 0 Recirculation damper in % 95
MILL FEED BELT STOPPED
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Raw feed to the Mill
Recirculation damper
Separator Speed
Hot air damper to mill
Mill fan damper
Raw Mill Act Power
Mill Outlet temp Mill Vibration
Mill Differential Press.
Raw mill inlet temp
Cyclone Differential Press.
Grinding Pressure
VRM reject Elevator
Pressure after ID fan
Mill Feed Belt R1J01 Stopped
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Mill Feed Belt R1J01 Stopped
Actions taken Significance
Grinding roller automatically raised, though the
response time was low as in EWE PRD K
- 017
Separator speed increased from 73.4 % to
92.6% while the Mill fan damper opening
reduced from 68 % to 48 % with reduction in
the heat input to the mill
To prevent mill vibration as a result of metal to metalcontact between the mill table and the grinding rollerand to reduce VRM internal circulation and lift thematerial in suspension
Stop hot gas generator , VRM hot air damper
closed
To prevent overheating of the upstream mill equipment
and damage to the separator bearing and mill fan
impeller and bearing.
Open the mill recirculation damper To maintain recirculate the heat mill in preparation formill start up, and to prevent turbulence in the kiln
Patroller called to carried out inspection to
ensure that there was no damage to equipment
and accident on personnel
Mill feed and other upstream conveyor started
back
Grinding Commences and operation stabilizedminutes later.
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Learning points
The operator needs to be highly attentive to be able to tackle any
emergency emanating from plant operation.
Kiln Coach Comment and Recommendation
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Thank you
Engr. ODUDIMU Olutayo Olugbenga