Odudimu Certification Scenerio

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    Presentation on kiln and Mill Incidents

    June 2012

    CEMENT

    WAPCO Nigeria Ewekoro 1

    Name: ODUDIMU, OLUTAYO OLUGBENGA

    Plant: EWEKORO 1

    Function: CCRO

    Experience: 7 yearsBackground: MECHANICAL ENGINEERING

    CRO Certification session

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    INTRODUCTION

    When operating the best designed and most stable plant, theoperator may face an emergency situation once in a while which

    requires immediate and drastic action. Quick and appropriate

    reaction is extremely important to prevent serious damage to the

    kiln and related equipment. In such cases, the Central Control

    Room Operator must ignore the normal criteria for stable operation

    and concentrate on getting full control of the immediate,

    dangerous situation. Most Important in such a situation is of

    course that the operator tries to keep his / her head cool.

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    CONTENTS

    Page

    Kiln Scenario1: Clinker Conveyor Stoppage 4 - 12

    Kiln Scenario 2: Cold Kiln 13 22

    Kiln Scenario 3: Burning Zone Ring Fallout 23 - 31

    Mill Scenario1: Limestone Failure / Pile Change over 32 - 37

    Mill Scenario 2: VRM fill up 38 - 43

    Mill Scenario 3: Mill Feed Belt Stopped 44 - 49

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    KILN SCENERIO 1:Clinker Conveyor Stoppage

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    Clinker Conveyor Stoppage

    On the 22nd December 2011 at 5:30pm, Methods Inspector on

    routine inspection noticed three (3) bad rollers on the apron clinkerconveyor and immediately activated the emergency switch to

    prevent damage to the conveyor.

    The sudden stoppage led to the stoppage of cooler breaker

    hammer and cooler drives which eventually force down the kiln

    drive to minimum speed (0.36rpm)

    One very bad roller was replaced within four minutes, clinker

    transport conveyor and cooler drives ran for about 10 minutes to

    reduce the materials in the cooler and repositioning for the

    remaining two bad rollers, which was completed after another 5

    minutes.

    CONSEQUENCE

    Thermal damage to the cooler components.

    KILN SCENERIO 1:Clinker Conveyor Stoppage

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    KILN SCENERIO 1:Clinker Conveyor Stoppage

    Incident Date: 22nd December 2011

    Time : 5:30pm to 5:50pm

    Shift: Day Shift

    BEFORE THE INCIDENT DURING THE INCIDENT

    180 Kiln Feed in tph 120

    Main Burner Fuel in Nm3/hr 4024 Main Burner Fuel in Nm3/hr 3610

    Calciner Fuel in Nm3/hr 6470 Calciner Fuel in Nm3/hr 4176

    ID fan damper in % 45 ID fan damper in % 35

    Kiln Speed in rpm 3.4 Kiln Speed in rpm 0.36

    Cooler Speed in stroke/min 15.1 Cooler Speed in stroke/min 0

    Preheater Exit

    Temperature in degree 360 Preheater Exit Temperature 405

    Cyclone 4 Temperature 845 Cyclone 4 Temperature 850

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    Clinker Conveyor StoppageActions taken Significance

    Immediate Selection of kiln / Cooler built in

    interlocking as in EWE-PRD-K-043

    To increase the interlocking time before stopping the kiln

    when cooler is not running

    kiln feed reduced gradually from 180tph to 120

    tph

    To prevent poor heat exchange between gas and

    material and unstable burning zone as a result of high

    volume loading in the kiln. To prevent material over -

    spilling from the backend.

    Main burner fuel, calciner fuel, ID fan draft were

    reduced stepwise

    To prevent overheating of the burning zone andmaintain constant free lime, maintain constant

    calcination to prevent shift in the burning zone andmaintain constant oxygen and in excess at the kilnbackend and at tower exit.

    Continuous shooting of cooler shut blasters / air

    cannons

    To move the hot materials at the CIS section of thecooler forward and prevent snowman formation in thecooler

    Missing bolts on the conveyor replaced by

    Mechanical crew

    To prevent deformation of the apron conveyor

    Clinker Conveyor, clinker breaker hammer andcooler drives stated back as in EWE-PRD-K-029

    Kiln speed gradually increased to maintain kiln

    speed feed ratio

    To maintain constant volume loading

    Kiln ramp up starts after stability have beenattained using SOP for ramp up i.e. EWE-PRD-K-032

    To optimize the operation.

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    Clinker Conveyor Stoppage (Event Trend from ECS)

    Kiln Speed

    Left Grate

    Center Grate

    Right Grate

    Pressure after ID fan

    Hood Pressure

    Kiln Feed

    Calciner Burner Fuel

    Main Burner Fuel

    Compartment 1 PressureID fan Damper

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    Preheater Outlet Temp

    ID fan Damper

    Kiln Torque

    Cooler Speed

    Kiln Feed Flow

    Apron Conveyor Current

    Kiln Speed Burning Zone Temp

    Kiln Hood Temp

    Clinker Conveyor Stoppage (Event trend from IP 21)

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    ID fan Damper

    Cyclone 4 temp

    Kiln Feed

    ain Burner Gas Flow

    Calciner Burner Gas Flow

    Pressure after ID fan

    Compartment 1 Pres.

    Apron Conveyor Current

    Clinker Conveyor Stoppage (Event trend from IP 21)

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    Clinker Conveyor Stoppage (Event trend from IP 21)Burning Zone Temp

    Kiln Speed

    Calciner gas Flow

    ID fan Damper

    ID fan outlet Pressure

    Kiln Feed flow

    Cooler Centre Grate

    Apron Conveyor Current

    Cooler Left & Right Grate

    Compartment 1 Pres.

    Preheater Exit Temp

    Kiln Inlet temperature

    Compartment 2 Pres.

    Kiln Hood Temp.

    Cyclone 4 Temperature

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    Learning points

    Kiln Coach Comment and Recommendation

    The operator needs to be highly composed, take fast and good

    decisions and be attentive to useful information to be able to tackleany emergency emanating from plant operation

    .

    Good action to save the kiln. The CRO must be well informed of the

    plant SOP and always at alert to manage the emergency condition.

    Iduh Lucky (Kiln Coach)

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    KILN SCENERIO 2: COLD KILN

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    On the 29th May 2012 between 8:10am and 9:20am, there was

    increase in the Carbon II Oxide (CO) level at the Preheater Exit ofthe kiln from 0.0 % to 0.05% (500ppm) leading to slight cooling of

    the burning zone.

    During the first appearance of the CO at the preheater exit, the

    Induced Draft fan damper was opened gradually to vent the

    system. Then, the feed and the speed were later reduced.

    As the material got to the burning zone, there was sharp drop in

    the in the secondary air temperature, burning zone temperature

    and cooler compartment 1 undergrate pressure.

    KILN SCENERIO 2:COLD KILN

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    INDICATORS Appearance of CO at the preheater exit analyser

    Decrease in the burning zone

    Decrease in the NOx level

    Decrease in burning zone temperature and secondary airtemperature.

    CONSEQUENCES AND DANGER

    The presence of CO results from an incomplete combustion with therelease of unburned particles falling into the material load. Theconsequences are:

    Local area of reducing condition

    Kiln feed end chamber build up

    Formation of sulphate ring

    Easier SO3 Volatilization

    Higher heat consumption.Date 15

    KILN SCENERIO 2:COLD KILN

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    KILN SCENERIO : COLD KILN

    Incident Date: 29th May 2012

    Time : 8:20am - 9:00am

    Shift: Day Shift of 29th May 2012

    BEFORE THE INCIDENT DURING THE INCIDENT

    kiln Speed in tph 3.6 kiln Speed 3.3

    Kiln Feed in rpm 200 Kiln Feed 185

    Cyclone 4 temperature 846 Cyclone 4 temperature 865ID fan damper 81 ID fan damper 85

    Calciner Fuel 7621 Calciner Fuel 7539

    Main Burner Fuel 4305 Main Burner Fuel 4355

    Burning Zone Temperature 1421 Burning Zone Temperature 1178

    Preheater Exit CO level in % 0 Preheater Exit CO level in % 0.05

    Preheater Exit Oxygen level in % 3.9Preheater Exit Oxygen level in% 4.1

    Preheater Exit NOx level in ppm 348 Preheater Exit NOx level in ppm 228

    Preheater Exit Temperature 350 Preheater Exit Temperature 354

    Compartment 1 Pressure 63 Compartment 1 Pressure 61

    Cooler Speed 21.1 Cooler Speed 15.5

    Kiln SHC 776.81 Kiln SHC 846.25

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    Quality Parameter on 29th May 2012

    Date 17

    Kiln Feed

    TIME LSF % SR % AR % C3SSO3/ALKALIS %

    RES(100um)

    RES(200um)

    8am 100.39 2.64 1.35 75.8 0.52 11.01 2.16

    10am

    12am 99.37 2.71 1.34 74.02 0.5 11.56 2.16

    2am

    Clinker

    TIME fCao % LSF % LW C3S C2S C3A SO3

    8am 2.97 91.14 1.28 44.46 32.66 6.41 0.13

    10am 4.42 101.19 1.26 58.66 14.89 6.01 0.14

    12am 2.74 98.4 1.31 61.24 15.51 6.18 0.12

    2am 2.46 99.45 1.29 59.97 12.06 5.63 0.11

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    COLD KILNActions taken Significance

    ID fan damper increased gradually from 80% to

    86% as in EWE-PRD-K-023E

    To improve the efficiency of combustion and clear the

    CO formation in the kiln

    Kiln Feed and Kiln Speed reduced gradually

    from 200tph and 3.6 rpm to 185 tph and 3.3 rpm

    respectively.

    The reduction in speed was to increase the material

    retention time in the kiln and to raise the burning zone

    temperature and reduction in the feed was to reduce the

    kiln volume loading

    Reduced Induced draft fan damper opening To maintain backend temperature, improved the burning

    zone temperature .

    Slight Increase in main burner fuel rate To raise the burning zone temperature and lowerpercentage oxygen at the inlet

    Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth

    Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth

    Clinker diverted to the clinker dump Not to pollute the clinker in the silo

    Kiln ramp up starts after the kiln had heated up

    using SOP for ramp up as in EWE-PRD-K- 032

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    Burning zone Temp

    Compartment 1 Pres

    Cooler Speed

    Preheater Exit Temp

    Cyclone 4 Temp

    Preheater Oxygen

    Preheater CO

    Main Burner Fuel

    Calciner Fuel

    ID fan Damper

    Kiln Speed

    Kiln Feed

    Kiln SHC

    KILN SCENERIO 2:COLD KILN

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    KILN SCENERIO 2:COLD KILN

    ID fan damper

    Kiln inlet Oxygen

    Preheater O2

    Preheater COPreheater NOx

    Kiln Inlet Temp

    Kiln Inlet CO

    Kiln Inlet NOx

    Kiln TorqueKiln Load

    Burning Zone Temp

    Kiln HoodTemp

    Pressure after ID fan

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    Learning points

    CO presence at the preheater if not properly handled can lead to kiln flush

    and lower production rate.

    To always maintain stable operating parameter in order to prevent shift in

    burning zone.

    To always stabilize cooler operation to prevent fluctuation in secondary air(kiln hood) temperature and tertiary air temperature

    The operator needs to be highly composed, take fast and good decisions

    and be attentive to useful information to be able to tackle any emergency

    emanating from plant operation

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    Kiln Coach Comment and Recommendation

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    KILN SCENERIO 3: BURNING ZONE RING

    FALLOUT

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    Burning Zone Ring Fallout

    On the 17th June 2012 between 8:00pm and 9:00pm, Burning

    Zone ring break loose in the kiln leading to slight cooling of theburning zone.

    Before the incident, the speed was on maximum speed 3.6 rpm to

    allow for the regular flow of material into the cooler as a result of

    ring impeding the flow of feed (material) in the kiln. This was done

    to achieving high cooler bed for optimal heat recuperation.

    As the coating drops, the kiln speed, kiln feed and ID fan damper

    were reduced for higher retention time in the kiln, and cooler

    speed reduced to maintain constant cooler bed depth for optimal

    heat recuperation while the main burner fuel was slightly

    increased.

    Further reduction in kiln feed was later done to raise the burning

    zone temperature.

    KILN SCENERIO 3:BURNING ZONE RING FALLOUT

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    INDICATORS Sudden change in the kiln drive amperage. There is a steep

    increase in the kiln power followed by gradual drop in kiln power.

    As power drops, kiln exit NOx and burning zone temperaturedecreases.

    Change in shell temperature on the kiln shell temperature scanner

    Large lumps observed at the burning zone after few minutes

    CONSEQUENCES AND DANGER

    Thermal damage to the cooler components.

    Overloading of the cooler with unburned feed

    Red hot clinker will leave the cooler damaging the upstream equipment

    Large pieces may jam the cooler hammer crusher

    Large quantities of material in burning zone resulting in cooling of burningzone,

    Damage to the cooler drive and grates Date 25

    KILN SCENERIO 3:BURNING ZONE RING FALLOUT

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    BURNING ZONE RING FALLOUT

    Incident Date: 17th June 2012

    Time : 8pm - 9:00pm

    Shift: Night Shift of 17th June 2012

    BEFORE THE INCIDENT DURING THE INCIDENT

    Kiln Feed in tph 150 Kiln Feed in tph 135

    Main Burner Fuel in Nm3/hr 3895 Main Burner Fuel in Nm3/hr 4015

    Calciner Fuel in Nm3/hr 6345 Calciner Fuel in Nm3/hr 5811

    ID fan damper in % 75 ID fan damper in % 50

    Kiln Speed in rpm 3.6 Kiln Speed in rpm 3.0

    Cooler Speed in stroke/min 18 Cooler Speed in stroke/min 14.2

    Preheater Exit Temperature 358 Preheater Exit Temperaure 360

    Cyclone 4 Temperature 840 Cyclone 4 Temperature 860

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    Burning Zone Ring FalloutActions taken Significance

    kiln speed was first reduced and later kiln feedas in EWE-PRD-K-044 The reduction in speed was to increase the materialretention time in the kiln and to raise the burning zone

    temperature and reduction in the feed was to reduce

    the kiln volume loading

    Reduced Induced draft fan damper opening To maintain backend temperature, improved the

    burning zone temperature .

    Slight Increase in main burner fuel rate To raise the burning zone temperature and lowerpercentage oxygen at the inlet

    Reduce Cooler grate speed To maximize and regularize heat recuperation andmaintain constant cooler clinker bed depth

    Patroller called to carried out inspection toensure that there was no damage toequipment and accident on personnel

    Kiln ramp up starts after the kiln had heated

    up using SOP for ramp up as in EWE-PRD-K-032

    B i Z Ri F ll

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    Burning Zone Ring Fallout

    Kiln Speed

    Main burner gas Flow

    Kiln Feed

    Preheater Analyser NOx

    Kiln Torque

    ID fan damper

    Calciner gas flow

    Burning Zone Temp

    Preheater Outlet Temp

    Cyclone 4 Temp

    B i Z Ri F ll t

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    Burning Zone Ring Fallout

    Kiln inlet NOx

    Burning Zone Temp

    Preheater Exit Oxygen

    Torque

    Kiln Feed

    Hood Pressure Temp

    Cyclone 4 Temp

    Calciner Burner Fuel

    Main Burner Fuel

    Compartment 1 Pressure

    Kiln Speed

    Central Grate Speed.

    Kiln Load

    ID fan damper

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    Learning points

    To always observe burning zone temperature and comparing with it NOxmeasurement, kiln torque and kiln load.

    To follow up with laboratory in the examination of the chemistry of the kiln

    feed including dust return quantity for possible elimination of ring

    formation

    To always maintain stable operating parameter in order to prevent shift in

    burning zone.

    To always stabilize cooler operation to prevent fluctuation in secondary air

    (kiln hood) temperature.

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    Kiln Coach Comment and Recommendation

    Good reaction except for the feed, although, it was due to

    the ring. But let us thereafter maintain constant feed to

    speed ratio

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    MILL SCENERIO 1: Limestone failure /Chute Blockage

    MILL SCENERIO 1 Limestone fail re /

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    INTRODUCTION

    On the 23th December 2011 at 9:30pm, the limestone reclaimer

    went on manual trip. The patroller was called to investigate the

    cause of the manual trip and make the reclaimer available for mill

    operation. It was discovered that there was chute blockage in

    reclaimer discharge chute to BC04 belt conveyor.

    The de - blocking of the chute was supervised by the Patroller

    while other operational controls to prevent incident stoppage on

    the mill was carried out at Central Control Room.

    CONSEQUENCE

    The consequence of feed failure to the mill is excessivevibration which may damage the internal components and the

    roller rocker arms.

    MILL SCENERIO 1: Limestone failure /Chute Blockage

    MILL SCENERIO 1 Limestone failure /

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    MILL SCENERIO 1: Limestone failure /Chute Blockage

    Incident Date: 23rd December 2011

    Time : 9:35pm to 10:05pm

    Shift: Night Shift

    BEFORE THE INCIDENT DURING THE INCIDENT

    Hot Air damper in % 100 Hot Air damper in % 0

    Recirculation damper in % 28.6 Recirculation damper in % 96

    Raw feed to the mill in Tph 280 Raw feed to the mill in Tph 0

    Mill fan Power in Kilowatt 3153 Mill fan Power in Kilowatt 2842

    Mill motor Powerin Kilowatt 1536 Mill motor Powerin Kilowatt 110

    Mill fan damper in % 58.4 Mill fan damper in % 38.9

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    Limestone Failure/ Chute Blockage

    Actions taken Significance

    Raised the grinding roller as in EWE

    PRD

    K - 017

    To prevent mill vibration as a result of metal to metalcontact between the mill table and the grinding roller

    Stop hot gas generator , VRM hot air damper

    closed

    To prevent overheating of the upstream mill equipment

    and damage to the separator bearing and mill fan

    impeller and bearing.

    Open the mill recirculation damper and slightly

    reduced the mill fan damper.

    To maintain stable sensible / latent heat in the mill in

    preparation for mill start up.

    Patroller called to carried out inspection and to

    de-block the chute and ensuring that there is

    no damage to equipment and accident on

    personnel

    Grinding Commences and operation stabilized

    minutes later as in EWE-PRD-K-006

    Limestone Failure / Chute Blockage

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    Limestone Failure / Chute Blockage

    Mill Motor power

    Mill Differential PressureLimestone Hopper Level

    Fresh feed to VRM

    Mill Vibration Cyclone Differential Pressure

    Mill Fan Power

    Hot air damper positionRecirculation damper

    ot Gas Generator gas flowMill Outlet Temp

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    Learning points

    The operator needs to be highly attentive to be able to tackle any

    emergency emanating from plant operation

    Kiln Coach Comment and Recommendation

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    MILL SCENERIO 2: MILL FILLED UP

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    MILL SCENERIO 2: MILL FILLED UP

    Incident Date: 24th December 2011

    Time : 9:30pm to 9:50 pm

    Shift: Night Shift

    BEFORE THE INCIDENT DURING THE INCIDENT

    Mill differential Pressure in mbar 90 Mill differential Pressure in mbar 121.8

    Feed to the mill in tph 286 Feed to the mill in tph 310

    Raw mill outlet Temp. in degree 72.3 Raw mill outlet Temp. in degree 63.5

    Mill vibration in mm/s 7.9 Mill vibration in mm/s 6.4

    Mill motor power in kilowatt 1537 Mill motor power in kilowatt 2221

    Mill Product Elevator Current in % 52 Mill Product Elevator Current in % 56

    Cyclone differential Pressure in mbar 6.9 Cyclone differential Pressure in mbar 5.3

    Hydraulic Grinding Pressure in barab 860 Hydraulic Grinding Pressure in barab 920

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    Mill (VRM) Filled Up

    OBSERVATIONS

    Increase in mill differential pressure

    Increase in VRM mill active power

    Decrease in cyclone differential pressure and mill airflow

    Decrease in mill outlet temperature (R1M01N5)

    Increase in mill reject elevator current (R1J05)

    Increase in the mill product elevator current (W1A10)

    Mill (VRM) Filled Up

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    Mill (VRM) Filled Up

    Mill Feed Mill Outlet TempMill Differential Pressure

    Mill Motor PowerMill VibrationMill Inlet Temperature

    Grinding Pressure

    Mill Fan Power

    VRM reject elevator Current

    Mill Product Elevator Current

    Mill (VRM) Fill d U

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    Mill (VRM) Filled Up

    Actions taken Significance

    Grinding roller pressure increased from 860barabs to 920 barabs as in EWE-PRD-K-018

    To increase grinding efficiency of the material.

    Feed to the mill changed from automatic mode

    to manual mode and the feed decreased by 20

    tph

    To reduced the material coming into the mill.

    Mill fan damper opening increased from 52 %

    to 62 % with increase in the heat input to the

    mill

    To reduce VRM internal circulation and lift the material insuspension

    Operation later stabilized and feed to the mill

    changed from manual mode to automatic

    mode.

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    Learning points

    Reclaiming operation to be stabilized to prevent fluctuation in mill

    operation.

    The operator needs to be highly composed, take fast and good

    decisions and be attentive to useful information to be able to tackle

    any emergency emanating from plant operation

    Kiln Coach Comment and Recommendation

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    MILL SCENERIO 3: MILL FEED BELT STOPPED

    MILL SCENERIO 3: MILL FEED BELT STOPPED

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    Mill Feed Belt R1J01 Stopped INTRODUCTION

    On the 24th April 2012 at 6:00am the mill feed belt conveyor

    R1J01 went on manual trip as a result of limestone that activated

    the emergency rope leading to the sudden failure of feed into the

    mill.

    The Separator speed was quickly increased and mill fan damper

    lowered to allow materials in suspension to drop on the mill table

    since the roller response time when raised was about 90 seconds

    which can cause excessive vibration when roller was not fully lifted

    up. Also, the heat input into the mill was gradually reduced. The

    Patroller called to investigate the cause of the manual trip.

    CONSEQUENCE

    The consequence of feed failure to the mill is excessivevibration which may damage the internal components and theroller rocker arms.

    MILL SCENERIO 3: MILL FEED BELT STOPPED

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    MILL SCENERIO 3: MILL FEED BELT STOPPED

    Incident Date: 24th April 2012

    Time : 6:00am to 6:05 am

    Shift: Night Shift

    BEFORE THE INCIDENT DURING THE INCIDENT

    Mill Differential Pressure inmbar 103.4

    Mill Differential Pressure inmbar 66.7

    Feed to the mill in tph 358 Feed to the mill in tph 0

    Mill outlet temperature indegree 62

    Mill outlet temperature indegree 106.4

    Mill motor power in kilowatt 1848 Mill motor power in kilowatt 123

    Separator Speed in % 73.4 Separator Speed in % 92.6Mill fan damper in % 68 Mill fan damper in % 46.8

    Reject Elevator Current in % 42.9 Reject Elevator Current in % 40.2

    Hot Air damper position in % 100 Hot Air damper position in % 0

    Mill Vibration in mm/s 6.7 Mill Vibration in mm/s 0.9

    Recirculation damper in % 0 Recirculation damper in % 95

    MILL FEED BELT STOPPED

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    Raw feed to the Mill

    Recirculation damper

    Separator Speed

    Hot air damper to mill

    Mill fan damper

    Raw Mill Act Power

    Mill Outlet temp Mill Vibration

    Mill Differential Press.

    Raw mill inlet temp

    Cyclone Differential Press.

    Grinding Pressure

    VRM reject Elevator

    Pressure after ID fan

    Mill Feed Belt R1J01 Stopped

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    Mill Feed Belt R1J01 Stopped

    Actions taken Significance

    Grinding roller automatically raised, though the

    response time was low as in EWE PRD K

    - 017

    Separator speed increased from 73.4 % to

    92.6% while the Mill fan damper opening

    reduced from 68 % to 48 % with reduction in

    the heat input to the mill

    To prevent mill vibration as a result of metal to metalcontact between the mill table and the grinding rollerand to reduce VRM internal circulation and lift thematerial in suspension

    Stop hot gas generator , VRM hot air damper

    closed

    To prevent overheating of the upstream mill equipment

    and damage to the separator bearing and mill fan

    impeller and bearing.

    Open the mill recirculation damper To maintain recirculate the heat mill in preparation formill start up, and to prevent turbulence in the kiln

    Patroller called to carried out inspection to

    ensure that there was no damage to equipment

    and accident on personnel

    Mill feed and other upstream conveyor started

    back

    Grinding Commences and operation stabilizedminutes later.

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    Date 49

    Learning points

    The operator needs to be highly attentive to be able to tackle any

    emergency emanating from plant operation.

    Kiln Coach Comment and Recommendation

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    Thank you

    Engr. ODUDIMU Olutayo Olugbenga