Upload
others
View
1
Download
0
Embed Size (px)
Citation preview
INTRODUCTION
Urea Deep Placement or UDP is the method of Deep placement (7-10 centimetres
below the soil surface) of urea briquettes, called Guti, near the roots of the rice plant
rather than spreading urea over the surface of the soil, which is the conventional
method. The Guti, which is the size of a mothball, slowly releases nitrogen
throughout the growing season. UDP are well-documented as superior nutrient
delivery systems compared with the traditional method of broadcasting urea. When
used to fertilize irrigated rice, briquettes are centred between 4 plants at a depth of
7-10 centimetres within 7 days after transplanting. Placement is conventionally done
either by hand or with a mechanical applicator. The results are: 1) Yields are
increased by 15-18 percent. 2) Fertilizer use is reduced by one-third. 3) Nitrogen
losses are reduced by 40 percent,
The technology allows for better absorption and efficiency of the fertilizer while
reducing runoff, and decreases the release of volatile greenhouse gas and
eliminates nitrification/ denitrification.
However, FDP technology is labour-intensive because fertilizer briquettes are hand-
placed near the root zone of rice plants. Further rising labor costs (close to $6 a day
during the season) makes the development of a mechanized & user friendly
applicator critical. This problem has delayed widespread farmer adoption. To
alleviate this issue, we developed a mechanical applicator for UDP.
The project includes designing and fabrication of the UDP applicator that performs
plunging of the urea briquettes at equal distances in the soil and that is easy to
operate and manoeuvre in paddy fields. The UDP applicator runs on a gasoline
powered engine and uses the Slider Crank Mechanism to Plunge urea briquettes
deep into the soil with fixed spacing.
With the help of UDP Applicator, the UDP technology can be successfully
implemented worldwide that would create huge impact on the agriculture around the
world increasing paddy productivity, reducing fertilizer consumption and
subsequently increasing GDP of paddy producing countries like India, Bangladesh
and Africa. Also, it will help reduce harmful emissions and help curb environmental
degradation.
The Urea Deep Placement Applicator or UDP Applicator is an automated version that
is run by a gasoline engine. A 197cc 3 HP Honda GK 200 Engine powers the
! 1
machine. The engine drives the plunging mechanism, picker mechanism as well as
the two lugged wheels through Chain Drives. The drive from the engine goes to the
gearbox via a friction clutch mounted on the crankshaft which can be disengaged to
disengage the mechanism. The gearbox is designed to provide the calculated speed
reduction to plunge urea briquettes at fixed distance. The gearbox transmits power to
the picker mechanism that has small buckets which picks-up urea briquettes from
the picker box and throws them in a pipe which delivers it under the plunger for it to
be plunged. The gearbox also transmits power to the crank of the slider-crank
plunger mechanism. The gear ratio of the picker and crank sprockets are such that
for every single rotation of the picker the crank will rotate 4 times since the picker
disc has 4 buckets on its periphery. The weight distribution of the machine
components is done to help the operator to manoeuvre it easily and such that it
balances itself in static as well as in dynamic conditions. It also has reduced risk of
toppling, even at high speeds. The wheels of the UDP Applicator have been selected
after several iterations. Two lugged wheels are used to propel the applicator in
forward direction and to provide sufficient friction or grip for the machine to prevent it
from slipping in the soil. The wheels can also provide movement to the machine on
concrete surfaces over short distances. A third Castor wheel that is located at the
back end of the machine performs three major functions: First, to give support to the
machine and keep it balanced, Secondly, the castor wheel helps in changing
direction of motion of the machine. It provides the advantage of Zero turning radius
to the machine, The machine pivots about any one of the lugged wheel and the
castor helps in turning the machine about the pivot with little effort. Lastly, the Castor
wheel acts as a furrow closing. That is, it covers the holes made by the plunger
during plunging operation by soil. The design of the UDP Applicator is shown below.
!
Fig. 1.0 design of udp applicator
! 2
LITERATURE REVIEW
1. Lupin M.S., Lazo J.R., N.D, et al, Briquetting, TP 963.4.U7B74
Results of tests by the International Fertilizer Development Center (IFDC) and
other organizations show that considerable improvement is achieved in the
agronomic efficiency of urea in wetland rice production by deep placement of
urea supergranules compared to broadcast application of urea prills. The
physical and chemical characteristics of urea make the material well suited for
production of urea supergranules by briquetting, which is an agglomeration
process using the application of pressure to powdered dry materials. Urea
briquettes of 0.8 to 2.0 grams produced by IFDC in a small briquetting
machine were of a good quality. Conceptual process designs were developed
for the manufacture of 1-to 2-gram urea briquettes considering different types
of urea feed material. The conceptual designs were used for developing cost
estimates for the production of uree briquettes. For briquetting plants added to
an existing urea complex, the estimated production cost premium for urea
briquettes is $14.5 to $20.3 per metric ton, depending upon plant capacity and
type of feed material. For a unit at a separate site, the estimated premium is
$36.8 per metric ton.
2. Khan A.U., Kiamco L., Tiangco V.,Fertilizer transfer to floodwater during deep
placement, IRPS No.96, Oct1983
This study indicates that presence of water during fertilizer placement plays a
major role in reducing fertilizer use efficiency in flooded rice fields. Fertilizer
applicators that have been developed in the past have transferred 40 to 70%
of the fertilizer to the floodwater during the placement operation.Five possible
ways of nitrogen transfer to floodwater are suggested. It was found that up to
40% of the placed fertilizer transfers to floodwater through dissolution during
transit froia the water surface to the furrow bottom. That was the major
avenue for fertilizer transfer.The second major transfer is when the fertilizer
solution and/or granules are pushed from the furrow bottom into the
floodwater as the furrow closes. Transfers due to nitrogen diffusion through
! 3
soil or through poorly closed furrows are not high. The authors argue that
minimizing nitrogen transfer to floodwater during fertilizer placement is the key
to improving fertilizer use efficiency in flooded rice fields. A deep placement
applicator concept for minimum transfer to floodwater is proposed. The paper
concludes that fertilizer dissolution and the dynamics of fertilizer solution in
flooded rice fields have not been fully understood and need further research
to improve fertilizer use efficiency.
! 4
PROBLEM FORMULATION AND METHODOLOGY
Stage 1: Prototype Designing
We started the design of the applicator with the intention to keep it simple, and
focused on easy fabrication, low cost, easy maintenance.
The applicator was designed keeping in mind the findings from the field visits to
Bangladesh & Ludhiana. It was clear that the machine needed to be able to run
between the planted rows of 20 cm width. We planned to make a machine with 2
powered front wheels and a single free rear wheel. The major challenge was to have
a machine with wheels distance as narrow as possible and yet be able to move
easily in deep wet mud. Also we did not want to increase the power requirement too
much and hence attempted this task with a low power input, as high power
requirement would significantly increase the operating costs and machine weight.
We identified the trans-planter and the power tiller as the 2 machines with similar
operating conditions as ours. Hence, we also studied them in great detail and
adopted certain aspects from their designs.
!
Fig 1.1 The first design
Inorder to provide mobility in wet soil without slipping we needed wheels that
provided sufficient traction and hence decided to have lugs attached. However, at
! 5
GearBox
Brique2ePicker
Engine
Wheel
Crank&Plunger
the same time, the wheels could not be allowed to sink too deep in the mud as this
would increase power requirement.
Another major design constraint we faced was that of machine width. We did not
want the side-powered lugged wheels to run over trans-planted paddy or previously
placed briquettes and dig them up. We thus decided that the powered wheels should
move in the rows adjacent to the one in which briquettes are being placed. The back
wheel would perform the furrow closing mechanism and cover the briquette
immediately after its placement therefore should be in the same row as the briquette
plunging mechanism.
Considering a plant row to row spacing of 6-8 inches, we had to maintain the spacing
between the front-powered wheels (inner to inner distance) to not more than 9
inches (with 3 inch wide wheels). We also decided to give an adjustability to the inter
wheel distance and provided an easy mechanism to do so for running the machine in
fields with greater crop spacing.
The narrow width would lead to instability of the machine: another cause of concern,
and to counter that we wanted to keep the center of gravity as low as possible to
ensure stability. However, the plunging mechanism’s requirements and ground
clearance needs meant that the crank’s center would have to be at a height of 70cm
above the bottom part of wheels. This height increase due to the plunging
mechanism has been a constant concern for us.
1.1 Power source –Gasoline Engine
Selecting the gasoline engine happened after weighing numerous pros and cons
versus diesel and battery options. The main reason for eliminating diesel was that of
weight increase. Diesel engines were much heavier and we could only find a
minimum weight of 44kg engine readily available in Delhi. The elimination of battery
was because of two reasons. Firstly, batteries are heavier, and secondly, they could
be riskier to use on wet paddy conditions. Hence, our choice for the first prototype
was a gasoline engine.
! 6
1.2 Gear Box
The engine & gearbox were both placed between the wheels. The plan was to
include the differential / clutch inside the gearbox at a later stage. Also the power
output for the crank would also be brought out from the same gearbox from the top.
1.3 Plunging Mechanism: Crank
Our earlier choice for plunging was a cam mechanism which would have ensured a
faster punching & return action during briquette placement. However, this
mechanism would have increased the complexity of the design and increased the
maintenance cost of the machine. We realized later that the crank would do the job
as well, while also not compromising on the cost and reparability aspects.
Stage 2: First Prototype Fabrication and Testing
2.1 Fabrication
Based on design above, we fabricated the first prototype in Ludhiana. To begin with
we decided to fabricate the frame, wheels, gear box and attach the engine to test
mobility and power of the machine.
2.2 Frame
It was decided to have the minimum inner to inner wheel distance as lesser than 9
inches. Hence, a width of 8 inches was fixed for the frame width between the wheels.
This provided sufficient design challenges throughout the process because
accommodating all the machine components between the wheels was always a
challenge.
2.3 Wheels
The powered-lugged wheels were 60cm in diameter fabricated on a 7mm thick bent
plate. The width of the wheels was 5inches. Each wheel contained 24 lugs and the
height of each lug was 3cm. The weight of a single wheel came to 15kg. The hub
and spokes had negligible weight as the spokes were made of hollow pipes, and
both the spokes and the hub had very less thickness.
! 7
2.4 Engine
The first design prototype of the UDP applicator was tried on a 1hp engine. The
engine was a light weight 6500rpm one. We designed a gearbox specific to its needs
and tried running the machine
2.5 Gear Box
Gear box was designed to bring down the engine rpm of 162 to wheel’s rpm of
40.The high speed of the engine increased the gear ratio and thus made the gear
box heavy.
! !
Fig 2.1 The 1hp engine Fig 2.2 Stage2 chassis – first prototype
! !
Fig 2.3 Gear box and engine assembly Fig 2.4 Power train assembly and
(stage 2) mounting
! 8
2.6 Testing
! !
Fig 2.5 Wheel dynamic testing Fig 2.6 Improved wheel design(with lugs)
During the initial days of fabrication, the frame was developed and tested in mud.
The testing was done on normal land and also on shallow wet mud. This brought out
a basic understanding of the difference in the power requirement in the two cases.
The testing was also done with the help of a spring balance to get an accurate
understanding of this difference. The test results were as below-
• (Power requirement in shallow wet soil) : (Power requirement in dry soil) = 3:1
• This ratio could significantly increase in deeper mud to the order of 10:1
2.7 Engine Issues
We soon realized the engine could move the machine but it did not have sufficient
power to overcome any obstacles that came in its way. The engine’s frame was very
delicate and we started facing problems immediately. The engine’s mounting point
broke and it became difficult to fit the engine without it. However, we managed by
slightly changing the mounting.
2.8 Gearbox smoothness issue
The high speed of rotation of the engine meant that we had to implement a high
gearbox reduction of 162. This made gearbox heavy and was not smooth in
operation.
2.9 Solution
The situation meant we had to hunt for a more suitable engine: higher power and
lower rpm. Hence, by the end of November 2012 we decided to move on to a more
powerful 3.5 hp 3750 rpm 70cc engine.
! 9
Table 2.1 Outline of stage 2
Criteria Aspect Details
Prototype Features Engine: Gasoline 1
Hp 6500 rpm
Diesel and battery options
discarded due to weight and
safety issues respectively
Frame Constraint: Width 8 inches,
as Paddy planted at 20 cm
separation so inner wheel
distance has to be less than
9 inches
Gear Box Gearbox reduction of 162 to
bring down engine rpm of
6500 to wheel rpm of 40
Wheels 2 Lugged Front Wheels: To
provide sufficient traction in
puddle fields
1 rear free wheel: To close
furrows and provide balance
& maneuverability
Drawbacks Engine: Insufficient
Power & Delicate
Gear Box: Heavy &
non smooth
Wheel: heavy
1 hp sufficient in dry land but
inadequate in wet land
High speed of engine
increased gear box weight
Proposed Solutions Replace Engine Replace 1 hp with 3.5 hp
engine of lower speed of
rotation
! 10
Stage 3 : Fabrication and Testing Prototype 2( Design with 3.5hp
engine)
!
Fig 3.1 Base design of stage 3 (prototype 2 – 3.5hp)
!
Fig 3.2 For comparing fabricated machine with base design
! 11
Gearbox
EngineFrontPoweredWheels
Brique2estorage
withpicker
Pipetoplace
brique2esbelow
plunger
Crank
ConnecJng
Rod
Plungertopunch
thebrique2esinto
thesoil
DifferenJal
3.1Fabrication
To overcome the challenges we faces in the initial design we began fabrication of the
3.5 hp engine powered prototype. And, once we achieved mobility in the machine we
thought of adding the picker & plunger mechanisms.
3.2Frame
The same basic frame used in the first prototype was used for the second prototype
too. There were additions on the frame later for adding crank, picker & plunger
mechanisms. And also minor changes on the frame were also made to for the engine
and gearbox mounting. The frame also required modifications when the briquette
container and picking mechanism had to shifted to reduce its speed (as shown in
images above, this is also described in the ‘Briquette Picking & Placement
Mechanism’ section).
!
Fig 3.3 Chassis – prototype 2
! !
Fig 3.4 Fabricated and assembled prototype 2 Fig 3.5 Dry Dynamic Testing
! 12
3.3 Engine & Gearbox
The new engine was selected with focus on weight, size, speed and power, and
hence selected a 3.5hp, 70ccengine that weighed 15kg (inclusive of an internal
gearbox that would help us reduce the weight of the external one). The engine came
with a kick start but we replaced that with long handle for starting the engine. The
kick start was not compatible with our machine design. In the eventual design we
could use a rope pulling mechanism to start the engine.
!
Fig 3.6 Design of prototype 2 explaining the relative position of the engine
and Gear box
Gearbox design
! !
Fg 3.7 Final design of the stage 3 gearbox Fig 3.8 Stage 3 gear box under
production
The gearbox design used for the 3.5hp engine is shown above. This gearbox
included a gear shifting mechanism to alter the speed of plunging / briquette
! 13
Gearbox
Engine
placement spacing. The new gearbox needed a much lesser gear ratio as the speed
of the 3.5hp engine reduced considerably over the previous 1 hp engine. Thus this
helped us reduce the weight of the new gearbox.
We also added the provision to change gears inside, using a lever, helping the
operator to change the speed of the plunger and hence vary the briquette spacing.
This would be useful for fields with varying crop distances. The gearbox was also
equipped with a neutral gear to stop the plunger movement completely.
With the 3.5hp engine, the engine & the gearbox were placed at a central location
between the front and the back wheels. The reason for this arrangement was that it
was not possible to fit the 3.5hp engine between the wheels (spaced 9 inches apart).
The gear sliding and lever mechanism inside the gear box (shown below) though
initially rough eventually smoothened out as we were able to fine tune the design.
! !
Fig 3.9Relative gear arrangement Fig 3.10 Assemble stage 3 gear box
of the stage 3 gear box with gear changing mechanism
3.4 Briquette Picking & Placement Mechanism
This mechanism comprises of a picker mechanism synchronized with the plunger
motion. The picker picks up one briquette during each briquette punching action of
the plunger. The picked urea briquette is then placed below the plunger through a
pipe. It is made to stop there by a rubber flap, until the plunger pushes the briquette
down into the soil with it during its downward stroke.
! 14
!
Fig 3.11 Stage 3 prototype explained
Plunger Mechanism Design
The initial design involved a crank fitted to a connecting rod through a pin. The
connecting rod on the other side was attached to the plunger. The joint was made at
the top of the plunger. This design was later changed and the connecting rod was
later attached to the side of the plunger. This improved the performance of the whole
mechanism.
!
Fig 3.12 Plunger mechanism under inspection
To increase smoothness of plunger movement the connecting rod’s length was
increased in order to reduce side forces on the plunger. This increase was
accompanied by a change in the height of the plunging mechanism & crank, in order
to maintain the plunging depth and ground clearance.
! 15
Crank
ConnecJng
Rod
Brique2estorage
withpicker
Pipetoplace
brique2esbelow
plunger
Plungertopunch
thebrique2esinto
thesoil
PinconnecJngthecranktothe
connecJngrod
ConnecJngRod
Plunger(Steelrod)
The plunger’s design was later changed from a joint at the top to a joint on the side.
The connecting rod remained the same but the connecting pin was replaced with a
screw to achieve the coupling.
This plunger design also did not need two separate inner and outer parts for depth
adjustment. We could simply do it by adding more holes for connecting the screw.
We had to shift from a steel based plunger to a nylon one. The steel provided huge
movement resistance as it did not allow any self abrasion. While passing through the
rubber flap at the bottom it would tremendously increase the stresses in the machine
frame. The frame also broke down as a result and we immediately decided to shift to
a nylon plunger. The nylon allowed self abrasion and adjusted to the design and
especially adjusted well with the rubber flap at the bottom.Hence, the plunger was
initially fabricated in metal and its length was made adjustable by having it made in
parts (inner & outer). Later it was made of a single nylon rod and the adjustability
was given by having different attaching points with theconnecting od
! !
Fig 3.13 Steel plunger and its sleeve Fig 3.14 Design correction of connecting
Rod,
! 16
Plungertop-outer
part
Plungerbo2om-inner
part
!
Fig 3.15 Inspection of plunger mechanism
!
Fig 3.16 Modified plunger mechanism for stage 3
! 17
Connec&ngRod
Plunger
Plunger’sSleeve
SleeveHolder
Crank
OldDesign
NewDesign
PlungingDepthadjustment
withseveralholeswith
threadsfora?achingwith
connec&ngrod
Connec&ngRod
Plunger
!
Fig 3.17 Nylon plunger with adjustable depth setting
Briquette picking mechanism
The briquette picker was initially directly mounted on the same shaft as the crank.
Hence, the rotation speeds were the same. For every rotation of the crank or a single
punching action of the plunger the picker would also complete one rotation.
However, as there were four cups in the picker it would pick up 4 briquettes per
rotation, when only one needs to be plunged. Hence, we covered the other 3 cups
(as shown in the image below) and briquettes were picked up by only one of the
cups. But in this arrangement we found that the percentage of briquettes being fed
to the pipe was less than 50%. We observed two problems some of the briquettes
being picked up were being thrown out of the box instead of being directed into the
pipe and due to high speed of rotation of briquette picker (same as that of the
plunger crank) briquette picking was not consistent.
As a first step we attached a lid to the briquette box to prevent briquettes from being
thrown out. And then we decided to reduce the speed of the picker 4 times and use
all 4 briquette picking cups instead of one. Now we could have one rotation of
briquette picker for every 4 rotations of the crank plunger. Even after attaching the
lid, Thespeed reduction required an additional chain and sprocket arrangement, as
well as redesigning of the frame. A separate shaft was mounted with a sprocket and
the picker box was connected to the crank shaft through a chain. But, the reduced
speed improved the briquette picking mechanism considerably.
! 18
Another issue we faced was briquettes getting stuck at the corner near the plunger
sleeve bottom or in the rubber pipe itself. We understood that the smoothness of the
e corner joint of the metal pipe was the main blocking point and made it smooth and
increased its inclination.
! !
Fig 3.18 Explaining the issue with the neck of the sleeve for plunger
Fig 3.19 Depicting the cumulative effect of the connecting pipe and the neck of
the sleeve in restricting the briquettes from reaching the sleeve
!
Fig 3.20 The modified picker mechanism for stage 3
! 19
Brique2estoragecontainer
Pickercoveredcups
Containerlid
Brique?esstuckatthecorner(ofmetalpipe)&
intherubberpipe(orangecoloured)
PlungerSleeve
!
Fig 3.21 The modification for the picker mechanism
Rubber stopper flap
A rubber flap was used below the plunger to stop briquettes from directly falling
down. But choosing the rubber was a tricky issue. The harder rubbers would provide
higher resistance while opening whereas softer rubber would get stuck between the
plunger and the sleeve corner during the return motion of the plunger. But trying 7-8
different types we were able to identify one ideal for our purpose
! 20
Brique2ehiVngmarks
!
Fig 3.22 The position of the rubber flap and the problems associated with its size
But still the rubber flap offered more than desired resistance to the plunger
motion and to counter this we increased the diameter from 3.5 to 5 inches. This
helped us achieve smooth motion of the plunger
The new 5 inch diameter rubber holder
!
Fig 3.23 Modified rubber holder (size increased)
! 21
3.5 Differential
To allow easy turning of the machine we decided to use a differential over a clutch
mechanism as the former was more compatible with the 8 inch width constraint of
the frame. The differential is a simple mechanism which allows the two powered
wheels to move at different speeds, thus, allowing the machine to turn and not
remain straight rigidly. We chose the differential of a three wheeler / auto rickshaw
called ‘Kerala’. We chose it mainly for its compact design, which matched our needs.
Though initial assembly and incorporation of the differential was a challenging and
time consuming as we had to encounter couple of failures and damages to internal
gear, we were able to get the desired results.
! !
Fig 3.24 Position of differential in Fig 3.25 Actual differential being used
the machine
3.6 Wheels & Axles
The same wheels were used as Prototype 1, flat and wide with small lugs. Two
separate axles were used for transmitting power from the differential to the two
powered wheels. These axles were in contact with internal differential gears through
a spline. But the point of contact of the axles with the differential gears is vulnerable
to high stresses and we had our axle breaking during testing. This forced us to use
one with larger diameter and more strength.
Note: A detailed material & load analysis can be submitted once the functional
prototype is ready and proper load analysis is possible. This analysis would be
helpful for the final production design of the applicator.
! 22
For the rear wheel initially we used a fabricated flat wheel but moved onto a
readymade nylon castor wheel, as it was smoother on and off the field.
! !
Fig 3.26 Fabricated castor wheel Fig 3.27 Rejected castor wheel (too heavy)
Another point of concern was the rear wheel and frame joint, which even broke
during testing. A better wheel fixing mechanism shown below did the trick.
! !
Fig 3.28 Space available for the position Fig 3.29 Mounting for the sleeve
of the power train
3.7 Acce lerator
A thumb based accelerator has been used. This particular accelerator design was
specifically chosen as it could be set at a particular throttle and keeps moving almost
! 23
at constant speed. This is much better compared to a handle based accelerator (like
the ones used in motorcycles) as it makes it easier to control the machine in a
planted field.
3.8 Testing
Testing was done in fields in Ludhiana. The first round of tests were conducted in dry
land conditions and the second round in wet field conditions similar to ones faced
during paddy transplantation.
! !
Fig 3.30 Dry dynamic testing of prototype 2 Fig 3.31 Stage 3 - completed prototype
Prototype 2
During dry field testing we faced issues such as:
• Inconsistency in plunging
• Inconsistency in briquette picking and placement
But fine tuning and adjustments to these mechanisms helped us achieve the desired
performance in dry land conditions.
Next the machine was tested in wet field conditions and here we faced the following
issues:
! 24
• Mobility and Maneuverability: The machine was immobile in dense wet soil
and was getting stuck. The inappropriate weigh distribution meant that that
most of the weight was concentrated on the non-powered back wheel. This
led to its sinking into the soil. Whereas the wider powered wheels remained
on the surface and slipped (also because of the lesser weight over these
wheels) thus was not able to create enough traction. Further concentration of
weight on the rear castor wheel did not allow the machine to turn easily, as for
that to happen, the castor wheel should not be loaded with weight
! !
Fig 3.32 Wet dynamic testing at Fig 3.33 Failure during wet dynamic
testing stage 3 of prototype 2
of prototype 2
3.9 Solution
One of the major problems was that the machine was very heavy and to make things
worse the weight was unevenly distributed. The gear box itself weighed 35-38 kg
and was placed behind the powered wheels. Further, the plunging mechanism and
the 10-15 kg engine were also placed behind the front wheels. This made the
machine rear-heavy and resulted in the non-powered castor wheel getting stuck in
the field during the motion. The gear box was designed to place briquetted at 50, 40
and 30 cm spacing, as per the farmer’s choice. We thought it would be better to have
a sleeker, lighter and easily detachable gear box which places briquette only at a
particular spacing. And, different gear boxes can be made available for placing
briquettes at desired intervals. Briquettes can then be placed at any desired interval
! 25
by attaching the appropriate gear box. Apart from saving close to 15-18 kg, the new
design for the gear box would allow us to place it between the powered wheels and
thus allow us to have a more favourable weight distribution and improved mobility
during operations.
Further we thought the design and size of the lugs on the wheels could also be
improved to generate enough traction. A possible solution was to use broader lugs or
ones similar to the ones on tractor/ paddy trans-planter wheels.
Criteria Aspect Details
Prototype Feature Engine: 3.5 Hp 70 cc Higher power and lower rpm 15 kgs with internal gearbox
Frame Redesigning to fit new engine, gear box and briquette plunging and picking mechanism
Gear Box To bring down engine rpm to wheel rpm of 40 To allow for variable briquette placement interval N e u t r a l O p t i o n i n c l u d e d t o discontinue plunging while machine was in operation
Plunging Mechanism Crank driven nylon plunger that allowed flexibility in depth of placement
Briquette Picking Mechanism
Picker synchronized with plunger picks up a briquette and places it below the plunger on top of a rubber flap Plunger while going down takes this briquette and places it in the soil
Wheels 2 Lugged Front Wheels: To provide sufficient traction in puddle fields
1 rear free wheel: To close furrows and provide balance &
maneuverability
! 26
Table 3.1 Outline of stage 3
Stage 4: Fabrication and Testing of Prototype 3
4.1 Fabrication
To overcome the challenges faced in operations of the previous design, we
conceptualized a new design, and started the fabrication process in Delhi.
Unfortunately, the fabricator we worked with in Ludhiana on the initial design was not
able to devote much time off late. In Delhi initially we had to work with several
fabricators rather than have one dedicated to us. But under this arrangement making
modifications to design was a challenge. Fortunately, Dr.Indramani Mishra of IARI
(Indian Agriculture Research Institute) was kind enough to allow us access to
equipment at the lab as well as testing fields.
In order to address the major concerns highlighted in the testing of the second
prototype we realized we had to design almost a completely new machine. The
engine & gearbox had to be shifted. A completely new gearbox design had to be
made to reduce weight and speed and increase torque. The frame design also had
to be reworked. The plunger design was altered for improved performance in wet soil
conditions and even though the picker mechanisms remained unchanged it had to
be mounted differently considering the new requirements.
Several design options were considered to achieve these objectives and the one
finally chosen along with the advantages it had over the previous design is shown
below in the image.
Differential A readily available differential system was added to allow easy turning of the machine
Drawbacks Poor Mobility and Maneuverability in wet
soil
Inappropriate weight redistribution heavily inclined towards the back wheel
Proposed Solutions
Reduce Weight Improve weight
distribution
Redesign Gear box Rearrange placement of gear box and engine
! 27
4.2 Weight balance shifting
The weight distribution of the machine was shifted forward by mainly shifting the
engine in front of the powered wheels by making the gearbox compact enough to fit
between the powered wheels. This arrangement provided torque balance about the
powered wheels and thus allowed the machine to be lifted about the wheel easily,
thus making turning the machine easy.
! !
Fig 4.1 Analysing prototype 2 and its shortcomings and improved design for Stage 4
! !
! 28
OldDesign NewDesignHeavierGearBox;behindthe
poweredwheels
Engineattherear
LighterGear
Box;between
thepowered
wheels
Engineatthe
BiggerLugson
wheels
Fig 4.2 Fabricated prototype 3 with Fig 4.3 Fabricated stage 4 prototype
round rim tyres with flat rim tyres
4.3 Weight reduction
Major weight reduction was achieved in the gearbox and through the following steps:
• Changing to Material of construction of casing from Mild Steel to Aluminium
• Using of Internal differential to eliminate the use of separate differential casing
and of any coupling shaft between them.
• Discarding feature that allows variable briquette spacing option
4.4 New power-train design
• New gearbox design with internal differential
• Gear ratio increased to provide higher torque and lower speed
• Power transmission by chain as compared to coupling used between engine
and gearbox earlier
Major advantages over the previous design:
- Vastly improved Mobility in wet mud conditions
- Much easier to turn by lifting the machine from the back
- Much lighter machine
- Stronger frame
! 29
!
Fig 4.4 New position of gear box and chain drive
The main design challenge faced during this phase was that of making the machine
move in wet fields. Multiple wheel and ski designs were tried before we arrived at
our final solution.
4.5 Engine
Engine- vibration was resulting in chain coming off often and to counter this and
reduce vibrations and increase stability we decided to secure it with rubber mounts.
4.6 Gear Box
A higher gear ratio of 27was used to achieve higher torque. The feature to allow
variable briquette placing was discarded. This meant that the gear box was much
lighter. Further, use of an internal differential and aluminum casing instead of mild
steel casing lead to more weight reduction
! 30
Chainfrom
engineto
gearbox
Newgearbox
withinternal
differenJal
!
Fig 4.5 Fabricated new gearbox with aluminium case
4.7 Frame
The frame’s design was changed to fit the new needs. To make it stronger a thicker
frame of 14 gauge was used. The handle design was changed to make it more user
friendly. We decided to replicate the wheel barrow handle design which we felt was
much more comfortable and easier to control.
Earlier design had chains and sprockets alignment & stability issues. The reasons for
this was high speed of motion for the one connected to the engine, the length of the
one connecting gear box and crank, and high gear ratio for the briquette picker one.
These were resolved through modifications to the frame, addition and inclusion of
fabricated guides to reduce the falling of chains.
! 31
!
Fig 4.6 Problems faced due to the length of the gearbox-crankchain
!
Fig 4.7 Guideway for the chains
4.8 Wheels & skis
Navigation in wet soil conditions was a major challenge with the previous prototype
and this meant that we had to design more effective wheels. 5 different versions of
the wheel were fabricated and tested before identifying the one that suits our need
the best. The designs were mainly based on transplanter & power tiller wheels used
for deep wet mud conditions. They have been described below.
Version 1: Paddy trans-planter wheels - Pipe wheels with long & sharp lugs
This wheel’s design was based on transplanter’s wheels. It was not heavy as it was
fabricated mainly from hollow pipes. The main issue during testing of this wheel was
! 32
LongChain:GearBoxtocrank
FabricatedChainGuide
that it sunk very easily in deep wet mud and hence could not move. The long lugs
would also dig into the soil and create a hole for the machine to get stuck.
!
Fig 4.8 Pipe wheels with long & sharp lugs
Version 2: Pipe wheels with additional skis
The skis were designed and fabricated to improve the machine’s performance. Even
though with the skis the machine’s movement slightly improved in wet mud, it still
easily got stuck.
!
Fig 4.9 Pipe wheels with additional skis
! 33
Skis
!
Fig 4.10 Failure of pipe wheels with additional skis
Version 3: Pipe wheels with small flat lugs
As mentioned above, we observed the long lugs digging into the soil and creating a
hole for the wheel hence, making it difficult for the machine to move forward. We
thus decide to try shorter and a higher number of lugs on the wheel. The higher
number of lugs would also reduce the force transmitted per lug, thus, further
reducing the chance of digging into the soil. The performance of this wheel was
much better than the previous wheel but was still not good enough for farm
operation.
!
Fig 4.11 Pipe wheels with small flat lugs
! 34
Version 4: Flat wheels with triangular lugs
We decided on trying flat and wide wheels with longer triangular lugs. This was
similar to the power tiller wheels used for wet mud conditions. It was much heavier
than the other wheels and with a 4 inch larger diameter. This wheel was designed to
avoid sinking of the wheel, increase traction during movement and also make it
easier to turn. This wheel was 4 inches larger in diameter than the other 3 sets of
wheels. It had a width of 3 inches. The wheel was successful in navigating through
wet soil.
!
Fig 4.12 Flat wheels with triangular lugs
Version 5: Flat wheels with small flat lugs
Simultaneously, we also designed extra wide wheels (5 inches) with a thin rim and
short lugs. But since the ones with triangular lugs were successful we decided to
continue with them.
4.9 Axles
During testing, one of the axles failed by torsion. The axle and keys got twisted. We
therefore decided to redesign the axle for higher load carrying capacity. The axle
was re-designed; new material was used and was hardened. The wheels were fixed
on the axle using splines, and keys were eliminated. The change in design mainly
consisted of diameter increase and cutting of splines on the axle. The material of the
axle was then changed to much stronger EN353. The axle has been providing much
improved performance since then.
! 35
! !
Fig 4.13 Damaged keys – key failure Fig 4.14 Failed axle – torsion failure
!
Fig 4.15 New axle with improved design
4.10 Crank
To increase stability the mounting for the crank was redesigned. The new mounting
had two journal bearings mounted on an extended frame. And, its thickness was
increased to improve strength and stability.
! !
Fig 4.16 Comparison of the new-redesigned crank with the old one
! 36
4.11 Testing
! !
Fig 4.17 Field preparation
!
Fig 4.18 Dry dynamic testing of stage 4 machine
Testing was done in fields prepared in IARI (Indian Agriculture Research Institute) in
Delhi. The first round of tests were conducted in dry land conditions and the second
round in wet field conditions similar to ones faced during paddy transplantation.
The machine performed well in dry land conditions but again faced some issues in
wet land conditions. Though unlike the previous attempt, the machine was able to
easily navigate the tough wet soil conditions and was easy to handle and
maneuverable. The machine was easy to rotate and due to better weight balance
could be easily lifted and made to pivot and rotate on the spot in dry soil, but in deep
wet soil it had a radius of 60-70 cm.
! 37
Though success achieved in mobility was very encouraging performance of plunger
in wet soil was a major challenge. The nylon plunger the mud (as in image above)
inside the plunger sleeve and this impeded its motion. Nylon creates hydrogen
bonds, and hence attracts water, which in turn makes mud stick to it easily. We are
therefore, shifting to a Teflon plunger which can repel water and avoid this situation.
!
Fig 4.19 Failure of the plunger due to increased friction and clogging because
of wet soil
4.12 Solution (Next Step)
Due to physical properties of nylon we are thinking of moving to a Teflon plunger that
would prevent mud from sticking onto its surface and impeding the motion.
Teflon plunger is smooth as compared to Nylon and the locking forces generated
during the plunge would be significantly reduced preventing the slider crank
mechanism from locking.
New Teflon plunger was installed and tested in air by inserting a container consisting
of dense mud resembling the paddy field condition beneath the plunger. The new
plunger was rigorously tested for an hour and the plunging was smooth.
The current mechanism is ready to be tested in actual field conditions.
! 38
! !
Fig 4.20 Nylon plunger is replaced by Teflon plunger
The machine was taken into the field but the starting mechanism of the TVS moped
engine failed. The current automobile engine has been highly unreliable for on- field
wet muddy conditions. A decision was taken to procure a new engine.
! 39
Stage 5: Fabrication and Testing of Prototype 4
5.1 Honda GK 200 engine
A new engine Honda GK 200 was procured best suited for agricultural applications.
ENGINE SPECIFICATION
Table 5.1 Specification of GK 200 Engine
Fig 5.1 Honda G 200 engine
Model GK 200
Type 4 stroke, Air Cooled, Single Cylinder, Horizontal Shaft
Displacement 197 cc
Net Engine Power 2.2 kW / 3 HP @ 3,600 rpm
Net Engine Max. Torque 7.9 Nm @ 2,500 rpm
Fuel Tank Capacity 3.3 litre (Kerosene), 0.35 litre (Gasoline)
Ignition System
Fly wheel Magneto Ignition, Transistor Type Magneto
Ignition
Air Cleaner Oil Bath Type
Dry Weight 17Kg
Dimensions LxWxH 330 x 405 x 425 mm
! 40
5.2 Clutch Mechanism
The previous engine had a centrifugal clutch mechanism which allowed the machine
to start at no load condition.The present engine doesn’t have an in built clutch
mechanism so we had to incorporate a clutching mechansim.
Selection of Clutch
1.Friction clutches:
Transmssion power by means of friction lining b/w the friction plate and pressure
plate.
2.Pulley and belt system:
The idler pulley is used as clutching mechanism.It is basically operated in two
postions to make the belt loose or tight.
We chose the second mechanism for it’s simplicity in design and fabrication.
V-type belts were chosen along with B-type pulleys according to the numerical
calculations performed considering the present gear ratio and the torque to be
transmitted.
The engine was mounted to the chassis along with the driving and driven pulleys.
The next step was to fabricate the idler mechanism and install it according to the
space constraints in the frame. The positions of the idler was decided and set
accordingly by installing the belt with the pulleys.
The new engine and power transmission mechanism was ready for testing.
! 41
! !
Fig 5.2 Clutch mechanism for the new power train
5.3 Testing
Dry land testing:
The machine was not able to disengage and considerable slipping was observed b/w
the belt and the driving pulley. Excessive heat was generated in the engine
pulley(driving pulley)
Wet land testing:
The machine was not able to move forward followed by excessive slipping earlier
observed.
The machine with the old engine (TVS moped) was able to move in wet muddy
conditions but the new engine with the same power was unable to do so.
Clearly the belt mechanism not able to transfer power as the load conditions in wet
muddy field is much more than we anticipated in our calculations.
Slipping mechanism verifies our observation.
! 42
! ! .
Fig 5.3 Testing of the stage 5 machine – prototype 4
5.4 Solution
The failure of belt pulley mechanism made way for the friction clutching as reliable
mechanism in our machine. The friction clutch would be manually operated by the
operator to engage and disengage the drive.
! 43
5.5 The Final Design
!
Fig 5.4 Side View
!
Fig 5.5 Front View
! 44
!
Fig 5.6 Top View
!
Fig 5.7 Isometric View
! 45
RESULT AND DISCUSSION
The Urea Deep Placement Applicator has been successfully designed and a
prototype has been fabricated which performs the operation satisfactorily.
The result of our project has been fairly positive and it gives way for further
development in this area of research. Various optimization techniques can be used
for further weight reduction. Improvisations in design could lead to a more rigid and
stiffer machine. Research on selection of materials for different components of the
machine can improve the handling and maneuverability of the machine further.
Further scopes in the field are the development of a Double Row UDP Applicator and
an Adjustable spacing Applicator. Also the integration of the UDP Applicator into a
rice transplanter can act as a boon in paddy production.
! 46
CONCLUSION
The UDP Applicator developed by our team is a success and performs the plunging
of Urea briquettes at equal fixed intervals properly. The percentage of briquette
placement in the soil is more than 94%.
The scope of our development is magnanimous if implemented properly in the
country and worldwide. It could create a huge impact on the production of paddy ,
decrease the consumption of urea immensely.
! 47
REFERENCES
Research Papers:
1. Markley G.L., Assembly System and Method for Chain Drive System, US
Patent No. 8387244 B2
2. Lupin M.S., Lazo J.R., N.D, et al, Briquetting, TP 963.4.U7B74
3. Crolla D.A., El-Razaz A.S.A., Combined Lateral and Longitudnal Force
Generation of Tyres on Deformable Surfaces, Journal of Terramechanics, Vol
3, pp220-245
Books:
1. Nortan N.L., Integrated Approach To Machine Design
2. Timoshenko, Strength Of Materials
3. Bhandari V.B., Elements of Machine Design
4. Rattan S S, Theory of Machines
Websites:
1. www.ifdc.org/Technologies/Fertilizer-Deep-Placement-(FDP)
! 48