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In-Situ Testing of a Darrieus Hydro Kinetic Turbine in ColdHydro Kinetic Turbine in Cold Climates
Shamez KassamShamez KassamMSc Thesis DefenseAdvisor: Dr Eric BibeauAdvisor: Dr. Eric Bibeau
In co-operation with: Manitoba HydroNew Energy Corporation IncNew Energy Corporation Inc
University of Manitoba
Hydro PowerHydro Power
2 Sources of Hydro Powery
Marine RiverMarine River
Wave Tidal Potential E
Kinetic EEnergy Energy
NRCAN ClassificationLarge Hydro over 50 MWSmall Hydro 1 to 50 MWMini Hydro 100 kW to 1 MWMini Hydro 100 kW to 1 MWMicro Hydro under 100 kW
Hydro Power CapacityHydro Power Capacity
Marine PowerMarine Power225 GW estimated by NRCAN and HATCH Energy
Potential River PowerInstalled capacity ofInstalled capacity of 72,500 MW in Canada3,500 MW from small hydro across 359 siteshydro across 359 sites
Kinetic River PowerYet to be assessed
Research ObjectiveResearch Objective
Evaluate Performance and DemonstrateEvaluate Performance and Demonstrate the Viability of River Kinetic Power in Cold Climates
Deployment of a 5 kW non-ducted Darrieus turbine
Performance evaluation in extreme cold conditions
Grid connect a kinetic turbine
Assess viability of a long term installation in Canada
Literature ReviewLiterature Review
Performance: Vertical Axis Hydro Turbiney
Non-Ducted
33% t 35%
Ducted
45% t 55%33% to 35% 45% to 55%
Ducts increase the local velocity across the rotor over 1.5 times
Literature ReviewLiterature Review
Laboratory TestingLaboratory TestingExtensive research into modeling (BEM)Models developed for optimizationL b t t ti t lid t d lLaboratory testing to validate models
On-Site TestingOnly one other Canadian grid connected kinetic turbine in 1983Turbine tested in St. Lawrence River (Darrieus)Testing took place during summer monthsg p g
Lack of KnowledgeIssues pertaining to a year round installation in CanadaIssues pertaining to a year round installation in Canada Operation in cold climates
Literature ReviewLiterature Review
Frazil IceActive Frazil
Small disks of ice: 1 – 4 mm diameter, 1 – 100 μm thickFormed in turbulent, supercooled watersDescribed as a blizzard of sticky ice particlesAccumulated rapidly into larger structures up to 30 m in diameter and 5 m in thickness
Passive FrazilPassive FrazilSlushy and non stickyDerived from active frazil in warmer waterGroup together to form blockages
Literature ReviewLiterature Review
Frazil Ice on Hydro PoweryActive frazil builds on turbine inlet vanes and trash racksUp to 30% power loss observed at Rivière-des-Praires25% d ti i fl th Ni Ri25% reduction in flow on the Niagara River
Frazil Ice PreventionFrazil Ice PreventionIce cover prevents water from super coolingReduces incoming active frazil into passive frazil
Experimental Set UpExperimental Set Up
Test SitePointe Du Bois generating stationEssential facilities and equipment available on siteL t d th Wi i Ri i th C di Shi ldLocated on the Winnipeg River in the Canadian Shield
River
FlowSpillway
Bridge
Bridge Boat
Station
Experimental Set UpExperimental Set Up
Anchoring and DeploymentAnchoring and DeploymentSolid rock river bed excellent for anchoringShore anchors installed at Points A, B, and C30ft 18ft t h l d l d i i t 200830ft x 18ft pontoon research vessel deployed in winter 2008
Experimental Set UpExperimental Set Up
DAQ: HardwareQData Acquisition System3 independent systems logging mechanical, electrical and video datavideo dataHoused in a box for protection, organization, and ease of transportation
930-A
DAQ BOX
RS-232
120 VAC in from shore FANPower bar
CT box
Disconnect switch
DT85
boat computercomputer
Power from Turbine
Power to Inverter
Camera Input
Experimental Set UpExperimental Set Up
DAQ: SoftwareData analyzed on hourly basisSoftware consolidates mechanical and electrical dataDaily graphs are complied and posted onlineDaily graphs are complied and posted onlineEmail alarm system
Flow EstimationFlow Estimation
Acoustic Doppler Velocimeter
ADV used to validate flow meter
Accuracy vital for performance calculations
Requires particulates laced within flow
Flow
Signal full of erroneous spikes and required filteringfiltering
CVParticle InjectionTurbulence
Flow EstimationFlow Estimation
De-Spiking ADV Signalp g g
2
Test 7Raw Signal
2 methods assessedMean replacement -1.9
Test 6Mean Replacement
-1.4
Test 6Interpolation Replacement
0
1
s)
pInterpolation replacement
-2
-1.95
)
-1.8
-1.6
)3
-2
-1
Flow
(m/s
Based on 1g criterion
Both estimate mean flow -2.1
-2.05
Flow
(m/s
-2.4
-2.2
-2
Flow
(m/s
0 10 20 30 40 50-4
-3
Time (s)
within 0.5%
Interpolation replacement 0 10 20 30 40 50-2.2
-2.15
Time (s)0 10 20 30 40 50
-2.8
-2.6
Time (s)p pgives more true flow pattern
Time (s)e (s)
Turbine PerformanceTurbine Performance
Winter TestinggProvided consistent power for 1260 hoursPower output with a 4.5% standard deviation in a steady flow with 1% standard deviationsteady flow with 1% standard deviation Turbine stalled repeatedly and required manual re-start
Turbine PerformanceTurbine Performance
Winter PerformancePerformance was poor at 10% efficiency
expected 30%expected 30%
Drive train housed in heated and insulated enclosureand insulated enclosure
Turbine support arms were found to be the major source of power loss
Winter testing had flat bar arms
Power Loss Due to Support ArmsPower Loss Due to Support Arms
Numerical Model2-D drag analysis conducted on rotating armUsing optimal Tip Speed Ratio (TSR) for array of flow ratesModel computes power loss per revolution for array of arm dragModel computes power loss per revolution for array of arm drag coefficients
FResults
Effect of Support Arms on Performance
L i f tF
Vd r a gF
ResultsPredicted loss of 1474 W
4000
5000
6000
7000s
[W]
θ
V∞ Arm drag distribution
Summer tests showed a measured loss of 1405 W 31000
2000
3000
4000
Pow
er L
oss
( , )P V∞ Ω1405 W
1.5
22.5
3
00.511.5
0
Mean Flow [m/s]Drag Coefficient (Cd)
Turbine PerformanceTurbine Performance
Summer Testingg3 arm profiles were tested for performance
Flat Bar
Profile arms tested in both rear and front position on vessel
Flat Bar
vessel
Water to wire efficiency based on output to grid
Profile Turbine designed with these arms
based on output to grid
Rotor efficiency based on f
Hydrofoil
grid output plus quantified losses
Turbine PerformanceTurbine Performance
Water to Wire Efficiency Net Rotor EfficiencyFlat Bar 9.6%Profile 21.3%Profile Front 23.6%
Flat Bar 15.9%Profile 28.6%Profile Front 29.1%
Hydrofoil 26.5% Hydrofoil 35.4%
Cold Climate OperationCold Climate Operation
IcingIcingAll aluminum pontoon research vessel encased in ice within daysSplashing from waves allowed ice to grow up towards theSplashing from waves allowed ice to grow up towards the deckIce accumulation pulled on chains and brought
Data Acquisition Shed
Temperature Data forPinawa, Manitoba
5
on chains and brought bow underwaterIce was manually cleared on a weekly -15
-10
-5
0
e (d
eg C
)
cleared on a weekly basisDetrimental to sensor located near water level
-30
-25
-20
Tem
pera
ture
10 yr Average2008 Average
located near water level -40
-35
Jan 01
Jan 0
4Ja
n 07Ja
n 10Ja
n 13
Jan 16
Jan 19
Jan 2
2Ja
n 25Ja
n 28Ja
n 31
Feb 03Feb 0
6Feb
09Feb 12Feb 1
5Feb
18Feb 21Feb 2
4Feb
27Mar 0
2Mar
05Mar 0
8Mar 1
1Mar
14Mar 1
7Mar 2
0Mar
23Mar 2
6Mar 2
9
Date
Cold Climate OperationCold Climate Operation
IcingIcingMultiple sensors lost
Load cell, Flow meters, Cameras
Ice did not accumulate on turbine bladesIce growth between pontoons would stall rotorIce bergs impacted rotor frequently when removing iceTurbine was removed for spring break up
Turbine DurabilityTurbine Durability
Risk of Impact During Summer MonthsRisk of Impact During Summer MonthsAnalyzed vibration readings for 2 months
A d f f i t f l iAssessed frequency of impacts from logs in summer
Qualified based Type of Impacts Number of Mean Time Qualified based on level of impacts
Type of Impacts Impacts [hours]
minor 8 148.35
VAHT deflects impacts rather than absorb
small 23 51.60
medium 5 237.36t a abso b medium 5 237.36
large 2 593.39
Turbine DurabilityTurbine Durability
Affect on PerformanceLast days of winter testing showed performance of damaged blades
Summer testing began with pristine blades
Effi i diff f 0 8% ith TSR diff f 0 24Efficiency difference of 0.8% with TSR difference of 0.24
ConclusionsConclusions
Turbine operates at over 35% efficiency and can self p ystartOperates well in winter if free of iceD fl i hi h f iDeflects impacts which are frequent in summerProtection required for winter installation (ice bergs)Safe deployment and cost effective anchoringSafe deployment and cost effective anchoringProduces reliable and consistent clean energy