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1
Hines Power Block 2Steam Turbine Mechanical Failure
2
Agenda
Background
Event Timeline
Root Cause Analysis Data
Vibration History
Operating Conditions
Coupling Bolts
Summary
3
Background
4
Background
Power Block 1 (2x1) ~500MW
CTGs are Siemens-Westinghouse W501FC+
STG is Westinghouse 2326RT2
Commissioned April 1999
Power Block 2 (2x1) ~530 MW
CTGs are Siemens W501FD2
STG is Siemens HE
Commissioned December 2003
Power Block 3 (2x1) ~530 MW
CTGs are Siemens W501FD2
STG is Siemens HE
Commissioned November 2005
Power Block 4 (2x1) ~510 MW
CTGs are General Electric 7FA+e
STG is GE D11
Commissioned April 2007
Power Block 1
Power Block 2
Power Block 3
Power Block 4
Cooling Pond
(inlet)
Cooling Pond
(outlet)
5
Background
PB2 Nameplate Data
Two (2) STG-5000F CTGs
187 MW each
One (1) Siemens HE STG
188 MW
23-stage HP section
11-stage IP section
3-stage LP section
Two (2) NEM three-pressure, unfired HRSGs
HP: ~1800 psig/1040 F ~420 kpph
IP: ~400 psig/600 F ~80 kpph
LP: ~80 psig/500 F ~90 kpph
HP
IP/LP
HP-IP/LP Coupling
IP/LP Interface
6
Event Timeline
2003 – Turbine brand new, but 42-inch Titanium L-0 fleet had issues with OEM 1st revision blades (e.g., tip and mid-span snubber losses). Exclusion zone established and time limits in exclusion zone were set.
2003 2004 2005 2006 2007 2008 2009 2010 2011 2012 2013 2014
Time2014 Expanded next slide
2007 – L-0 blades were replaced with new design (revision 2) on PB2S as a fleet validation unit. After OEM testing, no restrictions on
time in exclusion zone were required. Stress levels in exclusion zone were deemed acceptable.
2011 – Major (50khrs) outage; HP-IP/LP coupling re-assembled without data sheet or proper preload/set screw setting.
Incorrect data sheet for generator coupling supplied: 7 bolts at 33% less-than-full preload (correct setup is 8 bolts).
2012 – High transient vibration on STG during summer runs begin.
2012/13 – After ~ 5yrs, L-0 blades started to show erosion at trailing edge near platform.
2013 – Bearing #3 was raised to add more load to stabilize
bearing from high vibrations. Little success.
7
Event Timeline (cont’d)
Jan ‘14 Feb’14 Mar ‘14 April ‘14 May ‘14 Jun ‘14 July ‘14 Aug‘14 Sept ‘14 Oct ‘14
Time
• 2014 Mar-April – added a balance weight that changed slope of vibration increase ~5x.
• 2014 May 24 – Condenser black plant event, caused STG speed >360 rpm and vacuum >8 in HgA. Most likely cause for an existing erosion pit to grow from
~ 0.025" to 0.126" on L-0 blade and arrest. Crack was dormant with exclusion zone running stresses.
• 2014 June – OEM issued the first release of a detailed coupling assembly procedure as a result of other fleet coupling failures. These units were without
axial thrust loads like PB2 design.
• 2014 July 7 – STG Mechanical Failure Event resulted in all coupling bolts failing in ductile tension overload (not fatigue), raised the stress levels on L-0
section that caused multiple blade failures, all instrument pickup mounts failed, damaged control valve, stop valve, and damaged multiple stationary devices.
Duke RCA identified most likely cause was the failed coupling bolts initiated event, which allowed the L-0 dormant crack(s) to propagate.
• Collateral Damage – Cold slug of Hot Reheat steam or condensate caused a water hammer event due to failed non-return valve on Cold Reheat
line. As a result, water made it in the HP Turbine where it flashed and stretched the HP bonnet bolts and caused them to fail in tensile overload.
Water hammer event also caused turbine movement and cracked Bearing #2 housing, which allowed about ~1,300 gals of turbine lube oil (~20%
capacity) to be released and then catch fire.
• 2014 Aug – PB3S L-0’s were inspected with acceptable erosion on trailing edge.
• 2014 Oct – PB3S was found with loose coupling bolts on HP-IP/LP coupling after experiencing high vibration post L-0 inspection. OEM increased the
coupling bolt preload spec by as much as 40% for PB3S.
8
Event Timeline (cont’d)
9
Vibration History
20062004 2008 2010 2012
10
L-0 Erosion History
11
Condenser Incident
>8” HgA and >360 rpm ~ 450 sec
5/24/15
May 24, 2014: Loss of auxiliary power caused loss of cooling water and condenser back pressure
increased during steam turbine tripThis event likely started a crack (or multiple cracks) at erosion pit areas on L-0 blade(s) that were then left
dormant with normal back pressure limits and stresses
12
Summary of Coupling Bolt Stretch Info
New spec .009-.010”
13
HP-IP/LP Coupling Bolts (as found)
Close up of #1
14
HP-IP/LP Coupling Bolts (tensile failure)
Failed PB2 New Bolt
15
Hines PB2S Rotor Model
HP-IP/LP
CouplingHP-Generator
Coupling
HP-IP/LP Coupling carries shear, torque (LP&IP), axial (thrust), and minimal bending loading (fair faced
alignment). Loss of the coupling bolts would force IP/LP rotor to apply loads on stationary components to
support itself.
IPLP HP
16
L-0 Blade Failure Scenario
17
Summary
Trailing edge erosion was occurring on L-0 blades since installation in 2007; equipment was being inspected by a combination of OEM and Duke NDE resources on a regular basis.
During 2011 Major Outage, HP-IP coupling bolts were not properly secured and/or possibly not adequately preloaded, which allowed loss of tension over time and subsequent changes in vibration.
A 5-24-14 condenser back pressure vs speed event initiated a fatigue crack from an erosion pit and left a 3.2mm dormant crack on the trailing edge of a L-0 blade.
On 7-7-14, the unequally loaded HP-IP coupling bolts finally failed from excessive axial tension as fewer tight bolts were left to share the loading from thrust bearing unbalance.
As a consequence of the coupling bolt failure, the L-0 blades experienced very high vibratory loading, causing fatigue failure.
Other pre-existing conditions with a damaged non return valve caused water induction event in the HP turbine and HP stop valve.
The resulting oil leaks led to local fires that caused additional damage.
The Good News: the unit was rebuilt and returned to service on June 19, 2015.