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Harris Plant - Heater Drain System TransientsINPO ICES #305654 HNP Root Cause Evaluation 592995
Presentation Outline
System Overview
System History
Atypical System Characteristics
Recent Problems
Cause(s) of Problems
Generic Lessons Learned
2
Heater Drain System Schematic – ‘A’ Train
3
Heater Drain System Schematic – ‘A’ Train (Cont’d)
4
System History
Initial operation experienced significant system instability issues. Unstable HD and FRV control valve operation due to excessive pressure drops across the
valves. 10 plant trips during first five months of power ascension testing and commercial operation,
most of which were caused by BOP problems. A Study recommended seven modifications to the BOP. These included:
Removing an impeller stage from the Heater Drain Pumps. Replacing the pneumatic controllers on the #4 FWHs, #5 FWHs, and MSR Drain Tanks with
electronic level controllers. Trimming the Main Feedwater Pump impellers.
The result was significantly more stable and reliable plant operation. The modifications continued to work effectively for the next 25 years of operation.
5
Atypical System Characteristics
No Heater Drain Tank. Small level transients often result in a Heater Drain Pump trip.
Variable speed Condensate Booster Pumps. Heater Drain Pump trips have a small impact on overall plant output.
Make and model of electronic controllers are unique to the Heater Drain System. Knowledge of controllers eventually began to fade. Knowledgeable personnel (with few exceptions) moved on.
First 20 years - System largely operated and maintained by tribal knowledge and as-needed corrective maintenance.
6
Overall Timeline of NCRs December 1, 2010 – March 5, 2013
7
Attachment 3 Overall Timeline of NCRs
December 1, 2010 – March 5, 2013
Note: Three Clusters of Events
4379
8643
8110
4397
29
4397
7443
9824
4398
28
4404
7944
0623
4417
2044
1734
4445
37
4531
8145
4157
4672
87
4695
7146
9850 4742
08
4791
9347
9198
4798
9247
9893
4919
30
5032
0150
3429
5115
03
5186
03
5331
98
5423
7354
3175
5458
18
5517
71 5546
85
5622
08
5652
14
5675
82
5717
2757
2026
5728
3257
2835
5728
7657
3113
5734
3057
3457
5734
7157
3473
5737
2057
3783
5759
96
5862
6958
8010
5884
6258
9179
5895
6358
9576
5897
5259
0483
5915
6759
2296
5923
3659
2995
5938
43
11/1
4/10
11/2
8/10
12/1
2/10
12/2
6/10
1/9/
11
1/23
/11
2/6/
11
2/20
/11
3/6/
11
3/20
/11
4/3/
11
4/17
/11
5/1/
11
5/15
/11
5/29
/11
6/12
/11
6/26
/11
7/10
/11
7/24
/11
8/7/
11
8/21
/11
9/4/
11
9/18
/11
10/2
/11
10/1
6/11
10/3
0/11
11/1
3/11
11/2
7/11
12/1
1/11
12/2
5/11
1/8/
12
1/22
/12
2/5/
12
2/19
/12
3/4/
12
3/18
/12
4/1/
12
4/15
/12
4/29
/12
5/13
/12
5/27
/12
6/10
/12
6/24
/12
7/8/
12
7/22
/12
8/5/
12
8/19
/12
9/2/
12
9/16
/12
9/30
/12
10/1
4/12
10/2
8/12
11/1
1/12
11/2
5/12
12/9
/12
12/2
3/12
1/6/
13
1/20
/13
2/3/
13
2/17
/13
3/3/
13
3/17
/13
3/31
/13
Key: Black Font – NCRs that were used for event investigation. Red Font – Reactivity Management NCRs Green Font – Quick Hit Self-Assessments
Note distribution of NCRs. Numbers and dates are expected to be illegible.
2010 - 2011 Timeline
8
12/14/104A FWH level
transient
12/22/104A FWH level
transient
12/25/104A FWH level transient &'A' HDP trip
1/2/114A FWH level transient &'A' HDP trip
1/4/114A FWH level transient & 'A' HDP trip
Actions taken: - Instrument functional checks - Tightened tubing on LC-1251A CAUSE NOT IDENTIFIED
Actions taken: - Functional check of 1HD-17 - Visual instrument inspections CAUSE NOT IDENTIFIED
Actions taken: - LC-1251A setpoint adjusted - Monitor LC-1251A output CAUSE NOT IDENTIFIED
Actions taken: - Replaced failed LC-1250A with controller found in TTF - Created PM to replace all electronic LTs and LCs in R17
Summary of 2010/2011 events:
- 5 transients, 3 HDP trips - Initiated by equipment failure - Cause not identified 3 times - New failure introduced resulting in 1/4/11 event
Degraded controller installed
Replaced LC-1250A
(not refuted)
Replaced LT-1250A (cause)
2012 - 2013 Timeline
9
RFO 17Initial PM due for replacement of level controllers and transmitters
11/15/124A FWH level transient &'A' HDP trip
11/16/12Unsuccessful 'A' HDP start
2/11/134B FWH level
transient
2/15/134B FWH level
transient
2/27/134B FWH level
transient
3/2/13Unsuccessful
4BFWH restoration
resulting in ES isolation and 4BFWH level
transient
Old controller LC-1250A not
replaced in R17
Replaced LC-1250A
From 2010/2011 events: PMR processed to replace electronic level controllers and transmitters in R17. LT/LC-1250A was screen out from initial scope due to replacement on 1/4/11.
Obsolete, aged level transmitters installed of unknown shelf life
Defective controller installed
Defective transmitter
installed
Replaced LC-1250B
Replaced LT-1250B
Replaced LC-1250B
(not refuted)
Replaced LT-1250B (cause)
Replace aged controllers and obsolete transmitters in R18 per WO 2217334
Revised OP-136
Revised OP-136
Replaced LS-1251B
OP-136 not revised
Unsuccessful restoration of 4BFWH to 1HD-323 control
(clearance not lifted)
OP-136 inadequacy identified
10
Initiating10 CRs
42%Resulting12 CRs
50%
Not Applicable2 CRs
8%
Event Type
11
12
Part Quality37%
Setpoint Control12%
Design13%
Preventative Maintenance
38%
Plant
13
HU Tool Usage46%
Troubleshooting15%
Risk Perception
39%
People
14
Procurement & Obsolescence
55%
Communication & Task Preview
9%
Procedure Quality
36%
Process
Root Cause
15
• Previous actions taken to address Heater Drain System equipment failures, while appropriate, have not been thorough and intrusive enough to prevent additional failures and associated reactivity management events.
• Until the most recent series of failures, insufficient attention was given to the source, quality, and age of replacement parts.
• In addition, considering the number of Heater Drain System components that can cause a reactivity management event and the goal of minimizing the number of reactivity management events, the establishment of preventative maintenance tasks has not been broad and comprehensive enough.
Contributing Causes
Untimely resolution of obsolescence issues and inadequate shelf life controls resulted in defective components being installed.
Components impacting Reactivity Management were not considered in the initial PM basis development work for the Heater Drain System. The resulting lack of PMs resulted in several initial transients and reactivity management events.
Troubleshooting of Heater Drain System events were not managed effectively. 3 of 10 initiating events resulted in a total of 12 additional events before the System was successfully returned to service.
The portion of OP-136 used to set the alternate level controller setpoints for the 4A and 4B FWHs was found to have deficiencies that contributed to the recurrence and severity of Heater Drain System transients and reactivity management events.
16
Generic Lessons Learned
Systematic troubleshooting is vital. If you don’t have enough data to determine cause, seriously consider restarting equipment to
collect more data, rather than replacing all the parts that potentially could have caused the problem.
Clearly define the roles and responsibilities of personnel on your troubleshooting team and insist management respect and follow the organization established.
Divide data collection and other field work from troubleshooting to allow the troubleshooting team to stay focused and function well as a multi-discipline team.
Don’t be so focused on producing a Support/Refute Matrix or Operational Decision Recommendation, that you short change the data collection and analysis.
17
18