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Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow Irving HAMON, Electronic Materials and Assembly Processes for Space (EMPS) Workshop: 4.05.2011

Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

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Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow. Irving HAMON, Electronic Materials and Assembly Processes for Space (EMPS) Workshop: 4.05.2011. Purpose of the experiments. - PowerPoint PPT Presentation

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Page 1: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Experiments on Solder Column Interposer:

cryogenic cleaning and local laser reflow

Irving HAMON,

Electronic Materials and Assembly Processes for Space (EMPS) Workshop: 4.05.2011

Page 2: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 2

Purpose of the experimentsExperiments conducted to improve properties (solderability, cleanliness) of the connections of an electronic package.

This package integrates in a single component every functions of the satellite calculator.

Solder columns have been chosen as an example: some of the following results derived from the experiments could apply to other types of connections (solder balls, leads…) or even boards

Electronic package

ceramic

Solder columns ensuring the connection from the die to the substrate

Page 3: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 3

Solder Column Interposer (SCI)

the Solder Column Interposer (SCI) is made of a ceramic plate in which the array of solder columns are inserted. Basically, the attachment of SCI on the CLGA is made by reflowing eutectic solder bumps at the top of the SCI to form the package ready to be assembled in the end (CCGA for Ceramic Column Grid Array).

Sn10Pb90

Page 4: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 4

Assembly qualification Previous assembly qualification conducted in 2007 showed a poor reliability of

solder columns. During the qualification test programme (vibration + shock + thermal cycling), large voids and cracks within the solder joints were noticed on external rows of the array of columns.

The occurrence of such defects lead to end the qualification earlier than expected.

Cross sections of solder columns: left: defect-free, right: voids within the solder joint on an external row

Page 5: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 5

Defects observed after investigations

Investigations carried out proved that columns were porous and that porosities may tend to propagate during tests within the solder joints to create the voids observed.

SnPb column SnPb column

voidingoutgassing during thermalcycles

Visual inspection also showed the presence of organic contaminants at the end of the columns (green spots on the picture).

The following goes through the different improvements made to recover correct results.

Page 6: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 6

The study was broken down into 4 main steps:

SCI assembly on the CLGA Improvement of SCI reliability Package board assembly Thermal cycling

Page 7: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 7

Improvement of SCI reliability

2 major actions were performed to improve SCI reliability:

pollution removal by using a cryogenic cleaning method

solderability improvement and porosities mitigation by local laser reflow

Page 8: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 8

Improvement of SCI reliability

Pollution removal by cryogenic cleaning (technique developped by Air Liquide)

principle of cryogenic cleaning

projection of particles of dry ice on the surfaces to be cleaned

• infra red thermocouple + electrostatic

fieldmeter utilized during the experiment

nozzle

Page 9: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 9

Improvement of SCI reliability

Results after cryogenic cleaning temperature ranged between -1 to 8°C only 30 s is sufficient for cleaning electrostatic charges can be generated during the process surface roughness can be modified Inspection under UV light: green spots indicates the presence of

contaminants. More than 95% removed after cryogenic cleaning. Good method to remove contaminants

before cleaning after cleaning

Page 10: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 10

Improvement of SCI reliability

Results after cryogenic cleaning

left: before cleaning, right: after cleaning

surface roughness modified after processing

Page 11: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 11

Improvement of SCI reliability

Results after cryogenic cleaning

good results obtained, some improvements are necessary to be compliant with the electronic industry:

- charge generation: air deionizer necessary to prevent charge generation

- visual aspect after cleaning: impact of dry ice particles diameter on surface roughness to be optimized

Page 12: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 12

Improvement of SCI reliability

obtaining a smooth surface to regain a better solderability

SnPb column

laser

voids Aim:

forming a protective layer to prevent voids from coming out of the solder columns

Local reflow of the column tip by Laser reflow

SnPb column

Page 13: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 13

package

Laser beam

N2 flux

Improvement of SCI reliability Local reflow of the end of the column by Laser reflow

Page 14: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 14

Improvement of SCI reliability

Results after Laser reflow smooth surface obtained after Laser reflow. Controlled reflow that keeps the geometry of the columns after process.

Before laser processingBefore laser processing After laser processing

Page 15: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 15

Improvement of SCI reliability

Results after Laser reflow smooth surface obtained after Laser reflow. Controlled reflow that keeps the geometry of the columns after process.

Before laser processing :Rough surface

After laser processing: : smooth surface

Page 16: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 16

Improvement of SCI reliability

Solderability test

1 Part subjected to solderability testing after cryogenic + Laser reflow.

Reference standard: NF-A-89400 dip test flux used: C25D (RMA) immersion time = 5s temperature of solder bath = 235°C

measurement of the contact angle

- measurement of the force F

- visual inspection

SnPb column

Page 17: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 17

Improvement of SCI reliability Results after solderability test

not good according to the standard (slow wetting) but correct from an optical point of view (height of wetting area greater than the immersion depth) and better than previous solderability tests performed in the past (with regards to the height of wetting area)

Usually, with no treatment

After laser reflow

Page 18: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 18

Board assembly

3 parts were assembled on board:

1 part not processed 1 part subjected to cryogenic cleaning and Laser reflow 1 part subjected to Laser reflow (not polluted by contaminants)

Parts subjected to 500 Thermal Cycles (-55/100°C)

assembly after Laser reflow

Laser marking

Page 19: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 19

Results after 500 Thermal cycles

same behaviour for the 3 parts cracks within the solder joints (left picture) & solder shrinkage (right)

Laser markingcrack

Page 20: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 20

Cross section after 500 Thermal cycles

part not processed (left). Laser processed (right)

Page 21: Experiments on Solder Column Interposer: cryogenic cleaning and local laser reflow

Date - 21

Conclusion

The attempt to improve the SCI reliability failed; the same behaviour as during the first assembly qualification was observed (void, cracks within the solder joints).

Cleaning method (cryogenic cleaning) and Laser reflow: good techniques to regain better physical aspects and physical properties (solderability), but not enough in this case to counterbalance structural defects within the SCI.