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KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
1
19th National Award for “Excellence in Energy Management – 2018”
Confederation of Indian Industry
Presentation by ,Kirloskar Oil Engines Limited (KOEL)
Kagal, Kolhapur Plant
Mr. NN Kulkarni-Corporate Energy ManagerMr. VM Deshpande-Sr. GM-Maintenance & UtilitiesMr. SP Parab-Sr. Manager-Utilities
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
2
Content of the Presentation
Company profile
Specific Energy Consumption (Last 3 years)
Information of Competitors, National and Global Benchmarks
Energy Saving Projects for last 3 years
Innovative projects implemented 2017-18
Utilization of Renewable energy
Utilization of waste as a fuel
GHG Inventorisation
Green Supply Chain
Team Work, Employee involvement and monitoring
Implementation of corrective / preventive actions from ISO 50001, IGBC and GreenCorating
KIRLOSKAR OIL ENGINES LIMITED
Kirloskar Oil Engines Ltd-Kagal plant
Total Employees as on date
- 1181
Managers ( TL, GL & UL)
- 191
Operators (Team Associates)
- 990
Initiatives
5S
QMS, EMS & OHSAS
ENCON
Kaizen & POKA YOKE
Autonomous Maintenance
Six Sigma, QC Activities
Standardized Work
TPS
Kagal ( Kolhapur ) Plant
3
Incorporated in 1946 as a part of the Kirloskar Group of Companies, KOEL is an engineering conglomerate, founded by the late Mr. Laxmanrao Kirloskar.
KIRLOSKAR OIL ENGINES LIMITED
Specific Energy And Water Consumption•Reduce by 3-5% every year over next tenyears.
Specific Generation Of Waste & WasteGoing To Land Fills•Reduce by 3-5% every year over next tenyears
Use Of Renewables Energy• Increase by 5% every year over next tenyears.
GHG Emissions And Other ProcessEmissions•Reduce by 3-5% every year over next tenyears
Recyclable And Enhance Recyclability OfResources• Increase use of resources embedded in theproduct.
Share Of Harvested Rainwater In TheOverall Annual Use Of Water• Increase by 5% every year over next tenyears
Life Cycle Assessment Criteria For NewProducts.• Incorporate Life Cycle Assessment inalternative technologies and products.
Adopt Green Purchase Policy•Adopt Green Purchase policy &incorporate clean technologies at designstage
Product Stewardship Program•Promoting and managing ProductStewardship Program, By forgingpartnership with business and communities.
Depletion Of Natural Capital•Reduce by 5% every year over next tenyears
KOEL adopted CII program Mission for Sustainable Growth - 2007
4
KIRLOSKAR OIL ENGINES LIMITED
Executive Chairman Shri. AtulKirloskar signed Energy Policy -indicates Strong Commitmentfrom Top Management towardsENCON
3rd Revision in repsect toChanges in Global EnergyScenario
KOEL- Energy Policy
5
Key
Hig
hlig
hts
of
Po
licy
Benchmarking of products with the regional and national best.
Procurement of high energy efficient products and technologies
Eliminating wastage of energy and promoting reuse and recycling of
resources
Promoting and increasing use of renewable energy resources, within
and outside
Adopting New Building Norms
Involving all stake holders in the energy conservation
Sharing and enriching our experiences on energy conservation within &
Outside group
In line with the
requirements of ISO 50001
EnMS
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
ENERGY CONSERVATION
Share of various sources of Energy FY17-18
32.9%
18.6%
39.8%
8.7%
MSEDCL Renewable energy HSD
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
ENERGY CONSERVATION
Cost wise Share of various sources of Energy (Rs. M) FY17-18
113.152
17.659
77.417
10.007
1.875
MSEDCL Renewable energy HSD LPG FO Biogas Solar canteen
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
ENERGY CONSERVATION
% Share of various sections in Energy Consumption FY17-18
28.66%
9.23%
1.92%10.68%8.28%
5.46%
6.81%0.20%
1.02%
7.19%
20.56%EP-1 Machine shop
EP-1 ME -ATPP
EP-1 SE-ATPP
EP-2 Machine shop
EP-2 ATPP
Genset and fabrication
Common utilities
Fire fighting
ETP
Lighting
Compressor
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Specific Energy Consumption
Year
Specific Energy Consumption
Electricity
kWh/BHP
Thermal
kCal/BHP
2015-16 3.13 0.0023
2016-17 2.68 0.0022
2017-18 2.46 0.0019
Specific Energy Consumption (SEC) Reduction
Year% Reduction in Specific Energy Consumption
Electricity Thermal
2015-16 11% -15%
2016-17 14% 4%
2017-18 8% 14%
KIRLOSKAR OIL ENGINES LIMITED
Reduction in Specific Energy Consumption
Electrical Load of 10000 kW has added in different areas in last few years, still we are able to reduce SEC 1718 by 8% compared to SEC 1617.
0
0.5
1
1.5
2
2.5
3
3.5
2015-16 2016-17 2017-18
3.13
2.682.46
kWh
/BH
P
Specific Electrical Consumption (kWh/BHP) 8% reduction over FY 1617
KIRLOSKAR OIL ENGINES LIMITED
Reduction in Specific Energy Consumption
Various machine lines and testing facilities has added in different areas in last few years, still we are able to reduce SEC 1718 by 14% compared to SEC 1617.
0
0.0005
0.001
0.0015
0.002
0.0025
2015-16 2016-17 2017-18
0.0023 0.0022
0.0019
kCal
/BH
P
Specific Thermal Consumption (kCal/BHP)14% reduction over FY 1617
KIRLOSKAR OIL ENGINES LIMITED
12
Energy Pyramid for Efficient use and adoption of renewable energy
Grid Energy dependency
further reduced by increased
use of Renewable Energy
sources & devices
Energy Requirement
reduced by adoption of
energy efficiency measures,
process changes & new
products
Business As usual
energy requirements
& adopting operating
changes
Sustainability
KIRLOSKAR OIL ENGINES LIMITED
13
Method of arriving at SEC Target
Practice of regression analysis followed in fixing energy consumption andSEC targets.
Help in forecasting, monitoring, targeting energy and other resourcesplanning.
Decision of continuing or stopping production based on fixed and variable energy consumption can be justified
0.80
1.00
1.20
1.40
1.60
1.80
2.00
45000 55000 65000 75000 85000 95000 105000 115000 125000
kWh/BHP
BHP Production
y = 0.3815x + 69590
60000
70000
80000
90000
100000
110000
120000
40000 50000 60000 70000 80000 90000 100000 110000
kWh/month
BHP
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Target setting and Benchmarking
Sr. No
Specific Energy Consumption
Present Status (kWh/BHP) Short term target for specific Energy
Consumption reduction
Long term target for specific Energy Consumption reduction
FY 16 FY 17 FY 18 FY 19 FY 20 FY 21 FY 22 FY23
1Specific Energy Consumption
3.25 2.68 2.462.39(3%
Reduction)
2.32(3%
Reduction)
2.20(3%
Reduction)
2.10(5%
Reduction)
2.00(5%
Reduction)
Involvement of People
Initiated
Advanced EMS for Data Analysis
Installed
Data Analysis and prioritization
Initiated
Adoption of new technologies, Implementation of renewable projects
Implementation
ISO 50001 EnMSCertification, GreenCo Up gradation
Initiated
Certified Lead Auditor - EnMS• Santosh Parab• Nitin Kulkarni
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Target setting and Benchmarking
Parameter Specific Energy Consumption (kWh/BHP)
Year 15-16 16-17 17-18 18-19
Target 3.40 3.03 2.60 2.39
Actual 3.25 2.68 2.462.47
(Till end of quarter 1)
Remarks
Started monitoring with installation of new EMS system
Even though 50% increase in load, 18% reduction over previous year
Even though change in product mix, 8% reduction over previous year
Repetitive proto testing
KIRLOSKAR OIL ENGINES LIMITED
MNC Compititor 1(80 HP to 280 HP)
Kagal (20 HP to 150HP)
11
7.0
0
95
.90
* Source Data : MEDA
Benchmarking (National)
kWh / BHP (Internal)
Energy Consumption per Engine (ATP)
KOEL Pune KOEL Kagaltarget 1718
KOEL KagalBest
Achieved
4.0
1
2.4
6
2.2
5
For Benchmarking kWh / Engine is available from a Close Competitor product
range. Equivalent Conversion taken for KOEL engines
16
Better
KIRLOSKAR OIL ENGINES LIMITED
Compititor1
KOEL Compititor2 (MNC)
30
20
12
Cycle time in Min.
Benchmarking (International)
DG Set Testing Time
Engine Testing Cycle Time
17
Better
0
20
40
60
80
100
120
Competitor 1KOEL Kagal-16
KOEL Kagal-17Competitor 2
120
55
50
30
DG Set Testing Time in Minutes
KIRLOSKAR OIL ENGINES LIMITED
18
Projects implemented to achieve the target for last 3 years
Total No. of
ENCONProjects: 185
Annual
EnergySavings in
kWh
(Units): 29.00Lakh
AnnualFuel Saving(Kcal) :
690.9
Lakh
Total Cost
Saving:
Rs 433
Lakh
Investment
: Rs.
78.3
Lakh
SimplePayback : 3
Months
ROI:98%
Simple Payback : 3 Months
CategoryNo. of
projects
Units
saving
In lakhs
Fuel
saving
lakhs Kcal
Cost
saving
in lakhs
Investment
in lakhs
Low Investment 117 16.1 669.3 183.6 2.4
Moderate Investment 60 9.5 21.6 121.6 7.5
High Investment 8 3.4 0 127.8 68.4
Total 185 29.0 690.9 433.0 78.3
KIRLOSKAR OIL ENGINES LIMITED
19
Projects implemented to achieve the target for last 3 years
42%
28%
30%
Savings in Rs. Lakhs
Low Investment Moderate Investment High Investment
63%
33%
4%
No.of projects completed
Low Investment Moderate Investment High Investment
63% of low investment
project given 42% savings
33% of medium investment
project given 28% savings
KIRLOSKAR OIL ENGINES LIMITED
20
FY 2015-16
KIRLOSKAR OIL ENGINES LIMITED
Low Investment Projects
21
S.No. Title of Project Year
Annual Electrical Saving, Million
kWh
Annual Electrical
Cost Saving,
Rs Million
Annual Thermal Saving, Million
kcal
Annual Thermal Saving,
Rs Million
Total Annual Savings,
Million Rs
Investment Made (Rs
million)
Payback months
1 Conversion cost reduction by saving fork lift diesel 2015-16 6.30 0.21 0.21 0.00 0
2 To reduce the power consumption of hydraulic motor on leak test machines 2015-16 0.022 1.89 1.89 0.00 0
3 To reduce consumption of K cool 2015-16 2.40 0.30 0.30 0.00 0
4Elimination of Diesel wastage during 6R Engine Rigging & De-rigging in Test Cell 2015-16 0.15 0.04 0.04 0.00 1
5Reduce fuel consumption for DV Test Cell No.1 2015-16 4.53 0.27 0.27 0.00 0
6 Power Saving in Idle condition 2015-16 0.007 0.06 0.06 0.00 0
7 Power Saving in Idle condition 2015-16 0.001 0.01 0.01 0.00 0
8 Power Saving in Idle condition 2015-16 0.0006 0.01 0.01 0.00 0
9 Power Save from running instead of one MTR.than two 2015-16 0.001 0.01 0.01 0.00 0
10 Power Save from running instead of one MTR.than two 2015-16 0.0074 0.07 0.07 0.00 0
11 Power Saving in Idle condition 2015-16 0.002 0.02 0.02 0.00 0
12 Power Saving in Idle condition 2015-16 0.0004 0.01 0.01 0.00 0
13 Power Saving in Idle condition 2015-16 0.002 0.02 0.02 0.00 0
14 Power Saving in Idle condition 2015-16 0.0054 0.05 0.05 0.00 0
15 Save wastege of air when guage not in use 2015-16 0.015 0.14 0.14 0.00 0
16 Save wastege of air when guage not in use 2015-16 0.07 0.07 0.07 0.00 0
17 To reduce the power consumption of bush press hydr motor running 2015-16 0.004 0.04 0.04 0.00 0
18
Paint Booth flame proof Light Continuous power ON for shift. Even if no engine or part for painting
2015-160.018
0.01 0.01 0.00 0
Total 0.156 2.387 13.380 0.813 3.200 0.008
KIRLOSKAR OIL ENGINES LIMITED
22
Moderate Investment ProjectsInvestment between Rs. 1 Lakh – 10 Lakh
S.No. Title of Project Year
Annual Electrical Saving, Million
kWh
Annual Electrical
Cost Saving,
Rs Million
Annual Thermal Saving, Million
kcal
Annual Thermal Saving,
Rs Million
Total Annual Savings, Million
Rs
Investment Made
(Rs million)
Payback months
1Energy saving by replacing non energy efficient bearing with energy efficient bearing for AHU blower motor.
2015-160.032 0.27
0.27 0.03 1
2Save wastege of air when guage not in use 2015-16
0.23 2.092.09 0.01 0
3Power Saving by using LED Bulb 2015-16
0.001380.01 0.01 0.03 30
4Coolant wastge elimination 2015-16
2.160.00 0.00 0.01 21
5Energy cost reduction through cycle time reduction on DV crank case line Op-80 2015-16
0.0170.17 0.17 0.05 4
Total 0.280 2.542 2.160 0.003 2.545 0.116 0.547
KIRLOSKAR OIL ENGINES LIMITED
23
High Investment Projects Investment > Rs. 10 Lakh & above
S.No. Title of Project Year
Annual Electrical Saving, Million
kWh
Annual Electrical
Cost Saving,
Rs Million
Annual Thermal Saving, Million
kcal
Annual Thermal Saving,
Rs Million
Total Annual Savings,
Million Rs
Investment Made (Rs million)
Payback months
1To reduce Energy consumption of R1040 Assembly lighting 2015-160.072 0.97
0.97 0.54 7
2To reduce Energy consumption of EP2 Machine shop lighting 2015-160.048
0.41 0.41 1.60 47
Total 0.120 1.378 - - 1.378 2.140 18.636
KIRLOSKAR OIL ENGINES LIMITED
24
FY 2016-17
KIRLOSKAR OIL ENGINES LIMITED
Low Investment Projects
25
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, Rs Million
Annual Thermal Saving, Million kcal
Annual Thermal Saving, Rs Million
Total Annual Savings, Million Rs
Investment Made (Rs million)
1 HA6CC, Op40, Intermediate washing m/c heater elimination & CT optimization 0.004 0.03 0 0.033 Nil
2 HA6CC, Op140, Continuity test m/c heater elimination 0.004 0.04 0 0.036 Nil
3
HA6CC, Op10/130, Cleaning tool eliminated by replacing with thro' coolant tool (6mins) & M.C. cutting parameter optimized (4mins)
0.011 0.09 0 0.093 Nil
4 HA6CC, Power cost saving thro' optimization of tool magzine rotation on HMC 0.001 0.01 0 0.005 Nil
5 HA6CC, Op120, CT reduction by changing the Thrust tool cutter 0.002 0.02 0 0.020 0.2
6 HA6CC, Op100, Power saving mode introduced 0.005 0.04 0 0.040 Nil
7
HA6CC, Op150, Power saving thro' elimination of heater by use of CUMI make washing media
0.012 0.10 0 0.100 Nil
8 DVCBX, Washing m/c CT optimization 0.002 0.02 0 0.019 Nil
9 DVCBX, To reduce the comp washing frequency on washing m/c 0.002 0.02 0 0.021 Nil
10 DVCBX, Op30/50 CT reduction 0.018 0.15 0 0.154 Nil
11 DVCBX, Op40 CT reduction by cutting parameters optimisation 0.009 0.08 0 0.080 Nil
12 DVCC, Op110, Hyd motor ON/OFF during only cycle start/off 0.014 0.12 0 0.121 Nil
13
DVCC, Op50, 60, 80, Tool no sequencial arrangement to save power during magazine rotation
0.009 0.08 0 0.077 Nil
14
DVCC, Op60, CT reduction implementing Lakshya suggestions & rearranging the tool sequence
0.005 0.04 0 0.040 Nil
15 DVCC, Op10, Reducing the temp range of washing media 0.009 0.07 0 0.073 Nil
16 DVCC, Op90, Elimination of heater on washing m/c 0.129 1.10 0 1.099 Nil
17
Energy Saving through Hydaulic power pack optimization at Toyoda Top center - R1040 Crank case line & Crank shaft line
0.00528 0.522 0.520
18 Varsha Paintbooth water tank level optimisation 0.003 0.22 0.22 0
KIRLOSKAR OIL ENGINES LIMITED
Low Investment Projects
26
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, Rs Million
Annual Thermal Saving, Million kcal
Annual Thermal Saving, Rs Million
Total Annual Savings, Million Rs
Investment Made (Rs million)
19Energy Saving through Hydaulic power pack optimization at OP-170 at Crankshaft line 0.00043 0.003836 0.00
020 Reduce power cost of RCH line OP 40 by modification of PLC logic. 0.00156 0.01404 0.01 021 Reduce power cost of RCH line OP 30 by modification of PLC logic. 0.001989 0.0179 0.02 022 Energy saving by optimize Hydraulic power on Pressing machine RCH Op80 0.016728 0.1505 0.15 0
23EP2 --Stop the HYD .motor and Chip conveyour motor to run in ideal mode of 15 min . Machine No : 2636
0.001923 0.017313 0.017 0
24EP2-- Power saving logic implemented for Ideal run for Hyd , coolant and maganatic sepetor Motor Machine No : 2842
0.009324 0.058287 0.058 0
25 EP2 --Stop the HYD .motor to run in ideal mode of 10 min . Machine no 6739 0.008165 0.083916 0.084 0
26EP2--Power saving of induction motor In ideal cycle time of 15 Min . Machine no 5418 0.008514 0.073483 0.073 0
27EP2--Power saving of induction motor In ideal cycle time of 15 Min. Machine no 5405 0.013986 0.076621 0.077 0
28EP2--Instead of two one power pack is used to save the Enegry . Machine no 6726 0.000312 0.086148 0.086 0
29EP2--Hyd oil chiller will on only after control on ,previsoly it will on when machine main supply on . Machine no 2974
0.000312 0.002808 0.003 0
30EP2-- Hyd oil chiller will on only after control on ,previsoly it will on when machine main supply on . Machine no 2977
0.016464 0.002808 0.003 0
31 EP2--Power save of HYD press on camshaft .Machine no 7043 0.000005 0.148176 0.148 032 EP2--Machine lamp made switched off after EMG. PB pressed .Machine no 5433 0.003978 0.000045 0.000 033 EP2--Compressed air made off after EMG P.B Pressed .Machine no 5433 0.00171 0.034992 0.035 0
34EP2--Power saving logic implemented in ideal run to avoided the running of motor of HYD and chip conveyor . Machine No 931
0.004623 0.001709 0.002 0
35EP2--Power saving logic implemented in ideal run to avoided the running of motor of DM and Qunch .Machine No 8109
0.0225 0.04158 0.042 0
36EP2-- Power saving with alternate use of chemical in washing machine .Machine no OP 150 HA CRANK CASE
0.00432 0.2025 0.203 0.0095
37 EP2--Power saving with alternate use of chemical in washing machine 9041 0.0084 0.02616 0.026 0.00115238 EP2--Power saving with alternate use of chemical in washing machine 7800 0 0.1566 0.157 0.01152
39EP2--Interface flow control valve in pnumatic line which reduced the pressure from 6 bar to 2 bar 0.0003 0.00255 0.003 0.01
KIRLOSKAR OIL ENGINES LIMITED
27
Moderate Investment ProjectsInvestment between Rs. 1 Lakh – 10 Lakh
S.No. Title of Project
Annual Electrical Saving, Million
kWh
Annual Electrical
Cost Saving,
Rs Million
Annual Thermal Saving, Million
kcal
Annual Thermal Saving,
Rs Million
Total Annual Savings,
Million Rs
Investment Made (Rs million)
1To Provide electrical switch/autosenses near to the core plug pressing station on DV-Cylinder Head Line on OP-80 station 0.000941 0.008
0.0080.0002
2
To save electrical power cost by providing separate hydraulic motor ON/OFF system on OP40/50 Pressing machine & also provide only one hydraulic system for two m/c in single piece flow On R810 Cylinder head line
0.016118 0.1370.137
0.003
3
To save electrical power cost by activating hydraulic motor in power saving mode instead of continuously running in idle condition with in house modification in PLC logic on op-80 WIDMA m/c on 6R6K Cylinder head line
0.001024 0.0090.009
0
4To save electrical power cost by use 250 kg crane against 500 kg at input conveyor (component wt only 8 kg)on SL-90 Cy.head line 0.000353 0.003
0.0030
5 Reduce HA Crankcase line power consumption from 14.59 Units/Cyl. to 13 Units/Cyl. 0.070421 0.669 0.669 06 Reduce HA Crankcase line Air(power) consumption cost 0.009474 0.090 0.090 0.00157 To save electrical power cost on Micromatic (OP 70) m/c 0.006 0.050 0.050 08 To save electrical power cost on Toyoda (OP 80A) M/c 0.006 0.050 0.050 0
9To use the washing machine coolant at room temperature instead of hot coolant which is heated up to 55 to 60 degree Celsius 0.190737 1.812
1.8120
10 To reduce power consumed in heaters at OP130 final washing machine 0.010706 0.091 0.091 0
11To save 50% electrical power cost by Utilize all washing stations by using second chamber & start to wash at time two component in single cycle ( op-70 ) 0.01 0.085
0.0850.001
12 To reduce power consumption on rough washing machine on 6R/HA6 Crankshaft line 0.005529 0.047 0.04713 To reduce power cost by reducing cycle time of washing machine 0.002353 0.02 0.02014 DV CON ROD- Maintain line power consumption below 23kwh per component 0.037895 0.360 0.360 015 To eliminate heater of continuity test machine OP140 0.005059 0.043 0.04316 Reduce air consumption On r1040 crankcase line 0.003368 0.032 0.032 0.00217 Air consumption to be reduced when APG not in use 0.007053 0.067 0.067 0.00518 Power Consumption Saving on OP150 A , SL90 Lapping M/c 0.000588 0.005 0.00519 Power Consumption Saving on OP50, Fortuna M/c 0.000471 0.004 0.00420 Power Consumption Saving on OP140, Balancing M/c 0.000824 0.007 0.00721 To Reduce power cost by disconnecting mist collector on Op-85 0.005053 0.048 0.048 0
22To save electrical power cost on Streightening (OP 40), Micromatic (OP 70), Toyoda (OP 80A) & Washing (OP 120) M/cs 0.021 0.180
0.1800
23 To save electrical power cost by eliminating dirty tank coolant transfer 0.014 0.115 0.115 0
24To save Compressed air cost on Horizontal Induction Hardening (OP 20), Landis (OP 50), Micromatic (OP 70), & Radial Drilling (OP 100) M/cs 0.001 0.008
0.0080.002
KIRLOSKAR OIL ENGINES LIMITED
28
Moderate Investment ProjectsInvestment between Rs. 1 Lakh – 10 Lakh
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, Rs Million
Annual Thermal Saving, Million kcal
Annual Thermal Saving, Rs Million
Total Annual Savings, Million Rs
Investment Made (Rs million)
25 To reduce power consumption of OP100 by keeping machine in power saving mode 0.013 0.107 0.107 0
26Reduce power cost of RCH line by using single power pack for both Valve seat & valve guide pressing on op-80
0.015789 0.1500.150
0
27 Make separate ON/OFF Switch for Marposs Gauge 0.001209 0.105 0.105 0
28 Power consumption saving on OP180 , Final Washing m/c 0.008941 0.076 0.076
29 Power consumption saving on OP100, TAL M/c 0.000353 0.003 0.003
30 To Reduce Power consumption of hydraulic motor on OP80 WIDMA machine 0.001059 0.009 0.009 0
31 To Reduce Power consumption of hydraulic motor on v/s & v/g pressing machine 0.016118 0.137 0.137 0
32
To Reduce Electrical Power consumption on SL90 cylinder head line by changing man- machine work combination with cell wise time study 0.019292 0.164
0.1640
33
To Reduce Electrical Power consumption on R810 cylinder head line by changing man- machine work combination with cell wise time study 0.006 0.051
0.0510
34
To optimize compressed air flushing time on primary washing machine & save compressed air cost with ZERO investment 0.011412 0.097
0.0970
35
To Provide electrical switch/autosenses near to the core plug pressing station on DV-Cylinder Head Line on OP-80 station 0.000941 0.008
0.0080.0005
36
To save electrical power cost by use 250 kg crane against 500 kg at input conveyor (component wt. only 8 kg)on SL-90 Cyl.head 0.000353 0.03
0.030
37 Hot cure tank cleaning & DM water changing frequency is changed from once in a month to twice in a month 0.001684 0.016 0.016 0
38 To Reduce Power consumption cost by reducing cycle time of OP120 0.011579 0.110 0.110 0
39 Optimize Heating temp. ( OP- 80) for Final Washing on Camshaft line 0.02225 0.20025 0.200 0
40
To reduce power consumption cost from Rs.11.5 per cylinder to below Rs.10 per Cylinder, on R14040 Crankcase line 0.038211 0.363
0.3630
41
To reduce electrical cost by switch off the hitters while machine keep in emergency mode on op-70 ( Final washing) R810 cylinder head line 0.002942 0.025
0.0250
42 To reduce the Electrical power cost on OP-40 washing m/c on DV Cylinder head line 0.008471 0.072 0.072 0
43 Final Conveyor -Make Separate ON/OFF Switch for Tube , Fan ,Bulb . 0.000243 0.0213 0.021 0
44 Tooling Area Make Separate ON/OFF switch for Tube ,Fan , Pre Setter . 0.000248 0.02162 0.022 0
45 op-30 Mist Collector OFF during PDT . 0.001904 0.167 0.167 0
46 op-170 Torquening M/c logic modification for Integral model 0.001925 0.168 0.168 0
47 DV CON ROD- Reduce power consumption by providing power saver to op.120 0.007842 0.074495 0.074 0
KIRLOSKAR OIL ENGINES LIMITED
29
High Investment Projects Investment > Rs. 10 Lakh & above
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, RsMillion
Annual Thermal Saving, Million kcal
Annual Thermal Saving, RsMillion
Total Annual Savings, Million Rs
Investment Made (Rsmillion)
1 Energy efficient lighting 0.191 2.92 2.92 1.37
2 Solar roof top pumping system 0.029 0.25 0.25 1.61
3 Bio gas generator 0.0072 0.06 0.06 1
4 Rainwater Filtration plant 0.32 0.32 0.6
5 Open access Renewable energy purchase 5.047 5.05
6Cost saving through improving diesel draining process at Genset PDI lines 2.8
2.800.116
KIRLOSKAR OIL ENGINES LIMITED
30
FY 2017-18
KIRLOSKAR OIL ENGINES LIMITED
Low Investment Projects
31
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, Rs Million
Annual Thermal Saving, Million kcal
Annual Thermal Saving, Rs Million
Total Annual Savings, Million Rs
Investment Made (Rs million)
1 To eliminate air leakage of OP10 washing m/c 0.027 0.230 0.23 0.00
2 To reduced cycle time of DV 16 cc for PCN operation 0.001 0.007 0.01 0.00
3 To reduce power consumption in continuously coolant gun motor 0.002 0.013 0.01 0.00
4 To reduced cycle time of DVCBX R56 milling operation 0.008 0.064 0.06 0.00
5 To reduce the CT of OP70 by optimizing the cutting parameter 0.006 0.050 0.05 0.00
6 To reduce the CT of OP110/130 by optimizing the cutting parameter 0.003 0.022 0.02 0.00
7To reduced the power consumed in heating washing media on HA6CC, DVCC, R810CH, DVCH & SL90CH line
0.783 6.650 6.65 0.00
8 LPG cost reduction 53.55 0.191 0.19 0.00
9 To reduced power consumption by operation shifting 0.002 0.014 0.01 0.00
10 To reduce power consumption by implementing power saving mode in M/c 0.001 0.005 0.01 0.00
11 To reduce power consumption in idle condition due to hydraulic motor continuously ON 0.001 0.008 0.01 0.00
12 To reduce power consumption in idle condition due to chip conveyor continuously ON 0.002 0.014 0.01 0.00
13 To improve capacity by using combination tool for 6R BS3 0.002 0.020 0.02 0.00
14 To reduce cycle time by using combination tool for CRDI models 0.008 0.027 0.03 0.00
15 To reduce cycle time by eliminating probe cycle from mazak machine 0.003 0.027 0.03 0.00
16 To switch off nozzle operation from widma machine 0.003 0.023 0.02 0.00
17 To eliminate the pneumatic stopper from input stage 0.002 0.021 0.02 0.00
18 To improve line capacity by 45% 0.023 0.198 0.20 0.00
19 To improve line capacity by 10% 0.008 0.066 0.07 0.00
20Power saving logic implemented for Ideal run for , coolant chiller and magnetic separator Motor. 0.058 0.06 0.00
21Made selector switch is provided to on & off of 11 watt Tube light near Magazine. As tube light is runing when machine on .
0.004 0.00 0.00
22Selector switch is provide at Front side of operating panel for making on/off machine lamp at loading/unloading section .
0.004 0.00 0.00
23Foot switch used for Pneumatic Baker gauge which will stop the air when gauge is not used 0.035 0.04 0.00
KIRLOSKAR OIL ENGINES LIMITED
Low Investment Projects
32
S.No. Title of Project
Annual Electrical Saving,
Million kWh
Annual Electrical
Cost Saving, Rs Million
Annual Thermal Saving,
Million kcal
Annual Thermal Saving,
Rs Million
Total Annual Savings,
Million Rs
Investment Made (Rs million)
24Foot switch used for Pneumatic Baker gauge which will stop the air when gauge is not used 0.035 0.04 0.00
25Saving the electrical enegry for unneseery ruing of HYD motor during unclamping cycle. 0.084 0.08 0.00
26 External Fixture Flushing kept off during auto cycle 0.8 0.80 0.00
27Power cost saving on DV con rod line. 0.020 0.18 0.18 0.0028Power cost saving on HA con rod line 0.067 0.60 0.60 0.0029Power cost saving on HA Crank Case line 0.082 0.08 0.0030Power cost saving on HA Crank Case line 0.007 0.062 0.06 0.0031Power Consumption reduction 0.020 0.183 0.18 0.0032One engine testing for ten 3R engines of reliance code 0.002 0.021 0.05 0.07 0.00
33To reduce electricity consumption through modification in cooling tower fan motor starter 0.1 0.10 0.00
34Reducing the electric power consumption for DV Test Cell No.1 when engine not present for testing. 0.03 0.03 0.00
35Reducing the electric power consumption for DV Test Cell No.1 during test cell empty 0.03 0.03 0.00
36E-series canopy & base welding and finishing reduction 0.014 0.01 0.00
37Terminal box welding reduction 0.002 0.00 0.00
38DV integrated base welding reduction 0.013 0.01 0.00
39DV & SL90 baseplate rib cutting shifted from laser cutting to shearing machine0.010 0.01 0.00
40Elimination of use of EOT crane for Loading & unloading of fabricated material 0.205 0.21 0.00
41Energy conservation in D8.5325 baseplate laser cutting by reducing piercing & common cutting0.012 0.01 0.00
42To elimimnate latch catcher plate laser cutting by punching & shearing for all canopy0.019 0.02 0.00
43To reduce the power consumed in heating the washing media 0.017 0.14 0.14 0.00
44
To reduce Energy consumption of Gurukul and improve the illumination level 0.075 0.9 0.09 0.00
45Oil skimmer power saving on MAZAK FH7800 HA CRANK CASE M/C No : 0.02 0.02 0.00
KIRLOSKAR OIL ENGINES LIMITED
33
Moderate Investment ProjectsInvestment between Rs. 1 Lakh – 10 Lakh
S.No. Title of Project
Annual Electrical Saving, Million kWh
Annual Electrical Cost Saving, Rs Million
Annual Thermal Saving, Million kcal
Annual Thermal Saving, Rs Million
Total Annual Savings, Million Rs
Investment Made (Rs million)
1 We have installed Vaayu MIG24 unit at ME tool room office instead of AC. Comparison of vaayu MIG 24 & AC.
0.019 0.154 0.154 0.20
2Energy/Power cost reduction by utilization of renewable solar energy for heating up the washing tank water at Medium Engines Paint booth.
0.037 0.375 0.375 0.42
KIRLOSKAR OIL ENGINES LIMITED
Innovative Projects 2017-18
34
KIRLOSKAR OIL ENGINES LIMITED
30-Aug-18 35
Innovative Project 1- Elimination of electrical heaters for Component washing machine
Detailed information- Earlier for component washing machines, 5-6% concentration of washing chemical with water was heated to 55-600C to achieve the desirable results with electrical heaters. By replacing washing chemical with “Cumiclean CWF242” same results were achieved at room tempe rature and electrical heaters of the washing machines were eliminated. Throughout the factory, electrical heaters were eliminated for 33 numbers of washing machines. Same will be horizontally deployed for rest of the areas. Before-
Total connected load of electrical heaters-871 KW Electrical consumption per day -2612 kWh Electrical consumption per annum (@ 25 days per month, 12 months a year)- 783450 kWh
Savings achieved-
Savings per annum (@ Rs. 8.5/kWh)-Rs. 6659325/-
KIRLOSKAR OIL ENGINES LIMITED
30-Aug-18 36
Innovative Project 2- Solar Hot water system for Paint booth
Detailed information-Previously EP-1 Paint booth tank washingwater was heated with the help of electricheaters with the help of 4 heaters of 10 kWeach. Water temperature is maintained at50 Deg.± 5 Deg. Power consumptionmeasured was about 320kWh/day. It wasdecided to use solar hot water systemreceived from one of the company premisesto minimize the use of electric heaters byproviding hot water through solar system.After implementation of solar plant to heatup the water only in paint booth degreasingtank the Power consumption observed 200kWh/day.
Total Savings-3.18Lac/annum
KIRLOSKAR OIL ENGINES LIMITED
30-Aug-18 37
Innovative Project 3- Installation of Vaayu unit replacement to conventional AC
DESCRIPTION VAAYU AC
Coverage Area 1000 Sq. Ft 1000 Sq. Ft
MachineVaayu MIG 24
(Nos.1)10 Ton
Power Supply 230V, 1PH, 50Hz 230V, 1PH, 50Hz
Power Input 800 W 10,000 W
Per Hr. Power Consumption 800 W 10,000 W
10 Hr. Power Consumption 8,000 W 1,00,000 W
Monthly Power
Consumption2,40,000 W 30,00,000 W
Units Per Month 240 3000
Tariff @ Average Rs. 7 Rs. 7
Monthly Bill(Approx) Rs. 1680 Rs. 21,000
Yearly Expenses(7 Months) Rs. 11,760 Rs. 1,47,000
Savings Against Ac 92%
Detailed information-
We have installed Vaayu MIG24 unit at ME tool room office
instead of AC. Comparison of vaayu MIG 24 & AC.
KIRLOSKAR OIL ENGINES LIMITED
38
Gayatri Mantra-The source to sustenance
Utilisation of Renewable Energy Sources
KIRLOSKAR OIL ENGINES LIMITED
Renewable Energy-On site Installations
LAKE
KUND
Main
Plant 2
FGL-
588.40
FFL-
588.80
Main
Plant 1
FGL-
588.40
FFL-
588.80
H
M.S.E.B
Plot
A
BC
EF
D D
A - Fixed Axis Solar PV – 3.8 MWp
B – Single Axis Tracking Solar PV- 0.45 MWp
C- Roof Top Mounted Solar PV- 1.25 MWp
D- Admin Building Roof Top Mounted Solar PV- 0.082 MWp
E – Solar Parabola Steam Generator – 350 Kg/Day
F – 1 KW Solar Lighting and15 KW Solar Pumping System
G
G – Biogas Plant and Biogas Generator– 30 Cum / Day
15 KVA Generator
H
H – Solar Hot water System for Paint Booth – 1500 LPD
2
KIRLOSKAR OIL ENGINES LIMITED
Renewable Energy –OA and Solar PV
Windmill and Solar Units
kWh
Units
% of total Energy
consumption
Renewable Energy Used
(FY 15-16)
36,88,500
23.00%
SEM Meter Installation
Renewable Energy Used
(FY 16-17)
58,07,286
36%
Renewable Energy Used
(FY 17-18)
60,98,889
36% Against Target 50%
Obligations from Govt. and MSEDCL after Tariff change
Target
(FY 18-19)
50%
5.5 MWp Solar Captive Power
plant
Open Access energy
purchase
The share of renewable energy in total electrical consumption for FY 17-18 – 36%This has resulted into tremendous saving of Rs. 38 Lakhs
40
KIRLOSKAR OIL ENGINES LIMITED
Renewable Energy –Onsite installations
Units
Present Renewable energy generated
on - site
Present Renewable energy generated
on - site Achievement Target for 2018-19
(Additional 5% wrt 17-18)
(2015-16) (2016-17) In 2017-18
Biogas Plant (Cum.) 5494 6327 5881 6175
Solar Parabola Steam Generator (Kg
of Steam)28361 31991 16872 17715
Solar Pumping (kWh.)
NA NA 6600 6930( Addition of DC Solar Pump )
41
KIRLOSKAR OIL ENGINES LIMITED
Renewable Energy -5.5MWp Solar Captive PV Plant
• Total Plant Capacity-5.5MWp (DC output)
• Total no of solar modules-17220 modules
• Four types of Installations-Rooftop :1.25MWp – 3520 modulesSingle axis tracker ground mounted- 0.45MWp-1680 modulesFixed axis ground mounted – 3.80 MWp-11760 modulesAdmin bldg. roof mounted-0.082MWp- 260 modules
• Approximate yearly unit generation-8040 MWh
• Approximate carbon offset- 6500tons/annum
• Approximate % in total electricity consumption- 50%
• Generation till date- 17,00,000 kWh42
KIRLOSKAR OIL ENGINES LIMITED
43
Utilisation of Waste material as a fuel
Analysis Report received for co processing ( Using alternate fuel ) of paint sludge, ETP sludge,Phosphate sludge and Cotton waste which are our major Hazardous Wastes generates fromprocesses at M/s Ambuja Cement Works which is clearly indicating that above wastes can beco- processed.
We are awaiting for financial proposal from the waste co- processing agency.
Sr. no
Waste name CategoryGeneration Quantity TPM
Moisture Content %
Gross CV cal / gm
NCV (Cal/gm) Calculated
Ash content %
Sulphur %
Chlorides%
pH(5% sol )
Observations & comment
1 Paint Sludge 21.1 3.5 38 2560 2163 24.39 0.27 0/03 6.67
Waste can be co-
process in cement
kiln.
2 ETP sludge 34.3 8 78.43 388 NIL 12.52 0.02 0.003 7.7
3Phosphate sludge
12.5 0.8 73.27 39 NIL 21.5 0.002 NIL 3.85
4Cotton Waste
5.2 1 7.75 6094 5623 3.2 0.28 0.09 8.3
35% Hazardous WasteCan be Co-Processed
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LTD., KAGAL – RKQP 29th July’14KIRLOSKAR OIL ENGINES LTD. 40
We have 350-400kkg/daybiogas capacity with a gasgeneration of about 25-30cum/day. Part of the gas isused for canteen thermalapplication & remaining gas isfed to biogas generator togenerate electricity.
All street lights of EP1 and
Genset plant will be powered
by Biogas Generator
Daily electricity generation-25 to 30kWh/day
Utilisation of Waste material as a fuel
Generation started from May-17
Generation till date-9000 kWh
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LTD., KAGAL – RKQP 29th July’14KIRLOSKAR OIL ENGINES LTD. 40
GHG Inventorisation
Carbon Foot Print Report Data - Kagal-1 Plant Sr. No. Source Scope Unit Consumption GHG Emission (tco2)
FY15-16 FY16-17 FY17-18 FY15-16 FY16-17 FY17-18
1 HSD 1 kl 972.00 1,139.00 1,295.00 2,552.08 2,990.56 3,400.15
2 LPG 1 kg 184,870.00 162,478.00 195,034.50 554.61 487.43 585.10
3 FO 1 kl 28.73 26.77 58.29 85.59 79.76 173.65
4Compact Natural Gas (CNG)
1 SCM - - - - -
5 CO2 for cutting 1 kg - - - - -
6 CO2 for welding 1 kg - - - - -
7 CO2 in fire extinguisher 1 kg - - - - -
Total Scope 1 = 3,192 3,558 4,159
Scope 2
1 Electricity Purchased 2 kWh 11,954,222 10,161,709 10761047 10,907 9,271 9,818
Total Scope 2 = 10,907 9,271 9,818
Offset
1 Electricity Renewable kWh 4,038,736 5,807,286 6098889 3,685 5,299 5,565
2 Biogas m3 5,494 6,327 5880.5 10 12 11
3 Solar kg of steam 28,361 31,906 16872.25 0.00 0.00 0.00
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LTD., KAGAL – RKQP 29th July’14KIRLOSKAR OIL ENGINES LTD. 40
GHG Inventorisation
Action started to offset carbon footprint from FY16-17Difference between Total emission and Offset -5240 Tons of CO2 FY17-18
Sources of Emission:Scope 1- In house consumption of HSD, LPG, Refrigeration, CO2 Cylinders etc.Scope 2- Purchase of electricityScope 3- Will be started in FY 1819
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Green Supply Chain
Supply Chain Policy
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Green Supply Chain
Activities at Supplier EndSr.
NoSupplier Name Audit Name Faculty
Conducted in
year
Duration
(Hr.)
1 KFIL Supplier Process Audit Mr. Abhijit Koparde
2016-17 8 Hr
2 Rajrajeshvari Supplier Process Audit Mr. AbhijitKoparde
2017-18 8 Hr
3 K K Foundry Supplier Process Audit Mr. Abhijit Koparde
2017-18 8 Hr
4 Jadhav Industry Supplier Process Audit Mr. Suresh Patil
2017-18 4 Hr
5 Sound Casting Supplier Process Audit Ajit Konkire 2017-18 6 Hr
580600620640
Before After
63
5
61
0
K K Foundry
Furnace Energy Units / ton
0
5
Before After
1
2.5
Jadhav Industry
Saving in Rs. Lac
1200
1300
1400
Before After
13
50
12
50
Sound Casting
Plant Units…
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Milk Run -Model
Before Milk Run
After Milk Run
Delivery To KOEL
Return To Supplier
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
Milk Run -Model/Vehicle Optimization
Present Traffic Incoming Avg. 77 vehicle entries/day. - Aprox. 21% reduction
Avg. monthly Diesel Consumption 2200 ltrs. - Approx. 12% reduction
Reduction Freight Payment by 4.13 Crs in last three years. - Avg. 13.8 % reduction per year.
Advance information Proactive alerts.
Reduced personal visits .
Defined accountability & Responsibility.
Improved relationship .
KIRLOSKAR OIL ENGINES LIMITED
51
Employee Involvement
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
ENCON Awareness Creation Celebration ENCON WEEK Every Year (14 Dec. to 20Dec.)
KIRLOSKAR OIL ENGINES LIMITED
KIRLOSKAR OIL ENGINES LIMITED
ENCON Awareness Creation Celebration ENCON WEEK Every Year (14 Dec. to 20Dec.)
KIRLOSKAR OIL ENGINES LIMITED
54
Corporate Sustainability Report
KOEL is the First Engine Manufacturing company in India, whoreleased Corporate Sustainability Report & received highest levelcheck certification of A+ after being validated by global reportinginitiative (GRI), Netherland
KIRLOSKAR OIL ENGINES LIMITED
Sustainability Reporting
Sr. no.
Year Frequency Guiding Principles
1 Sustainability Report 2009-10
Annually GRI G3
2 Sustainability Report 2010-11
Annually GRI G3
3 Sustainability Report 2011-12
Annually GRI G3.1
4 Sustainability Report 2012-14
Biannually GRI G3.1
5 Sustainability Report 2014-16
Biannually GRI G4
6 Sustainability Report 2016-17
Annually GRI G4
KIRLOSKAR OIL ENGINES LIMITED
56
GreenCo – “Gold” Certified Plant
KIRLOSKAR OIL ENGINES LIMITED
57
IGBC – “Gold” Certified Building
KIRLOSKAR OIL ENGINES LIMITED
58
CII - National Award for “Excellence in Energy Efficient Unit 10-11, 11-12 , 13-14,14-15,16-17 & “ Energy Efficient Units” 12-13 & 15-16
KOEL won for “Parivartan Corporate Sustainability Stewardship Award” for their efforts in Resource Conservation 2 times 10-11 & 13-14
Accolades Energy & Environment
Kagal Plant also bagged “First prize” for year 16-17 and “Certificate of Excellence” award for 15-16 in State Level Energy competition by MEDA in Engineering Sector
Consecutive 8 times winner at National level -CII
KIRLOSKAR OIL ENGINES LIMITED
59
Accolades Energy & Environment
Kirloskar Group Inter-competitionAwards by auspicious hands ofEminent Personalities in Energy Sector
Tree Plantation by auspicious hands ofEminent Personalities in EnvironmentSector