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Drill String Safety Valve Project Report Adam T. Bourgoyne, Jr., LSU L. Scott Stevens, U. Kentucky

Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

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Page 1: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Drill String Safety Valve Project Report

Adam T. Bourgoyne, Jr., LSUL. Scott Stevens, U. Kentucky

Page 2: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Presentation Outline

n Background– Terminology– Problem Areas

n Objectives n Approachn Summary n Recommendations

Page 3: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Swivel

Lower kelly cock

Kelly

Saver sub DSSV(Stabbing valve)

Upper kelly cock

Terminology

•Stabbing Valves often used to stop flow on drill-string during trips.

•Once flow is stopped, an inside BOP can be put in place prior to stripping pipe back to bottom.

•Dynamic kill of UGB works best with drill-string on bottom.

Page 4: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Traditional 2-Piece“TIW” Valve

Drillstring safety valvesare ball valves used to stop flow through thedrillstring.

Terminology

Page 5: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Upper seat

Stem

Stem link

Body

Ball

Seal

Lower seat

Seal

Terminology

One-Piece Design

Page 6: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Upper seat

Stem

Stem link

Body

Ball

Seal

Lower seat

Seal

TerminologyOne-Piece Canister Design

Page 7: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Canister Design Cut-Away

Page 8: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Problem Areas

Drillstring Valves & I-BOP 25%

ChokeManifold Valves29%

Connections & Other19%

Choke& Kill

Valves11%

Rams9%

Annular8%

After Hauser, 1995

High Failure Rate for Pressure Tests

Page 9: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Problems Seen in Practice

n Failure to Close n Failure to Openn Failure to Seal

– Bottom to top.– Top to bottom.– Inside to Outside.

•Mobil Oil Survey of operators identified 29 failures during well control.

•Problems have led to blowouts and loss of life.

Page 10: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only
Page 11: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Project Objectives

n Identify Common Modes of Failure.n Identify Alternative/Auxillary Devices.n Investigate Improved Design.n Construct Test Apparatus.n Evaluate Improved Design.n Develop Recommendations for

Improved Safety.

Page 12: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Upper seat

Stem

Stem link

Body

Ball

Seal

Lower seat

Seal

Valve Failures

Page 13: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Flow-Cut Ball & Seat

Caused by Human Error(Partially Closed Valve)

Page 14: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Wireline-Cut Ball

Page 15: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Over-Rotation of Ball

Page 16: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Upper seat

Stem

Stem link

Body

Ball

Seal

Lower seat

Seal

Valve Failures

Page 17: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Side View

InteriorView

ExteriorView

Valve Stem Failure

Valve StemStop

Eroded Hole

Eroded Hole

Page 18: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Valve Failures

Upper seat

Stem

Stem link

Body

Ball

Seal

Lower seat

Seal

Page 19: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

canister cage

Page 20: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Valve Seat Failure

Page 21: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Auxillary Equipment

n Pit Volume Totalizer Systemn Drill Collar Floatn Drop-In Check Valven Velocity Valve n Double Valve Assemblyn Low Torque Valvesn Choke Manifoldsn Shear Rams

Page 22: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Student Design Projects

n New DSSV Design with Improved Torque Characteristics at high pressures.

n New DSSV Storage Stand.

Page 23: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

LSU DSSV Design

Trunnion Mounted Ball

Spring Loaded Seats

Page 24: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

TestStand

Test Apparatus Design

Page 25: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Test Stand & Pump

Page 26: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Choke & Control Room

Page 27: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

0

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0

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Torque & Position vs TimePosition (% closed) Torque (ft-lbs)

Time

100gpm

120gpm

140gpm

160gpm

180gpm

100

0

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500

600

700

60

40

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0

80

Page 28: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Closing Torque

With 2,000 psi Shut-In Pressure

FlowRate

2-PieceDSSV

1-PieceDSSV

(gpm) 1s close 1s close 4s close

100 100 110 350

120 240 150 370140 280 250 385

160 370 390 ----

180 550 545 ----

Water Hammer ?

900 psi

Page 29: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Closing Torque, 2.75-in. ID

0

100

200

300

400

500

600

0 2000 4000 6000 8000 10000 12000

Equalized Pressure (psi)

2-piece, Floating Ball (LSU, water)ITAG1-piece, Floating Ball (LSU, water)Hi-KalibreLSU Design (water)M & M (Lite-Torc, LSU, water)M & M (GRI, mud)Hi-Kalibre (GRI, mud)ITAG (GRI, mud)

Page 30: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Effect of Valve cycling in 16 ppg mud

0

50

100

150

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300

0 100 200 300 400 500 600Number of Cycles (Close/Open)

Hi-Kalibre (GRI, mud, horzontal)

M & M (GRI, mud, vertical)

ITAG (GRI, mud, vertical)

After Tarr -SPE39320

0.5% Sand

Page 31: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Opening Torque (0% Equalized)

0

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600

0 1000 2000 3000 4000 5000

Pressure Differential across Valve (psi)

LSU Design (water)

M & M (Lite-Torc, LSU, water)

1-piece, floating ball (LSU, water)

ITAG (GRI, water)

ITAG (GRI, mud)

M & M (GRI, mud)

Page 32: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

General Observations

n Operating torque requirements for valve can vary greatly with valve use and weathering.

n Valve storage and maintenance is an important aspect of maintaining low torque valve operation.

Page 33: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only
Page 34: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Double Click Hereto start Movie

Page 35: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Conclusions

n DSSV Failures are Significant.n Common Modes of Failure Identified.n Problems poorly understood in field.n Improved design is possible.n Valve maintenance is important.

Page 36: Drill String Safety Valve Project Report · Drill String Safety Valve Project Report Adam T ... High Failure Rate for Pressure ... Drill string safety valves should not be the only

Recommendationsn 1. The DSSV intended for use as a stabbing valve to stop flow through the

drillstring during tripping operations should not be used in the drillstring for other operations. The stabbing valve should be maintained in a "like-new" condition and used only during periodic pressure testing with fresh water.

n 2. Operators and/or drilling contractors should check threads, valve wrench, and lift sub on the stabbing valve and actuate the stabbing valve close and open each tour.

n 3. Operators and/or drilling contractors should use a drillstring float whenever practical to provide redundant protection against a high-rate flow through the drill-string during tripping operations.

n 4. When floats are not used, shear rams are recommended for redundant protection against blowouts through the drillstring during tripping operations.

n 5. Drill String Safety Valves should not be the only means for stopping flow from the drillstring at the surface when reverse circulating the well during completion operations. Flow should be routed through hydraulically operated valves and a choke manifold.

n 6. Drill string safety valves should not be the only means for stopping flow through the drill string when significant piping and flow restrictions are present above the valve.