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Damaged Compressor Stator Parts Resulting from Operation in Deep Choke Jean-Claude Pradetto & Urs Baumann MAN Diesel & Turbo Schweiz AG

Damaged Compressor Stator Parts Resulting from Operation

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Page 1: Damaged Compressor Stator Parts Resulting from Operation

Damaged Compressor Stator Parts–

Resulting from Operationin Deep Choke

Jean-Claude Pradetto & Urs BaumannMAN Diesel & Turbo Schweiz AG

Page 2: Damaged Compressor Stator Parts Resulting from Operation

Urs Baumann is Manager of the R&D departmentof MAN Diesel & Turbo Schweiz AGin Zurich, Switzerland.Urs has a diploma (MechanicalEngineering, 1987) from the SwissFederal Institute of Technology inZurich.Urs Baumann is member of theTechnical Advisory Committees ofthe Turbomachinery SymposiumATPS in Singapore.

Jean‐Claude Pradettois the Head of the In ServiceDevelopment group of MAN Diesel& Turbo Schweiz AG in Zurich,Switzerland.Jean‐Claude is responsible fortrouble shooting issues as well asfor the continuous improvement ofthe turbocompressors.He has a diploma (MechanicalEngineering, 1988) from the SwissFederal Institute of Technology inZurich.

Page 3: Damaged Compressor Stator Parts Resulting from Operation

Damaged Compressor Stator Parts–

Resulting from Operation in Deep Choke

The internal stationary parts of a high‐speed, oil‐free, integrated motor compressor used in gas storage service were found severely damaged. The analysis of the operational trend data suggested prolonged operation in deep choke condition. Additional CFD calculations for these operating points confirmed that severe flow separations and flow reversals (at exactly the damaged stages) had to be expected. 

Concluding from the RCA the following measures were taken:• Recalibration of the anti‐choke control to move the response line to higher pressure ratios • Instruction to the operators to switch from serial mode to parallel mode operation if the 

compressor is operated beyond the response line of the anti‐choke controller.

After repair (no design changes) the machine is now in service for more than one year without any problems.

Page 4: Damaged Compressor Stator Parts Resulting from Operation

Description of the System    Tandem HOFIMTM – Operating Modes

Serial Operation Parallel Operation

The machine is able to operate in serial parallel  modes, according to the requirementsof the process

Page 5: Damaged Compressor Stator Parts Resulting from Operation

fullcavern

highestpr.ratio

serialoperation

Gas Storage Application              Operating Conditions

emptycavern

freeflowintocavern

emptycavern

verylow

pr.ratio

paralleloperation

backpressurethrottling

fullcavern

freeflowfromcaverninto

pipeline

emptycavern

verylow

pr.ratio

paralleloperation

backpressurethrottling

max. storage pressure

min. storage pressure

pipeline pressurepressure

storage recovery

The backpressurethrottle ensuresthat the minimumpressure ratio ofthe compressor isalways maintained.

Page 6: Damaged Compressor Stator Parts Resulting from Operation

RCA Vibration Data Analysis

attemptto restart

failed due toexcessivevibrations

the machinetripped on 

high vibrations

Page 7: Damaged Compressor Stator Parts Resulting from Operation

RCA Vibration Data Analysis

event #1(120 um)

event #3(>330 um)

HP-pos. X

HP-pos. Y

event #2(220 um)

~4.5 sec

Trip

Step‐increase of thesynchronous vibration

axial pos.

speed

S2M Datalogger

3 distinctpeak eventsbefore trip

Page 8: Damaged Compressor Stator Parts Resulting from Operation

RCA Vibration Data Analysis

the waterfall plotreveales a stepincrease of theunbalance (1x)

and

an excessive shaftdisplacement(impact or the like)

Page 9: Damaged Compressor Stator Parts Resulting from Operation

Investigation Visual Inspection on Site

impeller 5

impeller 4

impeller 3

broken locking screwpiece of 4th stage hub labyrinth

trapped piece of 4th stage hub

labyrinth

impeller 5(shroud)

impeller 4(hub)

5th stage shroud

laby

4th stagehub laby (missing)

Page 10: Damaged Compressor Stator Parts Resulting from Operation

Investigation Inspection at OEM’s Facility

damaged diffuser vanes found in 

stages 3, 4 & 5 onlydamaged hub labyrinthsfound in stages 3, 4 & 5 only

damages found in HP compressor only

4th stage hub laby(upper half) withswirl brakes

Page 11: Damaged Compressor Stator Parts Resulting from Operation

RCA Interpretation of Damaged Laby’s

This side must havebeen loaded, hammeringcontact

completely batteredsurface, material missing.

cracks on both sidesimpeller

5 (shroud)impeller 4 (hub)

5th stage shroud laby

4th stagehub laby(missing)

Normal loadingdirection andloaded surface

Conclusion:Reversing flow directioncausing alternating loadon both faces

Page 12: Damaged Compressor Stator Parts Resulting from Operation

RCA Evidence for Operation at Choke

flowseparationradial

flow

• clearly visible flow patterns in thediffusers of the stages 3, 4 & 5

• the comparison with CFD simulationsof typical operating conditions evidences repeated

or continuous operation at choke.

Calculated Flow Patterns Typical for Operation at:

Page 13: Damaged Compressor Stator Parts Resulting from Operation

RCA Repeated or Continuous Operation at Choke

In choke conditions the diffuser of the last stage(s) do not increase pressure. Therefore the hub labyrinth has a reversed flow. 

Dynamic flow and pressure fluctuations duringchoke operation caused the damages in the last stages of the HP compressor. 

Operating point in serial operationEffective choke line

series parallel

Page 14: Damaged Compressor Stator Parts Resulting from Operation

Conclusion                                                       .• According to the production profile

prolonged operation at very low pressureratios was a fact (pi HP < 1.05, or evenbelow 1.00).

• The choke controller should haveprevented the machine from running in this condition.

• The choke controller response line was not set properly. Therefore the machinewas running in deep choke.

• The two compression sections werealways running in serial mode. With theselow pressure ratios parallel mode wouldhave been appropriate.

max. storage pressure

min. storage pressure

pipeline pr.pressure storage recovery

pressure

ratio

PI

volume flow

actual (measured) operatingpoints with pressure ratios

below 1.05

Page 15: Damaged Compressor Stator Parts Resulting from Operation

Measures Correct Implementation of theChoke Controller Response Line

Operating point in serial operationChoke controller response lineEffective choke line

• Prevent machine fromoperating in deep choke.

• Implementation of a correctchoke controller response line.

• Encourage the operator to switchfrom serial to parallel operationif the choke response line is reached.

• In this case the efficiency will besignificantly higher than in serialoperation.

Page 16: Damaged Compressor Stator Parts Resulting from Operation

Thank You for your kind attention

Questions ?

Jean‐Claude PradettoHead of In‐Service DevelopmentMAN Diesel & Turbo Schweiz AG+41 (44) 278 3820jean‐[email protected] 

Urs BaumannHead of R & DMAN Diesel & Turbo Schweiz AG+41 (44) 278 [email protected]