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Conquering sulphuric acid plant limitations with Conquering sulphuric acid plant limitations with TOPGUN and caesium-promoted VK catalyst By Mr. Casper Vittrup Frandsen, Haldor Topsøe and Carlos Lama, Southern Peru Copper Presented at 8 th Mesa Redondo de plantas de ácido sulfúrico Presented at 8 th Mesa Redondo de plantas de ácido sulfúrico 17-20 October 2010, Puerto Varas Chile,

Conquering sulphuric acid plant limitations …mesaredondachile.com/pdf/papers/24-conquering-sulphuric...Southern Peru Copper (SPC)Southern Peru Copper (SPC) The Southern Peru Copppp

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Conquering sulphuric acid plant limitations withConquering sulphuric acid plant limitations withTOPGUN and caesium-promoted VK catalyst

By Mr. Casper Vittrup Frandsen, Haldor Topsøe and Carlos Lama, Southern Peru CopperPresented at 8th Mesa Redondo de plantas de ácido sulfúricoPresented at 8th Mesa Redondo de plantas de ácido sulfúrico17-20 October 2010, Puerto Varas Chile,

AgendaAgendaCase study at Southern Peru Copper (SPC)Case study at Southern Peru Copper (SPC)

Steps in the study at SPC Defining the challenge(s)– Defining the challenge(s)

– Defining the goal of the study

Performing the study investigations and design– Performing the study – investigations and design

– Tailor made solution

Result of the study at SPC after implementation of the solutionsolution

Southern Peru Copper (SPC)Southern Peru Copper (SPC)

The Southern Peru Copper (SPC) facility in Ilo operates two pp ( ) y psulphuric acid plants – both units are treating the off-gasses from the Peirce-Smith Converters and ISASMELT furnace

Southern Peru Copper (SPC)Southern Peru Copper (SPC)Capacity plant no. 2 is 3780 p y pMTPD

Commissioned in Feb. 2007

Catalyst loading 698 m3 –185 l catalyst/MTPD

T t t d i d fTopsoe was contacted in end of 2009 for making an optimizing study of the performance of the converter

Turn around scheduled in September 2010 includingSeptember 2010 including screening and partly catalyst replacement

Original design and operation parameter during start of the studyoperation parameter during start of the study

Dilution air

From gas cleaning -

275,000 Nm3/hrFeed gasDesign ≈ 13% SO2PV ≈ 8% to >13%

Dry towerFrom gas cleaning mixing chamber

SO2 emission

T inletDesign ≈ 390°CPV ≈ 410°CSO2 emission

Design = 300 ppm SO2PV > 1000 ppm SO2

Bed 1

Top layer of

C t l t

Bed 2-4FAT

T outletDesign ≈ 615-620°CPV > 630°C

Cs catalyst

IAT, HEXFAT PV > 630°C

Acid productionAcid productionDesign = 3780 MTPD

SO conversion rates TOPGUN 2010SO2 conversion rates – TOPGUN 2010

Production rate[%]

SO2 feed gas concentration

[mole%]

Conversion[%]

SO2 emission[ppm][ ]

65% 8.49% 99.63% 360

88% 11.54% 99.44% 780

100% 13.13% 99.37% 1020

112% 14.75% 99.24% 1435

Design: Maximum 300 ppm SO2 emission at 100% load

Consequences of the limitations for SPCConsequences of the limitations for SPC

High SO2 emissionsg 2

Risk of damaging the catalyst and converter due to high temperatures outlet bed 1Forced to lower the SO2 feed gas concentrationExcess dilution air through the plantExcess dilution air through the plantMore attention to operating the dilution airLess flexibility in operating the acid plantLess flexibility in operating the acid plant Bottleneck in the operation of the Cu-smelter

Extra cost for SPC

Goal of studyGoal of study

Dilution air

F l i

Feed gasDesign = 13% SO2

Dry towerFrom gas cleaningT inletDesign = 390°C

SO2 emissionSO2 emissionOriginal design = 300 ppm SO2New design = 250 ppm SO2

Bed 1

Top layer of

C t l t

Bed 2-4FAT T outlet

D i 615 620°C

Cs catalyst

IAT, HEXFAT Design ≈ 615-620°C

Acid productionAcid productionDesign = 3780 MTPD

How to get an accurate basis for the study?How to get an accurate basis for the study?

TroubleshootingTroubleshooting

& TOPGUN& TOPGUN

Troubleshooting TOPGUNTroubleshooting - TOPGUN TOpsøe’s Portable Gas analysis UNitp y

On-site technical service – executed during operation

Portable SO2 and O2 gas analyser – No requirement for 2 2 g y qcalibration gas

Topsøe’s catalyst simulation program of the plant and catalyst fperformance

Ideal tools for obtaining data for studies

Troubleshooting TOPGUNTroubleshooting - TOPGUN

Troubleshooting TOPGUNTroubleshooting - TOPGUNMeasurements at the inlet of bed 4Measurements at the inlet of bed 4

2No Sample point SO2 (%) O2 (%)

1 Inlet IAT 0.905 7.9

Feed gasf h t

1

342 Inlet inter reheat HEX 0.874 8.5

3 Outlet inter reheat HEX 0.931 7.8

Thesis

from preheat

4 Inlet bed 4 1.466 7.9

Thesis– Centre column in the

converter

– Pre-heater by-passnon blinding valves

Summary of studySummary of studyCatalyst performancey p– Low catalyst activity in all beds - TOPGUN– Catalyst samples confirm the low catalyst activity – The conversion in bed 1 turn-off at inlet temperature at 400°C

M h i l fMechanical performance– No leaks in the external heat exchangers– IAT and FAT tower operates satisfactoryIAT and FAT tower operates satisfactory– Feed gas by-passing into the inlet of bed 4

Solutions for SPCTailor made catalyst loading

Solutions for SPCy g

– Only the necessary amount of catalyst is replaced to achieve the goal

B d T I t ll d V l [ 3]Bed no. Type Installed Volume [m3]

Bed 1 VK59, 12 mm DaisyVK38, 12 mm Daisy

20102010

3060

Existing screened catalyst, non-Topsøe 2007 50

Bed 2 Existing catalyst, non-Topsøe 2007 158

Bed 3 VK48, 12 mm DaisyExisting screened catalyst, non-Topsøe

20102007

60117

Bed 4 VK69, 9 mm Daisy 2010 90

Check and rectify mechanical problem around bed 4

Existing screened catalyst, non-Topsøe 2007 133

Advantages of VK caesium catalystAdvantages of VK caesium catalystVK59 in bed 1 – replacement of the existing Cs-promoted catalyst in bed 1– Operating with higher SO2 strength

– Increase the flexibility of operating

– Cleaner and faster start-ups due to the low ignition temperature of VK59

VK69 in bed 4 – partial replacement of the existing standard catalyst– Significantly reduction of the SO2 emission at full load

Increased sulphuric acid production rate– Increased sulphuric acid production rate

– Cleaner and faster start-ups due to the low ignition temperature of VK69

– Possibility of eliminating the preheat exchanger to bed 4 during start-ups duePossibility of eliminating the preheat exchanger to bed 4 during start ups due to the very low ignition temperature of VK69

Performance predictionPerformance prediction

Before catalyst replacement

Performanceprediction

Gas to bed 1Flow rateSO2

275,000 Nm3/hr13 mole %

Acid production [100% H2SO4] 3768 MTPD 3786 MTPD

Bed 1 inlet/outlet temperatures 410°C/ >630°C 390°C/615 620°CBed 1 inlet/outlet temperatures 410°C/ >630°C 390°C/615-620°C

Overall conversion efficiency 99.35% 99.85%

SO2 exit bed 4 >1000 ppm 250 ppm

Performance after catalyst replacementPerformance after catalyst replacementPlant was started up in again in Sept/Oct 2010p g p

The results of the new performances is based on results received from SPC– More flexibility in operating the plant due to low inlet temperature of

bed 1 down to 390°C

– General improvement of the performance of bed 4 due to the lowGeneral improvement of the performance of bed 4 due to the low ignition and lower operating temperature

No rectifying of the by-pass to bed 4

Performance after catalyst replacementPerformance after catalyst replacementData from SPC at a daily production rate of 80%

350.00 14.00

Average 10.2% SO2 feed gas

250.00

300.00

SO2 10.00

12.00

m S

O2

feed gas

150.00

200.00

feed

gas

- %

6.00

8.00

him

enea

- pp

m

Average 112 ppm SO2

50.00

100.00SO2

2.00

4.00 SO2

CAverage 112 ppm SO2 in the stack

0.00 12 hours operation [14 Oct. 2010; 07AM - 07PM]

0.00

% SO2 - CHIMENEA SO2 feed gas %

SummarySummaryIdentify challenges and limitationsTroubleshooting Implementation of tailor made solution P f d i l d ti b t T d th l tPerformed in closed corporation between Topsøe and the plant

Results for SPC:Results for SPC: More flexibility in operating the acid plantEnable operation at optimal and design conditionsLower SO2 emissionAchieved the goal

Thank you for your attentionThank you for your attentionSpecial thanks to

Mr. Carlos Lama and Mr. Jurado Kleber from Southern Peru Copper

QuestionsQuestions