Christmas Eve refinery explosion cause by frozen, ruptured pipe

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    EXECUTIVE REPORT

    C O O P R E F I N E R Y C O M P L E X I N C I D E N T

    D E C E M B E R 2 4 , 2 0 1 3

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    TechnicalSafetyAuthorityofSaskatchewanEXECUT IVE REPORT

    CO OP REF INERY COMPLEX INC IDENT DECEMBER 24 , 2013

    INCIDENTSUMMARYOnDecember24,2013atapproximately3:25pmlocaltime,anexplosionoccurredinthePolymerization

    Unit27(PMU)attheCoopRefineryComplex(CRC)inRegina,Saskatchewan. Theensuingfirewas

    extinguishedatapproximately9:00pmlocaltimeonDecember24,2013. Theblastandfiredestroyedthe

    equipmentandstructurearoundreactors1,2and3inthePMU. TheremainingfivereactorsinthePMU

    sufferedblastandpostincidentfreezingdamage,andwererenderedunusable. Blastdamagealso

    occurredtoCRCbuildingsandequipmentoutsideofthePMU. Blasteffectswerealsofeltatlocations

    outsidetherefinerycomplex. Nopersonnelwereinjuredintheincidentorinthesubsequentemergency

    response. Figure1showsapartialviewoftheexplosionfromaCRCsurveillancecamera. InFigure1,the

    PMUisnotwithintheviewofthesurveillancecamera,butislocatedoutsidetheupperleftoftheimage.

    Figure1: Explosionat3:25PMDecember24,2013

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    REFINERYDESCRIPTION

    LocatedinRegina,Saskatchewan,theCoopRefineryComplex(CRC)isawhollyownedsubsidiaryof

    FederatedCooperavesLimited(FCL)whichownsandoperatestheCoopRefineryComplex(CRC)

    facilies.

    TheCRCwasincorporatedonApril1,1934,andonMay27,1935produconof500barrelsofcrudeoilper

    daybegan.TheCRCcelebratedits79thyearofoperaonin2014.

    CRCFactsandHighlights:

    Occupies575acresoflandinNorthRegina;

    Employsover800peopleonapermanentbasis;

    Employsandcontractsover1,000addionalpeopleduringpeakmaintenanceperiodsand

    turnarounds;

    A$2.7billionprojecttoexpandandrevamptheCoopRefineryComplexwascompletedin2013;

    TheexpandedCRCcurrentlyhasabalancedproductcapacityof130,000BPDandpotenalfor145,000BPD;

    Approximately36.5millionbarrelsofcrudewereprocessedin2013,a20percentincreaseover

    2012andthelargestvolumeprocessedinthehistoryoftheCRC.

    INVESTIGATIVEPROCESS

    TheinvesgaonbeganwithemergencyresponsebyReginaFireandProtecveServices(RFPS)ontheday

    ofDecember24,2013.RFPSsecuredthesceneandbeganinialassessmentsandevidencecolleconon

    December25,2013. TheTechnicalSafetyAuthorityofSaskatchewan(TSASK)iniateditsinialdata

    colleconandassessmentonDecember24,2013.OnJanuary7,2014TSASKandRFPSformedajointinvesgaonteamcomprisedofmembersfrombothorganizaons.

    PMUDESCRIPTION

    ThepurposeofthePMUistotakelightolefinsresulngfromtheFluidCatalycCrackingUnit(FCCU)

    processandpassthemoveraphosphoricacidcatalystinsidepolymerizaonreactorstoproduceahigher

    molecularweightproductcalledpolygasoline. ThePMUreactorsoperateatapproximately1060psig

    internalpressureat390F. ThePMUhadatotalofeightpolymerizaonreactorsandadisllaonsecon

    forpropane,butane,andgasolineseparaon. The"frontend"oftheunitincludesanaminetreatment

    seconandcauscandwaterwashestoremovecontaminantsfromthefeedstock. Figure2illustratesthe

    PMUpriortotheincident. Theunitisdesignedto:

    1. Collect"polyfeed",propane,butane,andolefinsforchargetothereactors;

    2. Treat"polyfeed"forhydrogensulfide,mercaptan,andnitrogencompoundremoval;

    3. Processolefinsoveracatalystbedtocreatepolygasoline;

    4.

    Distillandseparateoutpropane,butane,andpolygasolineproducts.

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    OPERATIONSIMMEDIATELYPRECEDINGTHEEXPLOSION

    Prior

    to

    the

    incident

    on

    December

    24,

    2013,

    the

    PMU

    was

    opera

    ng

    within

    normal

    parameters

    forfl

    ows,

    pressuresandtemperatures. Operatorsdidnotobserveanythingoutoftheordinaryduringprocess

    operaonsthatday. ThefirstindicaonofaprobleminthePMU,asreportedbywitnesses,wasawhistling

    noiseanumberofsecondspriortotheexplosion. Instrumentaonforpolyfeedflowtoreactors#1and#3

    inthePMUrecordedbaddataqualitysignals16secondspriortotheappearanceoftheexplosionona

    surveillancecamera. Thebaddataqualitysignalswerecausedbytheescapeofpolyfeedfromarupturein

    thepipinginthePMU.

    Figure2: PolymerizaonUnit27(PMU)Before

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    INCIDENTANALYSIS

    Preceding MaintenanceOutages

    IntheweeksbeforetheDecember24,2013incident,thereweretwoPMUmaintenanceoutages,as

    follows:

    Outage1: ThePMUwasshutdownbetweenNovember26,2013andDecember4,2013duetoa

    maintenanceoutageontheupstreamfluidcatalyccrackingunit(FCCU). Sincethisresultedin

    shutdownofthepolyfeedfromtheFCCUtothePMU,opportunitywastakentoperform

    maintenanceinthePMU. AnumberofmaintenanceitemsinthePMUwereidenfiedand

    completed.

    Outage2: ThePMUwasshutdownbetweenDecember12,2013andDecember18,2013dueto

    anothermaintenanceoutageontheupstreamFCCU. Thisoutageagainresultedinshutdownof

    feedfromtheFCCUtothePMU,althoughtherewasnomaintenanceperformedinthePMUduring

    thisoutage.

    Outage1: November 26, 2013 December 4, 2013

    InordertopreparetheFCCUforthemaintenanceacviesduringoutage1,awaterfloangprocedure

    wasusedtopurgehydrocarbonsfromtheFCCUpipingandvessels. Waterfloanghadhistoricallybeen

    usedforthepurposeofpurginghydrocarbons. Waterfloangisaprocessthatulizeswatertoflush

    hydrocarbonresiduefromthesystemandrenderthepipingandvesselsfreeofexplosivehydrocarbonsand

    safeforwork. Theintentwasforthewaterfloangproceduretointroducewateruptothewaterbooton

    thecombinedfeeddrum,whichislocatedupstreamofthePMUreactors. Itwasintendedthat

    instrumentaonandasightglassonthewaterbootofthecombinedfeeddrumwouldbeusedtodetect

    thewaterleveltoenabletheintroduconofwatertobeproperlystoppedatthatpoint. ThecombinedfeeddrumwaslocatedupstreamofthePMUreactors,andlimingthewateratthecombinedfeeddrum

    waterbootwouldprecludeanywaterfromreachingthePMUreactors.

    Duringoutage1,thewaterfloangprocedurewasiniatedduringthenightshi ofNovember26,2013,as

    planned,buttheprocessfailedtostopthewateratthecombinedfeeddrumwaterboot. The

    instrumentaonatthewaterbootwasdefecveandthesightglasswasdifficulttoread. Waterwas

    pumpedpastthecombinedfeeddrumandintothePMUpipingandreactors. Thepumpingofwaterinto

    thePMUpipingandreactorswasnotintended. Theshutdownguidelinesforbothoutagesspecifiedthat

    thepolymerizaonreactorsweretobepurgedwithnitrogengasastheyweretakenoffline. Figure3

    illustrates

    the

    planned

    and

    es

    mated

    actual

    extent

    of

    waterfl

    oa

    ng,

    as

    well

    as

    a

    schema

    c

    representa

    on

    ofapolyfeedbypassline.

    MaintenancepersonnelbegandrainingwaterfromthePMUonNovember27,2013,however,issueswith

    freezingwaterwereencounteredasthisprocesswasundertaken,especiallyastemperaturesdroppedat

    night. Waterdrainingandicethawingacviesconnuedthroughtheremainderofoutage1. Thawing

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    methodsincludedthewrappingofsteamtracelinesaroundprocesslines,aswellastheinseronofsteam

    lancesintopipinginsulaonjackets.

    Duringoutage1,outdoortemperaturesdroppedconsiderablytowardtheendoftheoutage,ascanbeseen

    inthemelineandtemperaturedatashowninFigure4.

    Figure3: WaterFloangExtent

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    Nov. 26, 2013

    Outage 1 begins.

    Maintenance work

    in FCCU and PMU

    is performed

    during this outage.

    Water floatingprocedure done on

    night of Nov. 26

    accidentally

    introduces water

    into the PMU

    including bypass

    line 123BPL.

    Dec. 5, 2013

    Operations resume.Numerous frozen

    lines in the PMU

    require thawing.

    Bypass line 123BPL

    was found frozen

    and was thought to

    have been thawed.

    Dec. 24, 2013

    Operations are

    within normal

    parameters with

    no indication of a

    problem.

    Rapidly rising

    temperatures

    cause the ice plug

    in bypass line

    123BPL to thaw

    and allow high

    pressure poly

    feed to escape

    from the rupture in

    the bypass line.

    The hydrocarbons

    ignite causing an

    explosion in the

    PMU.

    Dec. 19, 2013

    Operations resume and are within normal

    parameters during Dec. 19 23 with no

    indication of a problem.

    At some point, ice formation in bypass line

    123BPL causes the bypass line to rupture.

    An ice plug remains inside bypass line

    123BPL, preventing the escape of poly

    feedDec. 12, 2013

    Outage 2 begins.

    Maintenance done

    to pressure relief

    valve in FCCUresulting in feed

    outage to the PMU.

    Water floating not

    done in this outage.

    Dec. 23, 2013

    The coldesttemperatures

    during the period

    Nov. 26 Dec. 24

    are reached

    during the early

    morning hours of

    Dec. 23.

    Figure4: TimelineofEvents NovembertoDecember,2013

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    Unit OperationDecember 5, 2013 December 11, 2013

    AstheFCCUandPMUweregraduallybroughtbacktooperaonaeroutage1,manyfrozenprocesslines

    connuedtobefoundandrequiredthawinginordertomakeprogress. ThePMUreactorinletsandoutlets

    werefoundfrozen. Thereactorfeedbypassline123BPLwasalsofoundfrozen. Gradually,processlines

    werethawedandunitoperaonwasachievedbyDecember6,2013.

    Reactorfeedbypassline123BPL,locatedadjacenttoPMUreactor2,isapartofthePMUandservesto

    divertfeedstockflowaroundPMUreactors1,2and3whenflowthroughthereactorsisnotneeded. Flow

    throughreactorfeedbypassline123BPLwasnotnecessaryduringthestartupandoperaonofthePMU,

    andthislineisnormallyclosedduringPMUoperaon. Bypassline123BPL,showninFigure5,formsa

    naturaldeadlegwhentheblockvalveslocatedattheboomofthelineareclosed. Deadlegsare

    componentsofapipingsystemthatnormallyhavenosignificantflow. Deadlegscanaccumulatewaterand

    freezemorereadilythanpipingthatisopentoflow. Deadlegsfrequentlyrequiregreateraenonwhen

    thawinganddraininginordertoachievecompleteclearing. Operatorswereunderthebeliefthattheyhad

    thawedanddrainedbypassline123BPLduringtheireffortstoachieveunitoperaon. Thethawingand

    drainingofthefrozenlineswasnotsystemacanddocumented,butreliedonoperatorexperseand

    memory. Theinvesgaondeterminedthatbypassline123BPL,infact,wasnotproperlydrainedofwater.

    DuringtheperiodofoperaonfromDecember5,2013toDecember11,2013temperatureswerecold

    throughoutascanbeseeninthemelineandtemperaturedatashowninFigure4.

    Outage2:December12 December18,2013

    Thepurposeofoutage2wastorepairafailedpressurereliefvalveintheFCCU,againresulnginshutdown

    ofthePMUduetoaninterruponoffeedfromtheFCCU. Duringthisoutage,procedureswererevisedin

    ordertomigatethefreezingissuesexperiencedduringoutage1,andwaterfloangdidnotimpactthe

    PMUreactorsandpiping. Addionally,nomaintenanceacvieswereperformedinthePMU. Theshutdownandsubsequentstartupaeroutage2wentrelavelysmoothly,withnoaddionalfreezing

    issues.

    Theinvesgaondeterminedthatthebypassline123BPLlikelyremainedfilledwithwaterthroughoutage

    2.

    Duringoutage2,temperatureswarmedupconsiderably,peakingat0ConDecember16,2013,andthen

    droppeddramacallytoastaclowof24Cwithawindchilllowof34Cattheendofoutage2on

    December18,2013,asshowninFigure1.

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    Figure5: RupturedBypassLine123BPL

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    UnitOperaonDecember19,2013December24,2013

    TherewerenofreezingissuesthataffectedunitstartupandoperaonduringDecember19to24,2013.

    ThePMUfunconedwithinnormalparametersforpressures,temperaturesandflowsduringthisperiod.

    Operatorswerenotawareofanyprocessproblemsthatcouldleadtoacomponentfailureduringthis

    period.

    OutdoortemperatureswereverycoldfromDecember19,2013toDecember21,2013. Beginningon

    December22andconnuingintoDecember23outdoortemperaturesdroppeddramacallytoastaclow

    of35Cat2:00AMonDecember23andawindchilllowof47Cat6:00AMonDecember23. These

    were,infact,thecoldesttemperaturessincethewaterfloangprocedureofNovember26,2013.

    Thebypassline123BPLdeadlegcontainedwaterthroughoutthecoldweatherthatoccurredbetween

    November26,2013andDecember24,2013. Waterinthelinefrozeandrupturedthelinedueto

    hydrostacoverstressatsomepointduringthisperiod. Aniceplugexistedwithinthelineandcreateda

    sealwhichpreventedtheescapeofhighlyvolalepolyfeedthroughthepiperupture.

    Beginningat6:00AMonDecember23,2013thetemperaturebegantorisedramacally,peakingat2Cat

    2:00PMonDecember24,2013.

    OnDecember24,2013unitoperaonswerewithinnormalparameters. DuetotheChristmasholiday,a

    numberofoperaonsstaff hadle earlythatday,resulnginmuchfewerthannormalpersonnelaround

    thePMUasthedayprogressed.

    Asoutdoortemperatureswarmed,combinedwithheatfromunitoperaons,theicepluginbypassline

    123BPLthawedandeventuallygavewaytothehighpressurepolyfeed. At3:25PMthiscausedasudden

    releaseofhydrocarbonsintothePMU,followedbyalargeexplosionandensuingfire. Theexplosionand

    firewerecentredonPMUreactors2and3,resulnginextensivedamagetothePMUstructurearound

    reactors1,2,3. TheexplosioncausedblastdamagetootherareasofthePMUaswellastosurrounding

    buildingsinotherunits. TheblastwasfeltinareasofReginawelloutsidetherefinerycomplex.

    Figure5showstherupturedbypassline123BPLaertheincident. Figure6showstheextentofdamageto

    thePMU.

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    Figure6: DamagetothePMU

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    FINDINGSANDRECOMMENDATIONS

    1. Proceduresforcoldweathershutdownshouldberevisedtoimprovedecisionmakingandthe

    idenficaonofcondionswhencoldweathershutdownispermissibleandcondionswhenitis

    not.

    Proceduresforcoldweathershutdownwereinadequate,astheydidnotconsiderthehighrisksposedbyextremecold.

    2. Proceduresforincidentinvesgaonshouldberevisedtoensurethatcorrecveaconsare

    implementedsothatincidentsdonotrepeat.

    AsimilarpiperuptureduetofreezingoccurredinDecember,2008,wheretheresulngvapour

    clouddidnotignite. Effecvecorrecveaconswerenotimplemented.

    3. CRCshouldestablishawrienfreezeproteconprogramthatincludestheidenficaon,

    migaon,managementofchangeandauditrequirementsforequipmentatriskduetofreezing.

    4. Proceduresforwaterfloangshouldberevisedtoensurethatinstrumentaonandprocess

    controlsareeffecveandmaintained. Addionalredundancyininstrumentaon,controlsand

    verificaonmethodsshouldbedeveloped.

    Theprimaryelectronicinstrumentforwaterlevelmeasurementatthecombinedfeeddrum

    waterbootwasaFisher2500pneumacleveltransmier. Thisinstrumentwasfoundtobe

    defecvewhentestedduringtheinvesgaon. Historicaldatafromtheinstrumentwas

    reviewedandconfirmedthattheinstrumentwasdefecveonNovember26,2013.

    Asightglassservedasasecondaryinstrumentforthewaterlevelmeasurementinthe

    combinedfeeddrumwaterboot. Thissightglasswasoperaonal,butwasdifficulttoread

    becausetheappearanceofwaterandpolyfeedarenearlyidencal.

    5. Thawingproceduresshouldberevisedtoensureallareasareaddressedsystemacally,especially

    deadlegs.

    Thawingprocedureswereinadequateinthattheydidnotsystemacallythawallvulnerable

    locaons. Thawingrelieduponoperatorknowledgeandmemoryofvulnerablelocaonsas

    opposedtoadocumentedandsystemacapproach.

    6.

    CRC

    should

    adopt

    the

    deadleg

    defi

    ni

    on

    set

    out

    in

    the

    American

    Petroleum

    Ins

    tute

    standard

    570

    andensurethisdefinionisunderstoodacrosstheorganizaon.

    Inthecourseoftheinvesgaondifferinginterpretaonsofwhatconstutesadeadlegwere

    apparentatCRC.

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    7. Deadlegsinpipingshouldbesystemacallyidenfied,documentedandeliminatedorotherwise

    migatedwhereverpossible. Deadlegsthatmustremainshouldbehighlightedandgivenspecial

    aenonthroughoutoperaonsandmaintenanceacvies.

    Thedeadlegonbypassline123BPLallowedwatertobecometrapped. Thiswatersubsequently

    frozeandrupturedtheline,causingthehydrocarbonleakandexplosionofDecember24,2013.

    8. Maintenanceproceduresshouldberevisedtoensurethatcricalsensingandmonitoring

    equipmentremainsfunconal.

    TheFischer2500pneumacleveltransmieratthecombinedfeeddrumwaterbootwas

    foundtobedefecve.

    9. CRCshouldsystemacallyidenfywhereinstalledpipingdiffersfromthedesignspecificaons. The

    differencesshouldbeanalyzedandsuitablyaddressedasnecessary.CRCshouldinvesgate

    whethercorrosionsurveydatacouldbeusedtoidenfywherepipingdoesnotconformtodesign

    specificaons.

    Althoughnotacauseofthisincident,inthecourseoftheinvesgaonbypassline123BPLwas

    foundtobe2Schedule80,whiledesigndocumentsspecifiedthislinetobe2Schedule160.

    2Schedule80hasawallthicknesswhennewof0.218,whereas2Schedule160hasawall

    thicknesswhennewof0.344.

    Thicknessmonitoringlocaons(TML)onbypassline123BPLwerelocatedatthetopelbowand

    theboomelbow,bothlocaonsbeingwellawayfromtherupturedarea. CRCthickness

    monitoringdataofOctober29,2013showsawallthicknessof0.220atthetopelbowanda

    wallthicknessof0.200attheboomelbow.

    10.CRCshouldreviseitscorrosionsurveyprocedurestoassesscorrosionunderinsulaon(CUI)on

    jacketedandinsulatedcomponents. Thecorrosionsurveyproceduresshouldulizemethodsto

    idenfyandassessareaswherecorrosionisthegreatest.

    Althoughnotacauseofthisincident,significantexteriorcorrosionwasfoundonbypassline

    123BPL. Bypassline123BPLwasjacketedandinsulated.

    Datafromthicknessmonitoringlocaons(TML)onbypassline123BPLdidnotdetectthe

    exteriorcorrosionthatwasfound. TheTMLswerenotlocatedattheareawheretheCUIwas

    found.

    CUIonbypassline123BPLresultedinawallthicknesslossofupto27%.

    Theplacementofsteamlancesinsideinsulaonjacketsforthepurposeofthawingfrozenlines

    isacommonpracceatCRC,andthismayplayaroleinCUI.

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    GLOSSARYOFTERMSANDABBREVIATIONS

    BPDbarrelsperday

    BypassLine123BPLThe2polyfeedbypasslinelocatednearthenorthsideofpolymerizaonreactor#2. Thisbypasslinedivertspolyfeedflowaroundpolymerizaonreactors#1,2and3.Thisbypassline

    isdesignatedonCRCdrawingsas27P1070FA5A2IH.

    CRC CoopRefineryComplex

    CUICorrosionUnderInsulaon

    DeadlegsComponentsofapipingsystemthatnormallyhavenosignificantflow.Someexamples

    includeblankedbranches,lineswithnormallyclosedblockvalves,lineswithoneendblanked,

    pressurizeddummysupportlegs,stagnantcontrolvalvebypasspiping,sparepumppiping,levelbridles,

    reliefvalveinletandoutletheaderpiping,pumptrimbypasslines,highpointvents,samplepoints,

    drains,bleeders,andinstrumentconnecons.

    FCCUFluidCatalycCrackingUnit

    PMUPolymerizaonUnit27

    PSIGPoundspersquareinch,gage. Ameasureofpressure.

    RFPSReginaFireandProtecveServices

    TMLThicknessMonitoringLocaon

    TSASKTechnicalSafetyAuthorityofSaskatchewan