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    Efficiency Improvement at IFFCO Paradeep

    S.K. Gandhi, Executive Director

    and

    Navin Nath, Chief Manager (Process)

    Indian farmers Fertiliser Cooperative Limited,

    Paradeep Unit

    Distt. Jagatsinghpur,

    Paradeep, Orissa

    Abstract

    In view of high cost of energy it is imperative to conserve

    energy to reduce the cost of production. Level of energy

    consumpt ion of an operating plant can also provide the insight

    of its physical and financial health. Article gives an insight on

    how IFFCO Paradeep Unit is continuously improving its

    performance in the areas of energy efficiency and

    environmental improvement. The measures implemented

    involves modification in the existing process and equipments,

    changes in the equipment layout, recycling of material and

    water, reduct ion of wastage and use of renewable energy. The

    details of these measures and resultant savings in energy andwater consumption and improvement in environment etc are

    elaborated.

    1.0 Introduction

    IFFCO Paradeep Unit operates two streams of Sulphuric acid plant (2 x 3500

    MTPD), one stream of Phosphoric acid (2650 MTPD as 100% P2O5) and three

    streams of complex fertilizer plant (3x2090 MTPD). The main raw materials

    such as Rock Phosphate, Sulphur, Sulphuric Acid and Ammonia are imported

    from various countries. The electric power requirement is met through Captive

    Power Plant (CPP) having two nos. turbo generator (TG) sets, each having

    capacity of 55 MW. In addition to the waste heat boilers in Sulphuric Acid

    Plant, there are two coal fired 110 TPH capacity Atmospheric Fluidized Bed

    Combustion boilers generating steam at a pressure of 61 kg/cm2(g) used for

    power generation and other utility requirements.

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    The raw materials are transported from Jetty to the plant through 5 kms long

    belt conveyors/pipelines. Water required for the plant is supplied from

    Taladanda Canal 2 km away from the plant site. Unique Features of Paradeep

    Unit :

    1) Largest Phosphatic fertilizer complex in India.

    2) Worlds largest single stream phosphoric acid plant: 2650 MTPD.

    3) Largest Sulphuric acid plants in India: 2 x 3500 MTPD.

    4) Captive power generation, hence self reliant.

    5) Own jetty for unloading imported raw materials without delays.

    2.0 Effic iency Measures Implemented since 2005

    Though the Paradeep plant was commissioned in the year 2000 but it wasunder closure by Pollution Control Board when IFFCO took over in 2005.

    There were various design and operational drawbacks in the plant. IFFCO

    took various systematic measures to improve its operation and energy

    efficiency. With the continuous improvement, Electrical as well as thermal

    energy has been brought down to the level of just half of its previous levels.

    Water consumption of complex has been reduced from 35000 m3/day to

    25000 m3/day. Some of the improvements made in the plant are described.

    3.0 Efficiency Improvement in Sulphuric Acid Plant

    3.1. Installation of Heat Recovery System (HRS)

    Lot of heat is generated in the Sulphuric Acid Plant in acid dilution and

    absorption. But a large amount of this heat is discarded in the cooling tower.

    However in the Heat Recovery System, the low level heat discarded to the

    cooling tower is used to generate the LP (4.0 kg/cm2g) steam.

    HRS operates at the upstream of existing Intermediate Absorption Tower

    (IAT). The HRS consists of a steam injection chamber, a packed heat recovery

    tower, a horizontal steam boiler, heater, preheater, diluter, an acid circulating

    pump, and two acid drain pumps. The schematic of sulphuric acid plant with

    heat recovery system is shown in Figure 1.

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    Figure 1: Schematic diagram of Sulphuric acid plant with heat recovery system

    The additional steam of about 65 MTPH produced by the heat recovery system

    has reduced the steam required from the coal fired boilers. Since the heat

    recovery system was installed, coal consumption has decreased by 35%. In

    addition to this it has reduced the heat load on cooling tower by 45 Gcal/hr.

    Which in turn have stopped the operation of 1 cooling water pumps, two cooling

    tower fans and have reduced the evaporation loss from cooling tower. Total

    savings attributable to the heat recovery system project are estimated at Rs 25

    croreper year.

    Figure 2 and 3 shows block diagram illustration of steam balance of the

    complex before and after HRS respectively.

    Furn

    ace

    I

    II

    SH 2

    SH 1

    IV

    III

    HRS

    HeaterHRS Tower

    Demister

    FAT

    Circulation

    DT Circulation

    Tank

    BoilerConverter 1 Converter 2

    Venturi

    Scrubber

    Hot HE450

    oC

    341.oC

    248.

    o

    C

    Cold HE

    Steam DrumHP Steam to export

    Stack

    Strong acid from IAT tank required

    during highhumidity only

    IAT Circulation

    Tank

    240oC

    DTFAT IAT

    Sulphur

    CW

    CWCW CW

    Air

    Blow DownIP Steam

    Economizer

    HRS

    Pre

    Heate

    r

    Boiler feed water

    To deaerator

    Treated water

    from existing

    system

    0.7 barg steam

    HRS

    Diluter

    HRS Boiler

    Steam

    Strong

    Acid to

    common

    acid tank

    N

    New HRS

    Product

    acid

    Blower

    Process water

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    Figure 2 Steam & Power balance PRE HRS-1

    Figure 3 Steam & Power balance Post HRS-1

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    3.2. Reduction of Catalyst preheating time during Cold Start-up of Sulphuric

    Acid Plant & simultaneous reduction of diesel consumpt ion.

    This schemes was designed in-house to preheat the catalyst by utilizing HP

    steam from coal fired boilers in the waste heat boiler of Sulphuric Acid Plant

    and also providing an interconnection between 1stbed outlet duct to 4th bed

    inlet duct in order to achieve 4thbed temperature early, during the cold start-

    up. After implementation of the above scheme, diesel consumption has been

    reduced from 100 KL to 60 KL thus saving 40 KL per startup per stream and

    Cold start-up time has been reduced from 36 hrs to 24 hrs thus saving 12 hrs

    of production. Total investment was just Rs. 1.0 lakh. The schematic of

    scheme is shown in Figure 4.

    Figure 4 Schematic diagram Modification of Start up in Sulphuric acid Plant

    3.3. Alkali Scrubber to arrest SOX emission during start-up

    Sulphuric acid plant is equipped with an Alkali Scrubber unit for scrubbing

    1,20,000 NM3/hr of gas. The scrubbing system controls SO3concentration in

    the stack during the plant start-up. Sodium hydroxide solution (15%) is used

    as scrubbing media. After absorption of SO3, sodium hydroxide solution gets

    converted into sodium sulphite and sodium bisulphate. The tail gas from final

    absorption tower enters at the bottom of the scrubber and rises to the top

    through polypropylene packing beds.

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    The moisture of the gas is removed by 20 Nos. of PPE fiber beds mist

    eliminators installed before the packing. The gas leaving the scrubber is

    vented in to atmosphere through the stack. The pH of the circulation solution is

    maintained at 6.8. A bleed off is taken from the circulating liquor to the final

    effluent tank where the aeration takes place. The solution is aerated for 120

    hours by a surface aerator to convert sodium sulphite and sodium bisulphate

    to sodium sulphate.

    3.4. Caesium promoted catalyst

    Caesium promoted catalyst has been added to the 4th bed (248 m3) of theconverter bed in Sulphuric Acid Plant. Out of the 248 m3 catalyst 50% is the

    caesium promoted catalyst. The conversion temperature with caesium

    promoted catalyst is as low as 340C where for normal catalyst its about 400-

    420 C. Because of low reaction temperature conversion of SO2 to SO3

    during cold start up is attained relatively faster, reduces the plant start-up

    duration and also reduces the emission of SO2 during start up.

    3.5. Utilization of vent steam from condensate receiver and CBD tank

    In sulphuric acid plant, the flash steam from condensate tank and boiler

    continuous blow down tank (CBD) were vented to atmosphere. To recover the

    loss of energy the flash steam was diverted to the nearby deareator tank with

    an investment on Rs 2.6 Lakh. The recovery of steam resulted in subsequent

    reduction of 7 ton of LP steam input to deareator. The block diagram of the

    scheme is shown in Figure 5.

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    Figure 5: Schematic showing Utilisation of Vent Steam

    3.6. Reduct ion in Boiler feed water pump discharge pressure from 105kg/cm2g to 90 kg/cm2g in Sulphuric Acid pant

    Though the boiler feed water header pressure requirement was about 90

    kg/cm2g, discharge of Boiler Feed Water Pumps was maintained at 105

    kg/cm2g to with a view that it provides operation flexibility. The detailed review

    of the boiler feed water system established that there is no need of keeping

    such a high discharge pressure. Reduction in the discharge pressure has

    resulted in the stoppage of one pump which was made stand-by, thereby

    resulting in power savings of 900 kW.

    3.7. Candle Filter to arrest acid mist in sulphuric acid plant

    In Sulphuric acid plant at the top of Inter pass Absorption Tower and Final

    Absorption Tower, trickling candle filters have been installed. The candle filter

    helps in arresting acid mist or droplets present in the outlet gases. The gas

    leaving the final absorption tower has an acid mist concentration of 40 mg/Nm3

    of SO3as against the norm of 50 mg/NM3, which is discharged through to tail

    gas stack of 131 meters height.

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    4.0 Efficiency Improvement in Phosphoric Acid Plant

    4.1. Modification of evaporators barometric condenser by installation of

    single sieve type distribut ion t ray and removal of steam ejector system.

    In evaporators, phosphoric acid is concentrated from 28% to 54 % P2O5.There

    are seven evaporators. Each evaporator is single stage, forced circulation unit

    consisting of rubber lined flash chamber, axial flow circulation pump and

    vertical shell and tube Heat Exchanger with impervious graphite tubes. Acid is

    re circulated at a high rate by the pump through the heat exchanger and into

    the flash chamber where an absolute pressure of about 66 mmHg is

    maintained to keep the acid at its boiling point. The vapours from the flashchamber flow under vacuum to the entrainment separator. From the separator

    phosphoric acid is returned to flash chamber and the vapour flow continues to

    fluorine scrubber. Vapours from the fluorine scrubber will come under direct

    contact with cooling water in the barometric condenser and the remaining non

    condensable gases are extracted.

    Figure 6: Barometric Condenser Before and After Modification

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    Earlier System:

    In the earlier system the vapors from the fluorine scrubber are condensed in

    baffle type barometric condenser where a large amount of cooling water

    condenses the partial amount of water vapor. Remaining water vapor and any

    non condensable gases are extracted by a two stage Vacuum jet steam

    ejector system consisting of two nos. of medium pressure (MP) steam (15

    kg/cm2g) ejectors and a water cooled inter condenser. MP Steam

    consumption in each ejector system was 2 MTPH. Total MP Steam

    consumption in all the seven evaporators was 14 MTPH.

    Modified system:

    In the modified system, baffle trays of barometric condenser were replaced

    with a single sieve tray where cooling water passes through the sieve at the

    top and condenses condensable vapours and extracts all the non condensable

    gases without vacuum jet ejection system. The modification was carried in-

    house with an investment of Rs 84.894 lakh, with savings of 14 TPH of MP

    steam equivalent to annual savings of about Rs. 5 crore.

    Figure 6 shows the schematic before and after modification.

    4.2. Installation of pre scrubber for improving Fluorine scrubbing efficiency

    Earlier reactor fumes were scrubbed in a single stage scrubbing system with

    pond water. This system was not adequate and was not meeting the norms

    fixed by the Pollution Board. After conducting in-house study a pre-scrubber is

    installed at the up-stream of the existing scrubber (Figure 7). Additional pre-

    scrubber vessel along with an additional scrubber exhaust fan and new stack

    with higher diameter was installed. This has improved the scrubbing efficiency,

    reduced the fluorine emission to the atmosphere from 20-25 mg/NM3 to 4-5

    mg/NM3.

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    Figure 7 Fluorine Scrubbing Unit

    4.3. Retrofit of Fluorine recovery uni t

    Earlier Hydro Fluorosilisic acid recovery system was bypassed. Hydro

    fluorosilicic acid produced in evaporator section was not recovered in the

    Fluorine Scrubber instead it was getting recovered in the barometric

    condenser which in turn lead to rise in the fluoride content in cooling tower and

    release of free fluorine in to the atmosphere. Fluorine recovery system was put

    into operation by major revamping viz brick lining of the scrubber, installing

    reliable pumps, circulation MSRL lines replaced with Poly-propylene lines etc.

    Presently about 20 MT / day hydro flurosilisic acid (18% - 20% H2SiF6) is

    recovered which in turn reduces emission of Fluorine to the atmosphere. The

    schematic in Figure 8 shows the modification.

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    Figure 8: Fluorine Recovery Unit

    4.4. Provision of a Single cloth wash tank in Phosphoric Acid Plant.

    There are seven (7) nos. of belt filters in Phosphoric Acid Plant. Each belt filter

    was having its individual cloth wash tank and cloth wash pump. All these 7 cloth

    wash tanks and pumps were replaced with common cloth wash tank and pump.

    This has reduced the power consumption by 27.5 kW and has also improved

    the accessibility & approach to the equipments and house-keeping of the entirearea.

    Figure 9: Schematic Diagram of Modification in Wash Tank

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    5.0 Effic iency Improvement in Complex Ferti liser Plant

    5.1. Steam Air heater in DAP:

    To evaporate the moisture of fertilizer, hot gases are supplied into the dryerthrough a duct which is lined with refractory. The hot air was generated byfiring

    fuel oil through a burner and a combustion chamber with supply of inlet air.

    System was retrofitted with steam heated air system for utilizing the captive

    steam of the plant by connecting the hot air duct of this new steam air heater to

    the existing discharge duct of combustion chamber as shown in Figure 10.

    Total expenditure for all the three trains was Rs. 6.78 crore and with the annualFO saving of 12150KL total monetary savings are about Rs. 51.22 crore.

    Figure 10: Steam Air Heater

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    5.2. Individual scrubbing system for Dust and Fumes in DAP/NP Plant

    There was a common dust and Fume Scrubbing System for scrubbing dust

    generated from conveyor, elevators, crushers & screens and Fumes from Pre-

    neutralizer and Granulator. Dust being heavier and system not designed for

    the combined scrubbing of fumes and dust, it was not able to suck the dust

    properly. To overcome the problem separate dust scrubbing system was

    installed from the scrap equipment and material (Figure 11). This modification

    improved dust scrubbing efficiency reduced the dust escape to the

    atmosphere and reduced the ammonia loss to atmosphere from 350 mg/NM3

    to 150 mg/NM3.

    Figure 11: Dust and Fumes Scrubbing Unit in DAP Plant

    6.0 Effic iency Measures in Utilit ies and Offsi te

    6.1. Energy savings due to installation of new BFW line from AFBC boiler to

    Energy Center

    Earlier a dedicated pump of 300 kW motor was supplying Boiler feed water to

    PRDS in Energy center. A new line from the discharge of BFW pump of coal

    fired boiler was provided to supply the required de-superheating water to thisPRDS. This has stopped the operation of 300 kW motor thus saved 300 kW

    power.

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    6.2. Installation of lower capacity Pump at Canal pump house

    The Canal pump house, which is the source of water supply to Paradeep Unit is

    at distance of about two kilometres. From the underground tank of canal pump

    house water is pumped to the plant through centrifugal pump of 3000 m3/hr

    capacity drive by 450 kW motor. On studying the water supply system, it was

    observed that the process requirement could be met with a pump of lower

    capacity of 1500 m3/hr only. Pump was replaced with lower capacity pump

    driven by motor of 160 kW thus saving 290 kW power.

    6.3. Replacement of Cool ing Tower fan blades from sol id FRP to Hollow FRP

    Fan blades of cooling tower in Sulphuric Acid Plant and Energy Centre were

    replaced from Solid FRP to Hollow FRP. Seven numbers of Fan blades were

    replaced in Sulphuric Acid Plant and 10 nos. of fan blades were replaced in

    Energy Centre Cooling Tower. Total reduction in power consumption was 300

    kW.

    6.4. Energy savings in Coal Handling Plant (CHP)

    There were 11 nos. of conveying belts were operated in the earlier layout.

    However with careful study the conveyor belts have been reduced to 7. This

    resulted in a power saving of about 200 kW.

    6.5. Trimming of Filter water pump impeller

    The filter water pumps are used to pump process water to different plants inside

    the complex. Each of the three pumps was designed to give a flow of 1800

    m3/hr at a discharge pressure of 6.90 kg/cm2. After an in-house study as per the

    requirement of the plant it was observed that the impeller of one pump can be

    trimmed for lower flow without any change in the discharge pressure. The

    impeller dia. of the pump was trimmed form 540 mm to 520 mm. This resulted in

    the power saving of 75 kW.

    6.6. Installation of De dusting unit for Product Handling Conveyors

    De-dusting units are installed at various locations in the product handling

    system to extract the dust and keep the environment dust free Figure 11). The

    system was designed in-house using scrap equipment & material.

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    Fig-11: De-dusting system for Product Conveyer and Bagging Plant

    6.7. Energy savings due to reduct ion in discharge head of Ammonia transfer

    pump

    A scheme was implemented to reduce the discharge head thus reducing the

    power consumption of Ammonia transfer pump by reducing the impeller from

    four stage to three stage. After implementation of the scheme, power

    consumption has been reduced from 71 kW to 59 kW, thereby saving 12kW of

    power consumption.

    6.8. Installation of Capacitor banks to increase Power factor

    Power factor at Paradeep unit was just 0.71. Capacitor Banks were installed

    and power factor improved to 0.90.

    6.9. Installation of Steam traps and Condensate recovery system

    A total of 387 nos. steam traps were installed in all the plants of the entire

    complex. This scheme has resulted in steam savings of about 5%.

    6.10. Installation of screw type un-loader

    Earlier, there were two Grab type un-loaders each of 1500 TPH capacity at

    Jetty for unloading Rock Phosphate & Sulphur from Ship. Unloading the

    materials through grab un-loaders, lot of dust was generated.

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    Now an additional Screw Type Enclosed Un-loader of 1800 TPH capacity has

    been installed to avoid the dust generation and any spillage (Figure 12). This

    system was commissioned in July 2013.

    Figure 12 Screw Un-loader

    6.11. Renewable Energy Measures

    As a part of green initiative; lighting of Administrative Building is done by

    installing the solar panels of 30 kW (3x10 kW) with an investment of Rs.70 lakh

    6.12. Measures for Water Conservation

    6.12.1. Water conservation measures in Phosphor ic Acid Plant

    a) Reduct ion in Fresh Water Consumption

    Previously, around 200 m3/h of fresh water was used in the lubricating oil

    coolers of the gypsum pump and ball mills. These coolers are now connected

    to the sulphuric acid plant closed loop cooling water circuit, thereby reducing

    fresh water consumption.

    b) Utilization of Waste Water from utili ty/offsite

    The waste water generated during back wash of resin in DM plant, tower blow

    down of sulphuric acid and power plant cooling towers of about 350 m3/hr are

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    being used in 7 nos. of belt filter condensers, vacuum ring pumps and for rock

    phosphate wet grinding. Thus saving about 9000 m3/day of fresh water.

    c) Use of pond water as pump seal water

    All the centrifugal pumps in phosphoric acid plant, except the pumps in ball

    mill section are designed to handle acidic solution; this made us possible to

    use acidic pond water as pump seal water instead of fresh process water thus

    saving 20 m3/hr of fresh water.

    The above modifications lead to zero consumption of process water in

    phosphoric plant with only minor consumptions for safety showers and

    cleaning purpose.

    6.12.2. Water conservation measures in Sulphur ic Acid Plant

    a) LP steam condensate recovery

    About 25 TPH of low pressure steam is used for melting of sulphur, molten

    sulphur storage tank and molten sulphur pipeline. All the steam condensate

    from the sulphur melting and storage area earlier drained to the storm water

    channel. This condensate is now sent to DM plant polishing unit. As a result of

    this about 20 m3/h of DM water is saved.

    b) Waste heat boi ler blow down recovery

    Earlier blow down from waste heat boilers of around 10 m3/hr was drained in

    the storm water channel. This is diverted to Intermediate absorption tower and

    Final absorption tower dilution tanks for sulphuric acid dilution thus reducing

    the consumption of water by 10 m3/hr.

    7.0 Impact of Improvements

    Figure 13 and 14 clearly indicate how Electrical Energy and thermal energy

    consumption of the plant improved over the years respectively. Specific

    consumption of electivity has been reduced from about 958 kWh/ MT of P2O5

    in 2006-07 to 568 kWh/MT of P2O5 in 2012-13. In the year 2013-14, it is

    expected that this shall be about 500 kWh/MT of P2O5. The water

    consumption has reduced significantly.

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    958

    833806

    718

    620 616

    568

    400

    500

    600

    700

    800

    900

    1000

    KWH/MTof

    P2O5inFertlizer

    Overall Specific Consumption of Electricity

    Thermal Energy Consumption was reduced from 2.99 Gcal/MT of P2O5 in the

    year 2006-07 to 1.71 Gcal/MT of P2O5 in the year 2012-13. Lowest thermal

    energy consumption of 1.07 Gcal/MT of P2O5 was achieved in the year 2011-

    11. Thermal energy consumption in recent years has gone up due to stoppage

    of Sulphuric Acid Plant for revamping the Absorption Towers. The overall

    specific consumption of water has been brought down from 12.90 M3 per tonne

    product in 2006-07 to 6.01 M3 per tonne of product in 2012-13 (Figure 15).

    Gcal/tonneP2O5

    1.18

    1.71

    2.99

    2.43

    2.04

    1.31.07

    0

    0.5

    1

    1.5

    2

    2.5

    3

    3.5

    2006-07 2007-08 2008-09 2009-10 2010-11 2011-12 2012-13

    Thermal Energy Consumption per tonne of Complex fertilizer

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    Figure 15

    8.0 Conclusion

    With moderate investment in the energy conservation and environment

    improvement measures as on-going process, there is steady decline of energy

    consumption and reduction in emission of sulphur dioxide and fluorine.Consumption of electric and thermal energy have come down from 568 kWh/MT

    of P2O5 to 500 kWh/MT of P2O5 and 2.99 Gcal/MT of P2O5 to 1.71 Gcal/MT of

    P2O5 respectively from 2006-07 to 2012-13. The water consumption has also

    been reduced from 12.90 M3/MT of product to 6.01 M3/MT of product during

    the same period.