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पता सू�च / Address List
1. मुख ् य अ भयंता (एचपीसी व जल पKरयोजना) एपीजेनको, हैदराबाद/ Chief Engineer (Generation I), APGENCO, Hyderabad
2. मुख ् य अ भयंता (पKरयोजना), एपीजेनको, हैदराबाद/ Chief Engineer (Projects), APGENCO, Hyderabad
3. मुख ् य अ भयंता (�व�युत �णाल�), एपीMान ् स ् को, हैदराबाद/ Chief Engineer (Power System), APTRANSCO,
Hyderabad.
4. मुख ् य अ भयंता ( उत ् पादन), ट�एसजेनको, हैदराबाद/ Chief Engineer (Generation), TSGENCO, Hyderabad
5. मुख ् य अ भयंता (पKरयोजना), ट�एसजेनको, हैदराबाद/ Chief Engineer (Projects), TSGENCO, Hyderabad
6. मुख ् य अ भयंता (�व�युत �णाल�), ट�एसMान ् स ् को, हैदराबाद/ Chief Engineer (Power System), TSTRANSCO,
Hyderabad
7. मुख ् य अ भयंता (इले.Oडज़ाईन), केपीसीएल, ब�गलूर/ Chief Engineer (Ele. Designs), KPCL, Bangalore
8. मुख ् य अ भयंता ( आर ट�), केपीट�सीएल, ब�गलूर/ Chief Engineer (RT), KPTCL, Bangalore
9. मुख ् य अ भयंता, एसएलडीसी, केपीट�सीएल, ब�गलूर/ Chief Engineer, SLDC, KPTCL, Bangalore
10. मुख ् य अ भयंता (एम.ट�.एस), टैनजोडको, चैन ् नै/ Chief Engineer (MTS), TANGEDCO, Chennai
(Fax No: 044 – 28585804)
11. मुख ् य अ भयंता (जल �व�युत), टैनजोडको, चैन ् नै/ Chief Engineer (Hydro),TANGEDCO, Chennai
(Fax No: 044 – 28553356)
12. मुख ् य अ भयंता (संर�ण एव ं संचार), ट� एन ई बी, चने ् नै/ Chief Engineer (Protection & Communication),
TANTRANSCO, Chennai
13. मुख ् य अ भयंता (पारेषण), �णाल� �चालन, एचएमट� कालोनी, केएसईबी, कलमस ् सेर�-683503/ Chief Engineer
(Transmission) System Operation, HMT Colony, KSEB, Kalamassery-683503
14. अधी�क अ भयंता-।, �व�युत �वभाग, 137, एनएससी बोस साल,ै पुदचुरे�- 605001/ Superintending
Engineer –I, Electricity Department, 137, NSC Bose Salai, Puducherry – 605001 (Fax No: 0413-
2331556)
15. जी एम ( �चा व अनु) द�-े।, पावर�Uड, सकंदराबाद/ GM (O&M), SR-I, PGCIL, Secunderabad
16. जी एम ( �चा व अनु) द�-े।।, पावर�Uड, ब�गलूर/ GM (O&M), SR-II, PGCIL, Bengaluru
17. महा�बंधक (ओ एस), एनट�पीसी, द��ण �े�ीय मुख ् यालय, सकंदराबाद/ General Manager (OS), NTPC SRHQ,
Secunderabad
18. मुख ्य महा�बंधक ,ट�पीएस-। �वस ्तार ,एनएलसी ,नैवेल� - 607807/ Chief General Manager, TPS-I Expn. NLC,
Neyveli-607807 (Fax No: 04142 – 265303)
19. मुख ् य अ भयंता (पारेषण) एनपीसीआईएल, मुंबई/ Chief Engineer (Transmission), NPCIL, Mumbai.
20. क� � "नदेशक, केजीएस, कैगा, कना#टक/ Station Director, KGS, Kaiga, Karnataka
21. क� � "नदेशक, एमएपीएस, कल ् पक् कम/ Station Director, MAPS, Kalpakkam
22. क� � "नदेशक, केकेएनपीपी, "तXनल ् वेल� िजला, त मलनाडु- 627106/ Station Director, KKNPP, Thirunelveli
Dist, TamilNadu-627106
23. Yी पी पी जेस ् ट�न, एजीएम (ईएम), एनट�ईसीएल, चने ् नै-103/ Shri P.P. Gestine, AGM (EM), NTECL,
Chennai-103.
24. Yी एम �भाकर, महा�बंधक (� व अ), एनट�पीएल, हाब#र ए� टेट, तूतुकुडी- 628004/ Sh. M. Prabhakar,
GM (O&M), NTPL, Harbour Estate, Tuticorin – 628004 (Fax No: 0461 – 2352842)
25. Yी सूय# �काश, उपा] य� (�चालन व अनुर�ण), जेएसड^ _ यू एनज` ल. तोरणग_ लु, ब_ लार� – 583275/
Shri Surya Prakash, Vice President (Operations & Maintenance), M/s JSW Energy Ltd, Toranagallu,
Bellary-583275
26. Yी शांताराम प,ै सह उपा] य� (�व�युत एवं पKरयोजना), जेएसड^ _ यू एनज` ल. तोरणग_ लु, ब_ लार� –
583275/ Shri Shantharam Pai, Associate Vice President (Electrical & Projects), M/s JSW Energy
Ltd, Toranagallu, Bellary-583275
27. Yी आर वी भbए, उपाध ् य� ( �चालन) यूपीसीएल, ब�गलूर/ Shri R.V.Bhat, Vice President (Operations), UPCL,
Bangalore
28. सह उपा] य� ( संर�ण व मीटKरगं), अदानी पावर ल, 8-ए, 'संभव' जज भवन के सामने, बोदकदेव,
अहमदाबाद- 380015, गुजरात / Associate Vice President (Protection & Metering), Adani Power Ltd,
8-A, ‘Sambhav,’ Opp. Judge’s Bungalow, Bodakdev, Ahmedabad 380 015, Gujarat, India
29. Yी dब�युत च$बत` (�धान �व�युत एवं सी आई अनुर�ण) ट�पीसीआईएल, e यानपुरम / नेलf तूX Uाम, मुतुकूर
मंडल, एसपीएसआर ने_ लूर- 524344/ Sh. Bidyut Chakraborty (Head Electrical and C&I Maintenance),
TPCIL, Pyanampuram/ Nelaturu Village, Muthukur Mandal, SPSR Nellore – 524344 (Fax No: 0861
– 305 2304)
30. Yी आर एस कुमार� वामी, सलाहार(�व�युत), सीईपीएल, मेलमरडूर Uाम, ओ+b�पदरम ता_ लूक, तूतुकुडी-
628105, त मलनाडु/ Sh. R.S. Kumaraswamy, Advisor (Electrical), CEPL, Melamarudur Village,
Ottipidaram Taluk, Tuticorin – 628 105, Tamil Nadu (Fax No: 0461 – 2614297)
31. Yी ;कशोर आक# ट, वKर. उपा] य� (� व अ), आईएल व एफएस, ट�पीसीएल, सी पुदपेुbै डाक, परनगीपेbै,
भुवन�गKर ता_ लूक, कुडलूर िजला, त मलनाडु- 608502/ Sh. Kishore Arcot, Sr. Vice President (O&M),
IL&FS Tamilnadu Power Company Ltd., C.Pudhupettai (post), Parnagipettai, Bhuvanagiri Taluk,
Cuddalore Dist, Tamilnadu – 608502 (Fax No: 0414-4252991)
*****
Agenda for the 64
th Meeting of PCSC scheduled to be held on 25
th May, 2017 Page 1
SOUTHERN REGIONAL POWER COMMITTEE BENGALURU
Agenda for the 64th Meeting of Protection Coordination Sub-Committee of SRPC to be held on 25th May, 2017 (Thursday)
1. Introduction
2. Confirmation of Minutes of last PCSC meeting
Confirmation of minutes of 63rd Protection Coordination Sub-Committee meeting held on 26.04.2017.
3. Grid Occurrences
3.1 Grid Disturbances (GD), Grid Incidences (GI), and trippings due to failure of Auto-reclosing (A/R), and mal-operation of PLCC equipment that occurred during the period March-April, 2017 given at Annexure-I would be discussed in the PCSC meeting.
Constituents are requested to furnish the following information in respect of the above grid occurrences to have fruitful discussions in the PCSC forum.
(a) Single line diagram of the station with switching devices, CT, PT and relay
details. (b) Cause of the tripping & Remedial Action taken (c) Relay setting details
Constituents are requested to bring/ furnish full particulars of the tripping events pertaining to their system.
3.2 In compliance of Regulations 5.2 (r) of IEGC, the Constituents are required to
furnish the following information in respect of Grid Occurrences within 24 hrs of occurrence of the same to SRLDC/ SRPC: (a) First Information Report (FIR) (b) Event Logger (EL) output (c) Disturbance Recorder (DR) output (d) Trip event analysis report (with pre and post fault system conditions) Non-furnishing of tripping details (FIR/DR/EL/TR) for the period 01.04.2017 – 30.04.2017 had been brought to Constituents’ notice vide letters (i) No. SRPC/ SE-III/ PCSC-63/ 2017/2107 - 08 dated 18.04.2017 and (ii) No. SRLDC/ SRC&S/2017/ dated 12.04.2017. Non-compliance in this regard would be discussed in the meeting.
4. Submission of Reports/Compliance by Constituents
4.1 Status of pending Protection Coordination Sub-Committee (PCSC) Recommendations
Status of the pending PCSC recommendations (up to 62nd PCSC meeting) given at Annexure-II may please be sent latest by 22.04.2017.
Agenda for the 64th
Meeting of PCSC scheduled to be held on 25th
May, 2017 Page 2
4.2 Remedial measures for "Transmission Elements under Forced Outage"
The Constituents are requested to furnish the remedial measures/ action taken by them for the tripping events as circulated vide our emails. (Annexure-III)
The tripping events are based on the daily reports at SRLDC website http://srldc.in/ DailyReport.aspx under the menu: Reports->Daily-> "TL under Forced Outage")
4.3 Certificate for Healthiness of Batteries
As per the MoP direction given in pursuant to recommendations of the Enquiry Committee (NEW grid disturbance on 30th & 31st July, 2012), RPC’s are required to obtain from their respective Constituents the monthly certificate for healthiness of batteries, installed at 220 KV and above voltage level Substations (for power supply to Relays, RTUs and PLCC equipment) and furnish the same to CEA/ MoP.
With reference to above, the Constituents have been requested to submit the certificate on healthiness of batteries on monthly basis (i.e. status for a month shall be sent by the 7th day of the following month) to SRPC Secretariat.
The sought status for the month of April, 2017 is awaited from the following SR-Constituents:
APGENCO (Thermal), KPCL, KPTCL, TANTRANSCO, PED, PGCIL (SR-II) & JSWEL
5. Status of Implementation of Line Differential Protection (LDP) in Nellore and
Simhadiri complexes
Line differential protection has been recommended to be implemented for all 400 kV lines at Nellore and Simhadri Complexes vide various PCSC/ PSAG/Special meetings.
Complex Constituents responsible for implementation
Nellore PGCIL (SR-I), APGENCO, APTRANSCO, TPCIL, MEPL, SEL and NCC
Simhadri PGCIL (SR-I), NTPC, APTRANSCO and HNPCL
All above Constituents are requested to kindly present the status of implementation of LDP and concrete action taken so far in this regard.
6. Review of Implementation of Protection Audit Recommendations (PAR) of
SR-Constituents Hon’ble CERC vide their Order dated 15.12.2016 issued in respect of KSEB petition (88/MP/2016) and KPTCL petition (135/MP/2016), has directed SRPC to monitor the status of completion of PAR regularly in PCSC meetings and submit bi-monthly report to the Commission confirming the completion of Phase-I and Phase-II of PAR of the Constituents of Southern Region.
http://srldc.in/%20DailyReport.aspx
Agenda for the 64th
Meeting of PCSC scheduled to be held on 25th
May, 2017 Page 3
In this regard, the present status of PAR implementation by SR-Constituents as maintained by SRPC is enclosed at Annexure-IV. All SR-Constituents are requested to kindly update the latest status of implementation of their respective PAR, and furnish the same in soft copy (Excel format) latest by 08.06.2017 to SRPC Secretariat ([email protected]).
7. Other Protection Issues, if any, with the permission of the Chair
8. Sending Agenda items for the PCSC meetings
As per the Guidelines of CEA/MOP, it has been decided to conduct the PCSC meetings on monthly basis. It is requested that Agenda Items for the PCSC meetings, if any, may please be sent latest by 5th working day of the month to SRPC Secretariat to compile and circulate the same so as to have fruitful discussions in the PCSC meetings.
9. Date of next PCSC meeting
The 64th PCSC meeting would be conducted on 29.06.2017 (Thursday) from
10:30 hrs in the Conference Hall of SRPC Secretariat, Bengaluru.
*****
Grid Occurrences - 64
For all tripping events involving failure of substation equipment, Constituents are requested to kindly furnish the SLD or equivalent pictorial representation showing (i) Location of the fault, and (ii) Bus-bar arrangement/ Configuration of feeders and other connected equipment with proper CB positions (OPEN/ CLOSE) at the time of occurrence of the fault.
I. Details of Grid Disturbances:
Sl. No.
Details of Event Date & Time Reason Remarks Category
1 Complete outage of North Chennai TPS STG-2
24-Apr-17 at 21:02hrs
Tripping of evacuating lines due to fault led to tripping of Unit
Gen Loss: 435 MW
GD-1
2 Complete outage of North Chennai TPS STG-2
25-Apr-17 at 18:27hrs
Tripping of evacuating lines due to fault led to tripping of Unit
Gen Loss: 435 MW
GD-1
3 Complete outage of North Chennai TPS STG-2
26-Mar-17 at 21:09hrs
Tripping of evacuating lines due to fault led to tripping of unit at NCTPS Stg-2
Gen Loss: 167 MW
GD-1
4 Complete outage of North Chennai TPS STG-1
26-Mar-17 at 23:14hrs
Tripping of evacuating lines due to fault led to tripping of unit at NCTPS Stg-1
Gen Loss: 250 MW
GD-1
II. Details of Grid Incidents:
Sl. No. Details of Event Date & Time Reason Category
1
Tripping of 400/220KV 315MVA ICT-1and 230kV elements at 400kV Vemagiri substation of APTRANSCO
09-04-2017 at 12:31 hrs
Suspected mal-operation of Busbar protection had caused tripping of 220kV Bus-1 at Vemagiri.
GI-2
2
Tripping of 400/220kV ICT-2&3 at 400kV Ghani substation of APTRANSCO
10-04-2017 at 17:29 hrs
ICT-2&3 got tripped due to operation of 220KV Bus-2 busbar protection at 400/220KV Ghani substation.
GI-2
3 Tripping of 400/220kV Dichipally ICT-3
14-04-2017 at 13:19 hrs
ICT-3 at dichipally tripped on operation three phase trip relays i.e. 86A and 86B relays
GI-2
Annexure-I
Page 1 of 4
4 Tripping of 400kV lines and ICT’s at Guttur substation of KPTCL
17-04-2017 at 00:40 hrs
Lightening arrestor flashover had occurred in 400kV Guttur-Narendra line-1 at Guttur end
GI-2
5 Tripping of 765/400 kV ICT-1 at 765kV Vemagiri(PG)
18-04-2017 at 15:56 hrs
ICT-I tripped on Mal-operation of Y-phase Buchholz relay
GI-2
6 Tripping of 400/220 kV ICT-1 at Nelamangala
20-04-2017 at 17:08 hrs
ICT tripped due to mal-operation of Buchholz relay
GI-2
7 Tripping of 400 kV Guttur-Narendra line-1
21-04-2017 at 18:01 hrs
Line tripped on operation of over-voltage protection at Guttur end and direct trip was received at Narendra. DR and EL of Guttur station were not furnished to validate the tripping
GI-2
8 Tripping of 400 kV Tirunelveli-Kudankulam line-3
23-04-2017 at 05:56hrs
R-phase to earth fault had occurred in line. Tie CB LBB got operated at Tirunelveli end due to sluggish operation of Tie CB
GI-2
9 Tripping of 400/220 kV ICT-2 and 3 at Hoody substation of KPTCL
26-04-2017 at 15:40 hrs
ICT-2 tripped on suspected mal-operation Oil surge relay of B-phase transformer. ICT-3 tripped due to overloading.
GI-2
10 Tripping of 220 kV Alipura - Regulapadu line
29-04-2017 at 09:25 hrs
line tripped at Alipura on earth fault GI-1
III. Details of Trippings due to Failure or Non-operation of Auto-Reclose:
Sl. No. Element Date & Time Reason
Category
1 Tripping of 400kV Uruvakonda-Jamalamadugu line-1
02-04-2017 at 17:58 hrs
R-phase to earth fault and line did not auto-reclose. Fault clearing time - 500ms
GI-2
2 Tripping of 400kV Ghanapur-Mamidapalli line
04-04-2017 at 19:01hrs
B-phase to earth fault. Line auto reclosed from Mamidapalli end and tripped from Ghanapur
GI-2
3
Tripping of 400kV Kudgi-Tumkur line-1
09-04-2017 at 00:13 hrs
R-phase to earth fault had occurred in line. At Tumkur end line auto-reclosed and later tripped due to direct trip receive. At Kudgi end breaker did not attempt for auto-reclose.
GI-2
4 Tripping of 400kV Mysore-Kozhikode line
10-04-2016 at 20:53 hrs
R-phase to earth fault had occurred in line. A/R was successful at Mysore and Main & Tie CB's tripped at Kozhikode end.
GI-2
Annexure-I
Page 2 of 4
5
Tripping of 400kV Krishnapatnam-Nellore line-2
11-04-2017 at 2:41 hrs
Line tripped on due to Y-phase earth fault. Line auto-reclosed at Nellore (AP) and did not auto-reclose at Krishnapatnam.
GI-2
6
Tripping of 400kV Krishnapatnam-Nellore line-1
12-04-2017 at 2:51 hrs
Line tripped on due to Y-phase earth fault. Line auto-reclosed at Nellore (AP) and did not auto-reclose at Krishnapatnam.
GI-2
7 Tripping of 400kV Alamathy-NCTPS-2
12-04-2017 at 3:31 hrs
Y-phase to earth fault. A/r not in service due to communication link failure
GI-2
8 Tripping of 400 kV Alamathy-NCTPS-1
12-04-2017 at 03:43 hrs
B-phase to earth fault. A/r not in service due to communication link failure
GI-2
9 Tripping of 400kV Krishnapatnam line-2
13-04-017 at 3:59 hrs
Y-phase to earth fault. line auto-reclosed from Nellore end and did not auto-reclose from Krishnapatnam end
GI-2
10 Tripping of 400kV Krishnapatnam line-1
13-04-2017 at 4:38hrs
Y-phase to earth fault. line auto-reclosed from Nellore end and did not auto-reclose from Krishnapatnam end
GI-2
11 Tripping of 400kV Vijayawada-Vemagiri line -2
18-04-2017 at 16:29 hrs
R-phase to earth fault had occurred in line. Auto-reclose was successful at Vemagiri end and breaker tripped at Vijayawada
GI-2
12 Tripping of 400kV Vijayawada-Nellore line
19-04-2017 at 16:57 hrs
Y-phase to earth fault had occurred in line and auto reclose was successful at Nellore end and breaker tripped at Vijayawada
GI-2
13 Tripping of 400kV Krishnapatnam-Chitoor line
20-04-2017 at 15:34 hrs
R-phase to earth fault had occurred in line. Auto-reclose was successful at Chitoor and auto reclose was not successful at Krishnapatnam end.
GI-2
14 Tripping of 400kV ALAMATHI- NCTPS ST2 line-1
23-04-2017 at 19:53 hrs
R-phase to earth fault had occurred in line. Line did not auto-reclose due to communication Link Fail between Alamthy and NCTPS
GI-2
15 Tripping of 765kV Srikakulam-Vemagiri line-1
27-04-2017 at 14:51 hrs
Y-phase to earth fault had occurred in line and line did not attempt auto-reclose.
GI-2
16
Tripping of 765kV Kurnool-Nellore PS line-2
27-04-2017 at 22:22 hrs
R-phase to earth fault had occurred in line. Auto-reclose was successful at Kurnool end and breaker at Nellore PS end did tripped and did not attempt for auto-reclose.
GI-2
17
Tripping of 400 kV Alamathy -NCTPS line-2
28-04-2017 at 1:00 hrs
Line tripped due to R-phase to earth fault. Auto-reclose is not in service as Fibre optic cable link is not healthy
GI-2
Annexure-I
Page 3 of 4
IV. Details of Trippings due to PLCC mal-operation:
Sl. No. Element Date & Time Reason
Category
1 Tripping of 400kV Munirabad-Guttur line
09-04-2017 at 18:04 hrs Line tripped due to direct trip receive
from Guttur end.
GI-2
09-04-2017 at 18:52 hrs
2 Tripping of 400kV Cudappah-Chitoor line
15-04-2017 at 19:00 hrs
Line tripped at Cudappah end only on direct trip receive and was holding from Chitoor end
GI-2
16-04-2017 at 10:59 hrs
3 Tripping of 400kV Gooty-Tumkur line
20-04-2017 at 10:38 hrs
Line tripped at Gooty end only and was holding from Tumkur end
GI-2
4 Tripping of 400kV VTPS-Malkaram line
20-04-2017 at 16:24 hrs
Line tripped on Direct Trip Receive at Malkaram and was in service from VTPS
GI-2
5 Tripping of 400kV Ramagundam-Dichipally line
29-04-2017 at 23:54 hrs
Line tripped due to operation of over voltage protection at Dichipally end. Ramagundam end did not trip as direct trip was not received from remote end.
GI-2
6 Tripping of 400kV Hyderabad-Kurnool line
30-04-2017 at 18:04 hrs
Line tripped on over-voltage protection at Kurnool end. Line was holding from Hyderabad end as direct trip was not received from Kurnool.
GI-2
*****
Annexure-I
Page 4 of 4
Meeting No /
Index
Details of Event Date & Time Reason PCSC Recommendations Utility responsible for
Implementation
Status of Recommendations
as on 15.05.2017
Remarks
61/IV/3 Tripping of 400 kV Vijayawada-
Vemagiri line-2
16-12-2016 at
21:52 hrs
&
26-12-2016 at
10:52 hrs
Line tripped on operation of over-voltage protection at
Vemagiri end and Direct Trip was received at
Vijayawada.
APTRANSCO to make DR & EL functional from Vijayawada end
for the line 400 kV Vijayawada – Vemagiri.
APTRANSCO Yet to be informed Pending
APTRANSCO mail dated on 31-08-2016:
To avoid the unwanted malopeartions due to the external LBB trip
initiation from PGCIL, Vide letter Dt: 04-08-2016, APTRANSCO has
requsted the PGCIL to arrange the Master trip relay and breaker contacts
of ICT-1 &2 LV side to enable the internal LBB feature in the Busbar
protection scheme at 220kV Gooty Switching station. Waiting for the
PGCIL response.
APTRANSCO mail dated on 15-11-2016:
To avoid the unwanted maloperations due to the external LBB trip
initiation from PGCIL, vide letter Dt: 04-08-2016, ARTRANSCO has
requested the PGCIL to arrange the Master trip relay and breaker contacts
of ICT-1&2 LV side to enable the internal LBB feature in the Busbar
protection scheme at 220kV Gooty Switching station. Waiting for the
PGCIL response.
APTRANSCO mail dated on 20-12-2016:
Waiting for the PGCIL response.
APTRANSCO mail dated 04.03.2017
SRPC is requested to coordinate with PGCIL in takind necessary action.
Pending
APGENCO to furnish a report on the remedial action implemented
w.r.t. overreaching of Krishnapatnam end distance relays during the
tripping of 400 kV Nellore (PG) - NPS line-1
APGENCO Yet to be informed Pending
Pending Implementation of PCSC Recommendations (up to 62nd Meeting)
Complete outage of 220kV Yerraguntla
substation and tripping of running Units
at Rayalaseema TPS
52/I/2 (GD) PendingMail received on 27-07-2016:
1.The drop out relays of reducer oil pumps time setting was increased for
all mills.So there will not be any trip under transient low voltage condition.--
--Complied
2.The recommendation regarding 2 sec time delay will be implemented
during unit shut down and will be intimated immediately after
implementation.------Pending
APGENCO 1. APGENCO to check associated logic for lube oil pump for correct
operation under transient low voltage conditions at Rayalaseema TPS,
Unit-1.
2. APGENCO to keep appropriate time delay/ fault ride through
delay (typically 2 sec) in VFD speed sensor relay at all its generating
Units including Rayalaseema TPS Units.
HV B-Ph Current transformer of 100MVA Power
Transformer -1 failed resulting into a bus fault on
220KV Bus-1. Unit-1 and Unit-5 at RYTPS tripped
during the fault at Yerraguntla substation
21-02-2016 at
10:39 hrs
Andhra Pradesh
APTRANSCO1.APTRANSCO to check the healthiness of the connecting cable
between Gooty (PGCIL) and Gooty (APTRANSCO), and replace it,
if required.
2.APTRANSCO to ensure that the distributed architecture employed
in implementing busbar protection at their Gooty 220 kV SS does not
introduce any unwarranted delays in transmitting the triggering signals
to the Central Unit.
LBB protection got operated for 400/220kV ICT-2
breaker which had resulted in tripping of 220kV Bus-
2 at 220kV Gooty Substation
24-06-2016 at
16:04 hrs
Tripping at 220kV Gooty Substation of
APTRANSCO
56/II/13
57/II/9 Tripping of 400 kV Nellore (PG) - NPS
line-1, 400 kV Krishnapatnam-Nellore
(AP) lines -1&2 and 400kV NPS -
MEPL line
18-07-2016 at
19:05 hrs
Triggering incident was snapping of Y phase
conductor in 400kV Nellore (PG) - NPS line-1.
Distance relay at Krishnapatnam end over-reached in
Zone-1, and resulted in tripping of 400kV
Krishnapatnam – Nellore (AP) lines - 1&2 from
Krishnapatnam end. Distance relay at MEPL over-
reached and resulted in tripping of MEPL-NPS line
from MEPL end.
Annexure-II
Page 1 of 30
58 TSGENCO The issue was discussed in PCSC-58 meeting held on 18.10.2016, when
PCSC forum agreed to de-link the implementation of the Item from the
scope of Protection Audit Recommendations (PAR), and pursue it as part
of PCSC Recommendations.
Pending
62/III/4 Tripping of 400 kV Sattenapalli –
Srisailam line-1
24-02-2017
at 06:48 hrs
R-ph to earth fault. Line did not auto-reclose at
Srisailam end.
TSGENCO (Hydro) to configure all protection relays DR‟s time scale
for a post-triggering period of 2 sec.
TSGENCO Yet to be informed Pending
Triggering incident was R-phase to earth fault in 220
kV Vijayawada TPS - Podili line. Breaker at
Vijayawada TPS end was under lockout and this
resulted in operation of LBB protection and further
leading to tripping of 220 kV Bus-1 at Vijayawada
TPS
02-06-2016 at
00:41 hrs
55/II/21
Telangana
APTRANSCO mail dated on 31-08-2016 & 15-11-2016:
1.Pending
2.Pending
3.PLCC carrier aided protection wasprovided.----Completed
A/R feature ----Pending
APTRANSCO mail dated on 20-12-2016:
At Podili on VTS feeder the old CGL make penumatic operated breaker is
to be replaced with new one.
APTRANSCO mail dated on 04.03.2017:
The existing neumatic mechanism of breaker does'nt support for enabling
of A/R feature on VTS feeder at Podili.
APGENCO/
APTRANSCO
TSGENCO TSGENCO mail dated 30.03.2017:
1. According to SRPC phylosphy power swing block settings are changed
to ALL ZONES BLOCK EXCEPT ZONE1.
---------- Completed
2. M/s. Siemens is requested to depute the service Engineer to update the
firm ware of existing SIPROTEC relays in 400KV switch yard. This work
will be completed on or before 15.04.2017. -------------- Pending
Pending
Provision of line differential protection for Jurala line 1 & 2 (line length-1.45 KM) feeders at 220 kV Jurala HPS [Carry-Over from Protection Audit Recommendations]
Pending1.APGENCO to ensure full-fledged redundancy of supply to the
auxiliaries of all Units in the to-be-reviewed LT arrangement by (i)
ensuring that each Unit‟s auxiliaries are fed from two Station
Transformers connected to different buses, or (ii) any other better
design.
2.APGENCO to keep LBB time setting as 200 msec at their
Vijayawada TPS.
3.APTRANSCO to take steps to provide PLCC carrier
communication & Auto-reclosure facility between VTPS and Podili
SS.
24-12-2016 at
10:52 hrs
61/III/5 Tripping of 400 kV Khammam - KTPS
line-2
Line tripped on B-phase to earth fault. First fault was
persistent for 380 ms. Auto-reclose was successful at
Khammam end during 1st fault. 2nd fault occurred
during re-claim time of breaker hence Khammam end
breakers also got tripped.
1. TSGENCO to implement the SRPC agreed philosophy for Power
Swing Blocking in all distance relays on the feeders emanating from
KTPS.
2. For the line under consideration, TSGENCO to consult relays
OEM to migrate to new versions of Firmware (from to 4.72.01) and
Pset (to 4.70.02).
Multiple tripping at Vijayawada TPS
(Gen Loss : 750 MW)
Annexure-II
Page 2 of 30
62/IV/5 Tripping of 400 kV Gajwel-
Bhoopalapalli line-1
16-02-2017
at 15:00 hrs
Line tripped at Bhoopalapally on DT receive and was
holding from Gajwel.
For the line under consideration, TSTRANSCO to carry out the
following in coordination with TSGENCO:
(i) Healthiness of PLCC system components (hardware and software)
at both ends shall be checked and faulty components shall be repaired/
replaced.
(ii) End-to-end communication for DT/ permissive & other signals
may be ensured by testing at both the ends.
(iii) Frequency bandwidth tuning of PLCC link for faithful
transmission of signals shall be carried out.
07-09-2015 at
2:58 hrs
Line tripped on operation of over-voltage protection at
Mahboobnagar and direct trip received at N‟sagar
station. DT receive was observed in DR and EL of
N‟sagar station. D.R/EL of Mahboobnagar was not
furnished to validate the overvoltage tripping
Tripping of 400kV Nagarjunsagar-
Mahboobnagar line
48/II/5 Pending
For the line under consideration, the following shall be carried out by
TSTRANSCO in coordination with PGCIL (SR-I):
(i) End-to-end communication for DT/ permissive & other signals
may be ensured by testing at both the ends.
(ii) Healthiness of PLCC system components (hardware and software)
at both ends shall be checked and faulty components shall be repaired/
replaced.
line tripped on direct trip receive at Gajwel and was
holding from Hyderabad
06-10-2016 at
12:16 hrs
Tripping of 400 kV Gaiwel-Hyderabad
line
59/IV/3 Pending
TSTRANSCO TSTRANSCO mail dated on 21-12-2016:
Due to employee bifurcation process and consequent relieving of
engineers, the data could not be given. However the data for the
subsequent disturbances are being communicated regularly.
TSTRANSCO to furnish a detailed report on the tripping event
along with remedial measures taken to PCSC forum.
220 kV feeders and ICT‟s connected to Bus-1 at 220
kV Ghanapur Station tripped on operation of Bus-bar
protection during fault in 220 kV Ghanapur -
Chandrayangutta lines 1&2
1.TSTRANSCO make DR‟s & EL‟s functional on all feeders distance
protection and busbar protection at their 220 kV Ghanapur SS.
2.TSTRANSCO to modify A/R Block logic such it gets blocked not
on account of mere Z2/ Z3 pick-up, but only when Z2/ Z3 protection
issues trip command at their 400 kV Mamidipalli SS for all feeders.
3.TSTRANSCO to spare one potential-free contact to PGCIL (SR-II)
for triggering DR/EL of 400/ 220 kV ICT‟s at their 400 kV Ghanapur
SS.
21-09-2016 at
19:10 hrs
Multiple trippings at 220 kV Ghanapur
substation
59/II/3 TSTRANSCO TSTRANSCO mail dated on 21-12-2016:
1. DRs and ELs are already functional and also submitted in the 59th
PCSC Meeting.
2. A/R Block logic is been modified.
3.---Pending
Pending
TSTRANSCO mail dated on 21-12-2016:
(i) Letter is been given to field for conducting end to end testing of 400kV
Gajwel-Ghanapur line.
(ii) Healthiness of PLCC system components will be checked while
conducting end to end testing.
TSTRANSCO
TSGENCO /
TSTRANSCO
Yet to be informed Pending
Annexure-II
Page 3 of 30
RTPS Tripping incidents and the Spl
meeting held at RTPS on 13th and 14th
March 2014
The PCSC forum recommended for replacement of existing
electromechanical relays with Numerical relays.
Karnataka
Spl meeting held at RTPS on 13th
and 14th
March
2014
Mar-1430/I/A Pending Mail recieved on 28-05-2015:
1. e- Tender folated for the retrofit of existing static relays with Numerical
version for lines M.nagar,M.bad,ICT-1 & 2 -Technical Bid & Price bid
opened . Bid evaluation and approval to place P.O. is in progress.
2. Retrofit of existing bus bar (CAG-34) with numerical version -
Budgetetory offers obtained and is in process.
3. Order placed on M/s Siemens to replace relays. The work will be
completed by May - 2015.
Mail recieved on 07-07-2015:
1. Retrofit of existing static relays with Numerical version for lines
M.nagar, M.bad and ICT- 1 & 2 -- Inspection of the Numerical relays at
M/s Siemens works completed on 11-06-2015 and Dispatch clearance has
been issued. Materials received.
2. Retrofit of existing bus bar (CAG-34) with numerical version –
Budgetary offers obtained and is under process.
Mail recieved on 07-09-2015:
1. Replacement of Old electromagnetic relays with Numerical relays has
been completed for RTPS-BTPS line & commissioned on 18.03.2014.
Raichur-PG1 & Raichur-PG2 lines have already retrofitted with numerical
relays.
The retrofitting of electromechanical relays with Numerical version for ICT-
1, ICT-2 and Munirabad line has been completed.
Retrofitting work for Mehaboobnagar line is pending. Awaiting for line
shutdown.
2. Job order placed on 26.06.2015 on M/s Alstom T&D India Ltd. Chennai
for retrofitting of relays for all 220kV lines at RTPS.
3. Retrofit of existing bus bar(CAG-34) with numerical version–
Budgetary offers obtained and is under process.
Mail recieved on 21-10-2015 and 23-11-2015:
1) Replacement of Old electromagnetic relays with Numerical relays has
been completed for RTPS-BTPS line & commissioned on 18.03.2014.
Raichur-PG1 & Raichur-PG2 lines have already retrofitted with numerical
relays.
The retrofitting of electromechanical relays with Numerical version for the
following lines/ICTs have been completed/commissioned as follows:
a) ICT-2 –Commissioned on 01-08-2015
b) ICT-1 ---Commissioned on 08-08-2015
c) Munirabad line--- Commissioned on 16-08-2015.
d) Mehaboobnagar line-- Commissioned on 09-09-2015.
2. Job order placed on 26.06.2015 on M/s Alstom T&D India Ltd.
Chennai for retrofitting of relays for all 220kV lines at RTPS.
3. Retrofit of existing bus bar(CAG-34) with numerical version–
Budgetary offers obtained and is under process.
KPCL
Annexure-II
Page 4 of 30
A fault had occurred in 220 kV Kadra and Kodasalli.
As A result, de-energization of 220kV bus occurred at
Kadra and Kodasalli.
13-11-2014 at
19:31hrs
41/I/1
Tripping of
400/220kV ICT-1 at
BTPS
43/II/14
16-02-2015 at
12:56 hrs
Triggering incident was B-phase to earth fault had
occurred in 220kV Kadra-Kodasalli line. Line tripped
from Kodasalli end only. 220kV Kaiga-Kadra tripped
in Zone-3 from Kaiga end. Tripping of evacuating
lines caused bus shut down at Kadra hydro station.
38/GD/3.5 GD-1 at Kadra and Kodasalli hydro
power station
GD-1 at 220kV Kadra power Station of
KPCL
ICT tripped due to operation of Over current and
Earth fault relay
14-01-2015 at
1:09
hrs
1. KPCL to make functional the Main2 (EPAC) relay with the
help of KPTCL at the earliest.
2. KPCL to investigate the reason for DC fuse fail during
transient fault in 220kV Kadra-Kodasalli line including the testing/
checking of DC supply cables, breaker control cables, and trip coils.
3. KPCL to ensure supply for Main-1& Main-2 protections, Trip
Coils (TC1, TC2) from separate battery banks.
KPCL
Mail received on 28-05-2015:
1. Main-2 relays already installed and commissioned.
2. DC fuses are intact. Till date no such incidence occurred.
3. Possibility of DC-1 & DC-2 arrangement and splitting of DC will be
reviewed.
Mail received on 07-07-2015 , 21-10-2015 and 23-11-2015:
1. Completed.
2. Completed.
3. Possibility of DC-1 & DC-2 arrangement and splitting of DC will be
reviewed.
KPCL to check the possibility of providing line differential protection
between RTPS and Yermarus stations.
Pending
PendingKPCL
Mail recieved on 28-05-2015:
1) e-NIT floated on 28.07.2014 for procurement of Numerical distance
relays & GPS. As there is change in scope of work and quantity of relays
by more than 25%, which is not permitted as per KTPP act. Hence, tender
cancelled and refloated on 05.05.2015 with revised scope of work and
revised PQR.
2. However, as per the recommendations of PSAG, Relays were
temporarily rearranged, replaced and wired up. testing & commissioning
shall be completed with the assistance of KPTCL.
Mail recieved on 07-07-2015:
1. Cover -1 of the bid is scheduled for open eing on 25.06.2015.
2. As per the recommendations of PSAG, Relays were temporarily
rearranged. testing & commissioning completed with the assistance of
KPTCL.
Mail recieved on 07-09-2015:
NIT floated on 5.5.15 through e-portal. Bid evaluation completed.
Obtaining of Administration approval to place P.O is in progress.
However, as per therecommendationsof PSAG-10, Relays
weretemporarilyrearranged.Testing & commissioning completed with the
assistanceofKPTCL.
Mail recieved on 21-10-2015:
NIT floated on 5.5.15 through e-portal. Bid evaluation completed. LOA's
issued to M/s Schneider Electric Infrastructure Ltd. on 08.10.2015.
Mail recieved on 23-11-2015:
LOA's issued to M/s Schneider Electric Infrastructure Ltd. on 08.10.2015.
Engineering work is in progress.
Status informed during Special Meeting held on 03.06.2016:
LOA‟s issued to M/s Schneider on 08.10.2015. Inspection of relays
completed and received at site. DI issued for all balance materials except
furnitures.
PendingKPCL1. The PCSC forum requested KPCL to speed up the installation of
Numerical Distance Protection relay in Kadra –Kaiga and
Kodasalli –Kaiga.
2. The PCSC forum requested KPCL to submit the implementation
status of PSAG-10 recommendations within a week‟s time.
KPCL vide their mail dated 07.07.2015 informed that revised relay settings
would be incorporated in co-ordination with KPTCL.
Mail received on 07-09-2015 , 21-10-2015 and 23-11-2015:
Revised relay settings are awaited from KPTCL.
Revised relay settings furnished by KPTCL will be incorporated in co-
ordination with KPTCL shortly.
Annexure-II
Page 5 of 30
49/II/15 Trippings at Raichur TPS 12-11-2015 at
00:30 hrs
Running Unit-4, 5 and Unit-8 and 400kV RTPS-
Yeramaras TPS feeder got tripped due to de-
energization of both 400kV Bus-1&2 at Raichur TPS
1. KPCL to carry out hot-line washing of RTPS-connected lines
regularly to avoid trippings due to fog and dust.
2. KPCL may see the feasibility of providing breaker flashover
protection at RTPS, and implement the same if possible.
KPCL Status informed during Special Meeting held on 03.06.2016:
1. Hot line washing was done previously.tender process is on for silicon
coating of insulators.
Pending
54/II/4 Tripping of 400 kV Raichur TPS-
Mahboobnagar line
05-04-2016 at
10:23 hrs
Line tripped on operation of Backup impedance
protection of line reactor. Direct trip was received at
Mahboobnagar end.
KPCL to keep the functioning of the concerned electro-mechanical
back-up impedance protection relay under observation, and replace it
with a spare at the earliest.
KPCL Yet to be informed Pending
54/II/9 Pending
46/II/21 Trippings at 220kV Raichur TPS 1. KPCL to check the operation of anti-pumping relay on 220 kV side
and keep it in healthy condition.
2. KPCL to provide manual reset to the 220 kV side master trip relay.
3. KPCL to use both the 220 kV buses as main buses under normal
operation, and should go for single bus operation only during
emergencies.
1.KPCL to undertake the following remedial measures to avoid
breaker flashovers:
(i) Replacing all porcelain insulators with composite insulators
(ii) Carrying out hot-line water washing of all insulators on regular
basis.
(iii) Applying Room Temperature Vulcanizing (RTV) Silicone high
voltage insulator coatings to all bus-connected ceramic insulators of
equipment like CT, PT, CB, Isolators etc.
2.KPCL to take steps to provide dedicated breaker flashover
protection to all breakers at Raichur TPS at the earliest.
KPCL
1. KPCL to revise the settings of GT‟s back-up O/C and E/F
protections considering their individual contribution to solid bus fault
at 220 kV bus of Nagjheri PH.
2. KPCL to upload/ make available various tripping files
(FIR/DR/EL/TR) for all tripping involving their stations in compliance
of IEGC Regulation 5.2 (r).
54/I/4 Tripping of Nagjheri Generators 220 kV Nagjheri - Bidnal line tripped on B-E fault at
12:28 Hrs. At the same time, five running generating
units (1, 2, 3, 4 & 6) at Nagjheri tripped on operation
of Generator Transformer‟s back-up Over Current &
Earth Fault protection.
07-06-2015 at
01:35 hrs
Mail received on 21-10-2015:
1) Anti-pumping contactors of all the nine 220KV Lines are in circuit and
tested periodically during AOH works of lines along with other protections.
2) Completed.
3) Possibility to use both the 220kV buses as main bus under normal
operation is under review.
Mail recieved on 23-11-2015:
1) Completed
3) Two bus operation for 220kV buses : In place of existing CT switching
relays, High speed manual heavy duty change over switch of sufficient
current capacity will be retrofitted to all feeders at 220kV station and same
will be operated manually during changeover of feeder by one bus to the
other and this arrangement may facilitate to put both buses in service. Time
required for this retrofit is around 90days . However, this work will be
taken up only after retrofitting of electromagnetic relays with numerical
relays for Main-2 protection of all 220kV lines, for which work is in
progress.
Yet to be informed
Yet to be informed
KPCL
Pending
Y-ph Pole of Tie-breaker of Unit-4 at RTPS failed.
Unit-4 got tripped on operation of Generator
Differential, Reverse power & LBB protection.
Operation of LBB protection led to tripping of BUS-2
at RTPS
Tripping of 400kV Raichur TPS Bus-2 13-04-2016 at
21:12 hrs
Pending
14-04-2016 at
12:29 hrs
KPCL
Annexure-II
Page 6 of 30
55/II/1
56/I/2 Complete outage of 220kV Sedam
Substation of KPTCL.
19-06-2016 at
15:27hrs
220kV Sedam-Humnabad-2 tripped at Sedam on
Distance protection, Zone-2. Sedam-RTPS-1 &2 lines
tripped at RTPS end only. 220kV Tandoor inter-state
line was hand tripped due to incoming supply failure
KPCL to disable GFC protection on all lines emanating from their
generating stations.
KPCL Yet to be informed Pending
57/II/3 Tripping of 400/220 kV ICT-2 at Raichur
TPS
07-07-2016 at
3:32 hrs
ICT-2 tripped on operation 400/220KV ICT-2 was
tripped on operation of 220KV side Instantaneous
over current protection during B-phase to earth fault
in 220kV RTPS-Sedam-II line.
KPCL to review appropriately the high-set of ICT‟s back-up O/C
protection at their 220 kV RTPS so that they do not operate for a
normal through fault.
KPCL Yet to be informed Pending
58/I/2 (GD) Complete outage of 220 kV Nagjheri PH
of KPCL.
31-08-2016 at
12:47hrs
Bus dead occurred at 220kV Nagjheri PH due to
tripping of evacuating lines.
(i) KPCL to disable high-set operation of DEF relays
(ii) KPCL to block DEF relays whenever corresponding distance
protection relays pick up at Kodasally end on Nagjheri – Kodasalli
lines, and
(iii)KPCL to provide stand-alone Event Logger at their 220 kV
Nagjheri PH.
KPCL Yet to be informed Pending
58/I/3 (GD)
Pending
PendingYet to be informed
KPCL In view of the availability of two buses along with healthy bus-
coupler at 220 kV RTPS, KPCL is recommended to put in service the
double-bus operation at 220 kV RTPS by suitably distributing loads
within 15 days.
Yet to be informedDuring testing of retrofitted distance protection in
400kV Raichur-2 feeder, LBB protection trip DC got
extended to Bus trip. This resulted in tripping of
220kV bus at RTPS and all connected 220 kV
elements. Unit-4 which is connected to 400 kV Bus
got tripped due to tripping of Station Utility
Transformer that is connected 220 kV bus
06-09-2016
at 14:40 hrs
31-05-2016 at
17:21 hrs
Direct Trip was sent from YTPS to RTPS and BTPS
01-05-2016 at
21:44 Hrs
LBB of 220kV Kodasalli breaker at Kadra end got
operated which resulted in tripping of Bus at Kadra
and in turn led to tripping of all elements
KPCL Yet to be informed
(i) KPCL to check settings of LBB protection in all relays from which
it was implemented, and ensure that their configuration, logic, and
timing are in order at their 220 kV Kadra PH.
(ii) KPCL to furnish details regarding the existing LT auxiliary
supply arrangement at their 220 kV Kadra PH, and take steps to
provide a suitable Auto-Main-Fail (AMF) panel for DG set to effect
its auto-starting in case of failure of LT supply.
(iii) KPCL to ensure time-sync of all relays (DR‟s & EL‟s) with GPS
at their 220 kV Kadra PH.
(iv) KPCL to provide stand-alone Event Logger at their 220 kV
Nagjheri PH.
KPCL
15-04-2016 at
15:36 hrs
1.KPCL to properly configure the distance relays at YTPS end on
both YTPS – BTPS line and YTPS-RTPS line with specific focus on
reaches and timings of Zone-2, Zone-3, and Zone-4 (reverse).
2.KPCL to ensure the healthiness of Direct Trip circuits and relay
coils at YTPS.
3.KPCL to ensure time sync of DR‟s and EL‟s at YTPS with GPS.
Pending
KPCL
Triggering incident was failure of R-phase CT of
400/220kV ICT-1. 400kV YTPS-RTPS line got
tripped from YTPS end. 400kV RTPS-
Mehaboobnagar line tripped on a B-phase to earth
fault.
1.KPCL to enable zero-sequence compensation feature, if not already
done, in all differential relays of transformers at RTPS.
2.KPCL to examine in detail the reasons for SOTF operation at RTPS
end for the fault on RTPS-Veltoor line, and if required relay
(configuration) settings at RTPS end may be suitably got revised with
the help of their OEM.
3.KPCL to take steps to enable auto-reclose for the Tie-CB‟s in the
dias containing Munirabad and Veltoor (Mehboobnagar) at RTPS.
Yet to be informed Pending
Tripping of Units at Raichur TPS 54/II/13
Tripping of 400kV Bellary TPS-
Yeramarus TPS line and
400kVYeramarus TPS - Raichur TPS
line
55/II/19
Multiple tripping at 400 kV Raichur TPS
Station
Complete outage of 220 kV Kadra power
station of KPCL
Annexure-II
Page 7 of 30
58/I/7 (GD) Complete outage at Varahi Hydro Power
Station
15-09-2016 at
14:06 hrs
LBB protection operated and caused bus shut down at
Varahi PH
(i) KPCL to check and correct configuration settings of LBB
protection in all relays from which it was implemented, at their 220
kV Varahi PH.
(ii) KPCL to provide stand-alone Event Logger at their 220 kV STR
PH.
KPCL Yet to be informed Pending
58/I/3 (GD)
58/I/5 (GD)
58/I/6 (GD) 12-09-2016 at
14:47 hrs
Yet to be informed Pending
(i) KPCL to adopt the following VT fuse-fail logic for all 220 kV
lines emanating from NPH:
“Under VT fuse fail condition, distance protection shall normally be
kept blocked. However, upon detection of a fault (sensed by negative
sequence component), blocking of distance protection shall give rise
to operation of its inherent Over-Current protection set with a definite
time delay of 500 msec”.
(ii) KPTCL/ KPCL to revise Zone-2, Zone-3 and Zone-4 (reverse)
timings of DPR of all 220 kV lines emanating from Nagjheri PH in
line with Ramakrishna Committee guidelines.
KPCL Yet to be informed Pending
Yet to be informed
Disturbance in Kerala system
06-09-2016
at 14:40 hrs
9-09-2016 at
11:19 hrs
LBB of 220kV Kodasalli breaker at Kadra end got
operated which resulted in tripping of Bus at Kadra
and in turn led to tripping of all elements
21-01-2017
at 00:38 hrs
KPCL
(i) KPCL to check settings of LBB protection in all relays from which
it was implemented, and ensure that their configuration, logic, and
timing are in order at their 220 kV Kadra PH.
(ii) KPCL to furnish details regarding the existing LT auxiliary
supply arrangement at their 220 kV Kadra PH, and take steps to
provide a suitable Auto-Main-Fail (AMF) panel for DG set to effect
its auto-starting in case of failure of LT supply.
(iii) KPCL to ensure time-sync of all relays (DR‟s & EL‟s) with GPS
at their 220 kV Kadra PH.
(iv) KPCL to provide stand-alone Event Logger at their 220 kV
Nagjheri PH.
KPCL
(i) KPCL to ensure the integrity of the connecting cable/ conductor
from Generating Unit-3 to its corresponding GT breaker at their STR
PH.
(ii) KPCL to ensure the healthiness of Manual Current Regulator
(MCR) of Unit-3‟s AVR at their STR PH.
(iii) KPCL to ensure the healthiness of AVR‟s of all Units of STR
PH.
(iv) KPCL to provide stand-alone Event Logger at their 220 kV STR
PH.
Complete outage of 220 kV Sharavathy
Tail Race PH
Partial disturbance occurred in central Kerala grid due
to overloading and tripping of 220 kV lines. Loss of in-
feed to 220 kV Kalamassery, 220 kV Brahmapuram,
220 kV Ambalamugal, 220 Pallom & 220 kV Kochi
occurred. Generation at Neriamangalam, Panniar,
Chengulam and Pallivasal also got affected during the
incident.
(i) SLDC, KSEB to put in place proper mechanism to ensure
adequate load-generation balance is maintained in their control area at
all times, and due vigilance is exercised in operating an already
depleted transmission network.
(ii) KSEB to put UFR in service at New Pallom end on 220 kV New
Pallom – Amabalamugal line as part of Kudankulam Regional
Islanding Scheme.
KPCL
Complete outage of 220 kV Nagjheri
substation of KPCL
PendingSpurious operation of LBB protection of line feeder
had led to tripping of 220 kV bus at Sharavathy Tail
Race power house.
PendingMail received on 27-05-2015 (KPTCL) & 29-07-2015:
1.Existing Back up relays will be replaced by numerical type distance
relays.Procurement is in tendering stage.
2. Completed.
3. Completed.
KPTCL Mail recieved on 23-01-2016:
1. Existing back up relays will be replaced by Main-2 protection. LOI
issued M/s Alstom for taking up the works.
KPTCL Mail Recieved dated 25-05-2016:
Under the Scope of R&U. The work will be taken up by M/s Alstom
shortly.
KPTCL Mail Recieved dated 25-04-2017:
1. ALSTOM make P442 type Numerical relays are supplied to the site,
replacement of M-1 relays(OPTIMHO) by new relays will be taken up
shortly
KPTCL1. PCSC forum recommended KPTCL to replace the old static
distance protection relays with numerical relays.
2. PCSC forum also requested KPTCL to provide a broken conductor
alarm indication in Control Room.
3. Standing instruction needed to be given to the all substation
personnel for not changing the relay settings without approval of
RT/MRT wing.
Fault had occurred in 220kV
Mahalingapura-Narendra line-2. Due to the failure of
relay operation at Mahalingapura, breakers at remote
end tripped which resulted in bus dead condition.
25-10-2014GD-1 at Mahalingapura Substation of
KPTCL
38/GD/3.1
Yet to be informed Pending
Triggering event was the fault on 220 kV Nagjheri
–Kodasalli line-2. Both buses of 220 kV Nagjeri
power station of KPCL got
de-energized.
62/I/1
Complete outage of 220 kV Kadra power
station of KPCL
Annexure-II
Page 8 of 30
220kV Sedam-
Tandur line
Line tripped on Yphase to earth fault from both the
ends
20-12-2014
at 22:20 hrs
40/IV/1 KPTCL was requested to explore the possibility of providing A/R
feature to this line and submit the remedial measures to the PCSC
forum.
Mail received on 27-05-2015 & 29-07-2015:
1. C&R panels of 500MVA ICT 1&2 will be replaced under scheduled
R&M works.
2. O&M personnel are instructed to take sufficient care in order to avoid
unwarrented trippings. --- Completed.
KPTCL mail received on 23-01-2016:
1. New C&R panels(with numerical relays) erected for 500MVA ICT-1
&2 under R&M work, which will be commissioned shortly.
KPTCL mail received on 25-05-2016:
1. New C&R panels(with numerical relays) erected for 500MVA ICT-1
&2 under R&M work, which will be commissioned shortly.
KPTCL mail received on 25-04-201:
1. New CRPs mounted in bay KIOSK commissioned under R&M works.
KPTCL1. PCSC forum recommended KPTCL to replace the relay with a
different make.
2. KPTCL was also requested to train the O&M personnel
adequately before performing any maintenance works to avoid such
unwanted trippings.
Suspected mal-operation of 220kV side Rphase
over current relay
01-12-2014Tripping of 400/220kV
ICT-2 at Hoody
substation of KPTCL
40/I/1 22-12-2014 at
21:22 hrs
Mail received on 28-04-2015:
1. In view of operating 220kV Ambewadi SS in split bus mode, action is
being taken up by KPTCL. Problem in the 220kV bus coupler breaker is
attended and isolator overhauling work is under progress. Spilt bus
operation at Ambewadi will be made possible at the earliest.
2. ICT Protection system at Ambewadi and trippings occured at Supa GS
during the instance is checked up and remedial measures already furnished
in this regard.
---- Completed
Mail recieved on 29-07-2015:
1. Action is being taken by KPTCL for operating Ambewadi in split bus
mode. Problem in bus coupler breaker is attended.Isolator overhaulling
work is completed.PTs are already provided to 220kV Bus-II. After
commissioning of Bus-II PTs, Ambewadi can be operated in split bus
mode. Pending works will be completed within a months time.
KPTCL mail recieved on 23-01-2016:
1. Bus-II PTs yet to be commissioned.Planned to complete before end of
April-2016.
KPTCL mail recieved on 25-04-2017:
1. Yet to be attended
39/I/5
1. Till the completion of R&M works for bus bar and LBB protection,
KPTCL shall explore the possibility of having split bus operation at
Ambewadi and submit the details of the same to PCSC forum.
2. KPTCL shall provide the details of the tripping of Supa hydro
station connected downstream from 110 kV bus.
Triggering incident was B-phase to earth fault in
220kV Ambewadi- Nagzari line-1. B-pole of breaker
did not open at Ambewadi end. LBB protection not
available at Ambewadi end. All elements tripped on
Zone-2 from remote ends.
Mail recieved on 29-07-2015:
Carrier protection is being restored for 220kV Sedam-Tandoor line at
Sedam end. After restoring the carrier protection , AR will be enabled.
KPTCL mail recieved on 23-01-2016:
Carrier protection is being restored for 220kV Sedam-Tandoor line at
Sedam end. After restoring the carrier protection , AR will be enabled.
KPTCL mail recieved on 25-05-2016:
SEE,SCADA to update the latest status
KPTCL mail recieved on 28-06-2016:
Action is being taken to restore carrier protection.AR will be enabled once
carrier signal is restored.
KPTCL
GD-1 at 220kV Ambewadi Station of
KPTCL
Pending
Pending
Pending
KPTCL
Annexure-II
Page 9 of 30
Tripping of Unit-1&2
along with 400/220kV
ICT-2 at Raichur TPS
1. KPTCL shall provide A/R feature on Ambewadi – Ponda 220 kV
D/C inter-state line.
2. Till the completion of R&M works for bus bar and LBB protection,
KPTCL shall explore the possibility of having split bus operation at
Ambewadi and submit the details of the
same to PCSC forum.
47/II/13
48/I/2 (GD) Complete outage of 220kV Peenya
Substation in Karnataka
42/I/1 (GD) Fault occurred in 220kV Sedam-Shahpur line
41/I/4
06-08-2015 at
4:51 hrs
Yet to be informed
Pending
1. KPTCL to provide Bus Bar protection and LBB protection at
Sedam S/s and furnish the status of their implementation to PCSC
forum.
2. KPTCL to implement A/R feature on 220 kV Sedam-Tandur inter-
state line.
15-02-2015 at
14:24 hrs
220kV RTPS-Lingasugur line-2 tripped at TPS end
on operation of distance
protection zone-1. 400/220kV ICT-2 got tripped on
operation of earth fault
protection. 220kV RTPS-Lingasugur line-1&3 tripped
on distance protection zone-2 and zone-3
respectively. Due to tripping of ICT-2, the running
units got overloaded and it was mentioned that under
frequency occurred as units are on load control. The
Units got tripped on under frequency.
27-01-2015 at
8.00 hrs
Mail received on 27-05-2015:
1. Bus Bar protection will be provded under R&U.
2. A/R yet to be enabled.
Mail received on 29-07-2015:
1. Procurement of Bus bar and LBB protection is in the final tendering
stage.
2. Action is being taken to restore the carrier protection for 220kV Sedam-
Tandoor line. AR will be enabled after restoration of PLCC.
Mail received on 28-04-2015:
Procurement of Bus bar and LBB protection is in the final tendering stage.
2. Action is being taken to restore the carrier protection for 220kV Sedam-
Tandoor line. AR will be enabled.
Mail received on 29-07-2015:
1. Procurement of Bus bar and LBB protection is in the final tendering
stage.
2. Action is being taken to restore the carrier protection for 220kV Sedam-
Tandoor line. AR will be enabled after restoration of PLCC.
KPTCL mail received on 23-01-2016:
1. Bus bar protection panels pocured and erected at Sedam. Wiring ,
testing ,commissioning is being taken up.Planned to complete by April
2016.
2. Action is being taken to restore the carrier protection for 220kV Sedam-
Tandoor line. AR will be enabled after restoration of PLCC.
KPTCLR-Phase to ground fault occurred on 220kV Sedam-
Shahpur line. Fault not cleared from Sedam end due
to stuck-breaker condition. While the Sedam- Sahapur
line tripped from Shahapur end in Zone-1, the other
220 kv lines from Sedam tripped at remote ends in
Zone-2. This caused complete outage of 220kV
Sedam substation.
Complete outage at 220kV Sedam
Substation of KPTCL (GD-1)
12-03-2015 at
7:51 hrs
Complete outage of 220kV Sedam
substation of KPTCL
KPTCL mail received on 25-05-2016:
Presentl 220kV Nelamangala -Hoody(i.e. nelamangala-Peenya-Hebbal -
Hoody line is made LIILO at Yelahanka sub station and breaker at
Peenya is kept open, necessary modification in distance relay settings
adopted for new configuration.
KPTCL to activate non-directional Over Current protection with a
time delay of 600-800 msec for Fuse
failure condition at Lingasugur.
Mail received on 29-07-2015:
1. Procurement of Bus bar and LBB protection is in the final tendering
stage.
2. Action is being taken to restore the carrier protection for 220kV Sedam-
Tandoor line. AR will be enabled after restoration of PLCC.
All connected 220kV lines and transformers were
taken on 220kV North bus as South bus was under
shut down for conversion of strung bus to rigid bus
and isolator replacement under R&M works. Failure
of HV side Y phase CT of 150MVA Transformer-3
occurred at Peenya Substation which resulted in
operation of Differential and HV REF protection. The
failure of CT also resulted in a 220kV bus fault in
North Bus.
KPTCL to revise distance relay settings at Nelamangala end for 220
kV Nelamangala – Hebbal - Peenya line – 1 for the effective line
length of 17 km. These new settings can be appropriately reviewed as
and when the tie-arrangement at Hebbal is done away with.
PendingComplete outage of 220kV Ambewadi
substation of KPTCL
Pending
42/I/2 (GD)
27-09-2015 at
4:23:17 hrs
Fault in 220kV Ambewadi-Nagjheri line-2
KPTCL
KPTCL
KPTCL
Pending
Pending
1. KPTCL to provide Bus bar and LBB protections for 220 kV
bus at Sedam S/s.
2. KPTCL to implement A/R feature on 220 kV Sedam-Tandur
inter-state line.
KPTCL
Annexure-II
Page 10 of 30
52/I/3 (GD) Complete outage of 220kV Shimoga
substation
22-02-2016 at
15:03 hrs
220kV Bus Bar protection operated during failure of
R phase CT in DVG-2 line bay.
KPTCL to operate 220 kV Shimoga on multi-bus operation under
normal conditions, put it on single-bus operation only under
emergency conditions.
KPTCL KPTCL Mail received dated 25-04-2017:
Replacement of existing BBP by new BBP with 4 zone protection is being
taken up under R&U.
Pending
56/II/6 Tripping of 220kV Ambewadi-Ponda
(Xeldam) line-1
10-06-2016 at
13:33 hrs
Line tripped on Y-E faut due to DPR, Z1 operation KPTCL to keep A/R for Ambewadi – Ponda (Xeldam) line-1 in
service with immediate effect.
KPTCL Yet to be informed Pending
48/I/3 (GD) 30-09-2015 at
10:41 hrs
KPTCL to fast-track providing A/R on all 220 kV lines emanating
from Ambewadi SS to prevent Station shut-down on temporary faults.
Failure of Lightning Arrestor of Y-phase Line Reactor
of 400kV Guttur-Hiriyur line-1 and line tripped on
distance protection Zone-1. Bus-bar protection of
400kV Bus-2 at Guttur substation also got operated
during the event sensing this through fault. 400/220
kV ICT-1 & 2 at Guttur, 400kV Kaiga-Guttur-2,
400kV
Guttur-Narendra-2, 400kV Guttur-Hiriyur-2 and
400kV Guttur-Munirabad which are on 400kV Bus-2
got tripped during the incident. 400kV Guttur-
Narendra-1 which was on Bus-1 also tripped at the
same time.
Multiple tripping at 400kV Guttur sub-
station
17-01-2016 at
18:53 hrs
Tripping of 220 kV Chikkodi-Mudshingi
and 220 kV Chikkodi-Talandage lines
51/II/21 1. KPTCL to configure all DR‟s and EL‟s at 400 kV Guttur SS so
that they will also get triggered for BBP operation.
2. KPTCL to ensure time-synchronization of all DR‟s and EL‟s with
GPS at their 400 kV Guttur SS.
KPTCL mail received on 23-01-2016:
Will be complied in a months time.
57/II/1
Complete outage of 220kV Peenya
Substation of KPTCL
49/I/1.3 (GD)
53/I/1
KPTCL Mail received dated 25-05-2016:
SEE, RTC, Bangalore to update the status
KPTCL Mail received dated 28-06-2016:
Providing numerical bus bar protection to 400kV buses and GPS time
synchronising equipment at Guttur is considered under R&U. Work is
awarded to M/s Alstom, execution will be taken up shortly.
KPTCL Mail received dated 25-04-2017:
GPS and accessories will be supplied during May 2017, expected to
complete the work within a month after supply of materials
1. KPCL to provide A/R on all 220 kV lines emanating from Nagjheri
PH.
2. KPTCL to provide A/R on all 220 kV lines emanating from
Ambewadi SS.
220kV Nagjheri-Ambewadi line-1 tripped at 13:33
hrs due to B phase to earth fault. Ambewadi was
radially fed from Nagjheri power station through
220kV Nagjheri-Ambewadi line-2. Tripping of this
line caused 220kV Bus shut down at Ambewadi and
remaining lines and transformers were hand tripped
220kV Ambewadi-Nagjheri line-2 tripped on B-phase
to earth fault. This resulted in loss of supply to 220kV
Ambewadi bus. 220kV Ambewadi-Ponda line-1&2
were hand tripped after deenergization of bus at
Ambewadi.
Complete outage of 220kV Ambewadi
Substation of KPTCL
KPTCL PendingOutage of 220kV Ambewadi station in
Karnataka
Pending
Triggering incident was failure of B-ph PT of 220kV
Bus-2 (western bus) at 220KV Chikkodi substation.
220KV Chikodi- Belgaum-I line tripped on DEFR
(Inst), 220KV Chikkodi-Kudachi line tripped on
Distance protection and also 100MVA transformer-2
tripped on E/F protection.
29.10.2015 at
14:34 hrs
Pending
Pending16-03-2016 at
11:39 Hrs
KPTCL
Yet to be informedKPTCL
220kV Peenya-Nelamangala-3 tripped on B-E fault at
both ends. At the same time, 220kV Peenya-
Nelamangala-4 tripped on R-Y fault only at
Nelamangala end, and was in service from Peenya
end. Due to tripping of these two lines, 220kV Peenya-
Nelamangala-2 tripped on overcurrent protection.
KPTCL to furnish a report on the tripping of 220 kV Peenya-
Nelamangala line-4 Nelamangala detailing the remedial measures
taken including the settings adopted for Z1B (Zone extension) and
Power Swing Block.
01-07-2016 at
03:03 hrs
KPTCL Mail received dated 25-05-2016:
SEE, RTC, Bangalore to update the status
KPTCL
KPTCL Yet to be informed Pending1.KPTCL to take steps to provide busbar protection at their 220 kV
Chikkodi inter-regional substation, and furnish a time-line for the
same.
2.KPTCL to review distance protection settings for 220 kV Chikkodi
– Kudachi line.
3.KPTCL to furnish equipment failure report of the current incident to
PSE&TD Division of CEA with a copy marked to SRPC.
Annexure-II
Page 11 of 30
59/II/13 Tripping of 220 kV Bidadi (PG) - Bidadi
lines - 1&2
02-10-2016 at
10:32 hrs
Line-2 tripped in DPR, Zone-2 and Line-1 tripped on
operation of E/F protection from Bidadi end.
KPTCL to resolve PLCC carrier communication issues on 220 kV
Bidadi – Bidadi-PG D/C lines, and subsequently restore Zone-2
timing to normal values.
KPTCL Yet to be informed Pending
62/II/3 Tripping of 220 kV Bus 2 and connected
elements (220kV HAL #1 and 2,
400/220 kV ICT- 1, 2 and 220/66 kV
ICT-2) at 400/220 kV Hoody substation
of KPTCL (Load loss : 590 MW)
09-01-2017 at
23:06 hrs
Failure of R-phase CT of 220/ 66 kV transformer-2 at
220kV Hoody end resulted in a bus fault in 220kV
Bus-2. Fault was cleared by backup protection of
ICT's (220kV lines were being radially operated) due
to absence of busbar protection
1. KPTCL to provide Busbar protection at their 220 kV Hoody SS at
the earliest.
2. KPTCL to furnish an Equipment Failure Report on CT failure to
CEA with a copy marked to SRPC.
KPTCL KPTCL mail received dated 25.04.2017:
Numerical BBP is being provided under R&M works
Pending
59/IV/4 Tripping of 400 kV Guttur-Hiryur line-1 10-10-2016 at
3:15 hrs
Line tripped at Hiryur end due to direct trip receive
and was holding from Guttur
For the line under consideration, the following shall be carried out by
KPTCL in coordination with
PGCIL (SR-II):
(i) End-to-end communication for DT/ permissive & other signals
may be ensured by testing at both the ends.
(ii) Healthiness of PLCC system components (hardware and software)
at both ends shall be checked and faulty components shall be repaired/
replaced.
KPTCL
Tripping of 400 kV Neelamangala-
Hoody line-1
62/IV/4 KPTCL Yet to be informed Pending
Complete outage of 220kV Nagjheri
power station and 220kV Ambewadi
substation of KPTCL
Tripping of 220 kV Chikkodi-Mudshingi
and 220 kV Chikkodi-Talandage lines
51/I/3
62/II/5 Tripping of 220 kV South Bus and
connected elements (220kV HSR, 220kV
Nagnathpura, 220 kV Harohalli, 220 kV
Subramanyapura, 220 kV Tataguni, 220
kV Mallur and 400/220kV ICT-2 and 3)
at 400/220kV Somanhalli substation of
KPTCL
(Load loss: 850 MW)
20-01-2017 at
14:34 hrs
Triggering incident was fault in 66 kV Somanahalli -
Bannerghatta line and fault was cleared by operation
of Back-up OCR at Somanahalli end.
KPTCL to provide numerical Busbar Protection at their 220 kV
Somanahalli SS at the earliest.
KPTCL to carry out the following for the line under consideration:
(i) Healthiness of PLCC system components (hardware and software)
at both ends shall be checked and faulty components shall be repaired/
replaced.
(ii) End-to-end communication for DT/ permissive & other signals
may be ensured by testing at both the ends.
Line tripped at Hoody end on direct trip receive and
was holding from Neelamangala end.
15-02-2017
at 13:44 hrs
57/II/1 Triggering incident was failure of B-ph PT of 220kV
Bus-2 (western bus) at 220KV Chikkodi substation.
220KV Chikodi- Belgaum-I line tripped on DEFR
(Inst), 220KV Chikkodi-Kudachi line tripped on
Distance protection and also 100MVA transformer-2
tripped on E/F protection.
Yet to be informed Pending
KPTCL mail received dated 25.04.2017:
Numerical BBP is being provided under R&M works
PendingKPTCL
KPCL/ KPTCL
01-07-2016 at
03:03 hrs
Status informed during Special Meeting held on 03.06.2016:
1. KPTCL informed that the matter had been taken up with concerned Line
Operation and Maintenance wing to carry out corridor clearance and
maintenance as per schedule to avoid frequent line faults in this corridor. A
letter had also been addressed to Chief Engineer, Bhagalkot zone, to ensure
lines in & around Kali complex are maintained in healthy condition. ---
Completed
2. KPTCL assurd that the final modified SPS would be implemented at
Nagjheri PH at the earliest. ------ Pending
3. KPCL informed that Nagjhari- Kodasalli Lines 1 & 2 had been kept in
service since 23.05.2016 @ 08.06hrs. ---- Completed
KPTCL Mail received dated 28-06-2016:
Modifications to be carried in Nagzari SPS logic is submitted to
SRLDC/SRPC for verification and approval
220kV lines from Nagjheri power house started
tripping from 11:00 hrs due to fault in lines. The
sequence of tripping is shown in SOE list. At 12:33
hrs, 220kV Narendra-Ambewadi lines-1&2 got
tripped which resulted in loss of evacuation path to
Nagjheri station resulting in tripping of running Units
and complete outage at Nagjhheri power station.
220kV Ambewadi station also got de-energized due
to tripping of source feeders i.e. 220kV Narendra-
Ambewadi-1&2 and 220kV Nagjheri-Ambewadi-
1&2.
22-02-2016 at
12:36 hrs
Pending
KPTCL Yet to be informed Pending
1. To avoid tripping of transmission lines on transient faults, KPCL/
KPTCL is recommended to carry out periodic patrolling of lines, and
ensure their proper maintenance by carrying out jungle/ bushing
clearance and trimming of tree branches within the RoW of
transmission lines as per the SRPC transmission line patrolling
guidelines (available under the menu item "All Uploads Operation
Miscellaneous Transmission Line Patrolling Protocol /
Guidelines for Southern Region" on SRPC website).
2. KPCL/ KPTCL to review operation of SPS at NPH for
functionality (reduction of generation with tripping of evacuating
lines) and healthiness.
3. KPCL to put 220 kV Kodasalli - Nagjheri D/C lines into service if
more than 200 MW generation from Kali Complex (with Nagheri
Contribution not less than 50 MW) is ensured on sustained basis.
1.KPTCL to take steps to provide busbar protection at their 220 kV
Chikkodi inter-regional substation, and furnish a time-line for the
same.
2.KPTCL to review distance protection settings for 220 kV Chikkodi
– Kudachi line.
3.KPTCL to furnish equipment failure report of the current incident to
PSE&TD Division of CEA with a copy marked to SRPC.
Annexure-II
Page 12 of 30
56/I/3 Complete outage of 220kV Ambewadi
Substation of KPTCL.
24-06-2016 at
20:57hrs
B phase to earth fault had occurred in 220 kV
Ambewadi-Ponda line-2. Fault was cleared by
tripping of feeders from remote end
1.KPCL & KPTCL to furnish an action taken report on the
recommendations given by PSAG-16 to PCSC forum.
2.KPTCL to keep A/R for Ambewadi – Ponda line-2 in non-auto
mode (i.e., only 3-ph trip should get extended on occurrence of a
fault) till the line is closed from Ponda end.
KPCL/KPTCL Yet to be informed Pending
62/V/3 TANTRANSCO mail dated 12.04.2017:
1. The recommendation will be ensured. AR logic will be configured in
Distance Protection relay itself instead of BCU. OEM has been addressed.
2. Post triggering period of 2 sec. to cover AR operation in DR time scale
will be provided.
Pending
1. TANGEDCO to replace existing Check-Zone relay with a new one
possessing required performance.
2. TANGEDCO to take steps to provide numerical busbar protection
at their 220 kV Tuticorin TPS. TANGEDCO may also explore
providing dual CT‟s (on either side) for all B/S breaakers at the time
of commissioning of numerical BBP, if there were no space
constraints.
3. TANGEDCO to take steps to provide for standalone Event Logger
(EL) and standalone Disturbance Recorder (DR) with automatic
downloading facility to a centralized server.
Failure of Bus Section-I Y-ph CT resulted in
operation of bus-bar protection for Bus Sections -I &
II. Running Units#1, 4 and 5, 230 kV Kayathar,
230kV Kudankulam, 230kV Sterlite, Station
Transformer-1, 2 & 3 got tripped during the incident.
Unit – 2 & 3 were not in service.
25-01-2017 at
22:36 hrs
Tripping of running Units & 230kV
feeders at Tuticorin TPS of TANGEDCO
(Gen Loss: 640 MW)
62/II/7 TANGEDCO TANGEDCO mail dated 15.04.2017:
1) New Relay is tested and ready for replacement.Now all 5 units are in
service.The relay will be replaced when lesser units are in service. ---
Pending
2.a)Steps are taken to renovate & mordernization of all the control panel
into Numerical based control panels. --- Pending
2.b) Since 230 KV indoor switchyard has no spare space providing dual
CT`s is not fessible. -- Completed
3) Procurement of EL & DR is under progress. --- Pending
Pending
KPTCL Mail Recieved dated 25-05-2016:
SEE,SCADA to update the status of healthiness of carrier protection of
220kV RTPS-Raichur 1 &2 lines
KPTCL Mail Recieved dated 28-06-2016:
Details sought from KPCL for review of ICT's back up (high set) proection
settings as suggested. KPCL is yet to furnish the details required to give
the revised settings.
Tamil Nadu
Complete outage of 220kV Ambewadi
station of KPTCL and 220kV Nagjheri
of KPCL
15-03-2016 at
12:28 hrs
ICT-3 tripped due to operation of back-up earth fault
protection during fault in 220kV RTPS-Raichur line-
1.
KPCL/KPTCLKPCL/ KPTCL to check the ICT‟s back-up (high-set) protection
settings, and ensure that they operate with a time delay of 100 msec.
Tripping of ICT-3 at Raichur Substation
KPTCL Mail received dated 28-06-2016:
Modifications to be carried in Nagzari SPS logic is submitted to
SRLDC/SRPC for verification and approval
1. KPCL to furnish a report on the reasons for Unit-6 tripping at
Nagjheri PH.
2. KPCL/ KPTCL to modify suitably the SPS at Nagjheri Power
House such that it would also factor in the over loading of Ambewadi-
Narendra lines.
3. KPCL to put 220 kV Kodasalli - Nagjheri D/C lines into service if
more than 200 MW generation from Kali Complex (with Nagheri
Contribution not less than 50 MW) is ensured on sustained basis.
1. TANGEDCO to take properly configure A/R logic at NCTPS-II in
that in case of unsuccessful auto-reclsoure, three-phase trip shall be
given along with A/R block.
2. TANGEDCO to configure all protection relays DR‟s time scale at
NCTPS-II for a post-triggering period of 2 sec to capture events such
as complete A/R operation.
R-phase to earth fault due to de-capping of insulator.
Auto-reclose attempt was unsuccessful.
22-02-2017 at
06:16 hrs
Tripping of 400 kV NCTPS-
S.V.Chatram line-2
Pending
Complete outage of 220kV Nagjheri
power station and 220kV Ambewadi
substation of KPTCL
51/I/3
53/I/3 (GD) Ambewadi Narendra line-2 tripped on fault and
220kV ambewadi Narendra line-1 tripped due to over-
loading. Running Units at Nagjheri also tripped during
the event due to tripping of evacuating lines
KPCL/ KPTCL Status informed during Special Meeting held on 03.06.2016:
1. KPTCL informed that the matter had been taken up with concerned Line
Operation and Maintenance wing to carry out corridor clearance and
maintenance as per schedule to avoid frequent line faults in this corridor. A
letter had also been addressed to Chief Engineer, Bhagalkot zone, to ensure
lines in & around Kali complex are maintained in healthy condition. ---
Completed
2. KPTCL assurd that the final modified SPS would be implemented at
Nagjheri PH at the earliest. ------ Pending
3. KPCL informed that Nagjhari- Kodasalli Lines 1 & 2 had been kept in
service since 23.05.2016 @ 08.06hrs. ---- Completed
KPTCL Mail received dated 28-06-2016:
Modifications to be carried in Nagzari SPS logic is submitted to
SRLDC/SRPC for verification and approval
KPCL/ KPTCL18-03-2016 at
14:40 hrs
220kV lines from Nagjheri power house started
tripping from 11:00 hrs due to fault in lines. The
sequence of tripping is shown in SOE list. At 12:33
hrs, 220kV Narendra-Ambewadi lines-1&2 got
tripped which resulted in loss of evacuation path to
Nagjheri station resulting in tripping of running Units
and complete outage at Nagjhheri power station.
220kV Ambewadi station also got de-energized due
to tripping of source feeders i.e. 220kV Narendra-
Ambewadi-1&2 and 220kV Nagjheri-Ambewadi-
1&2.
22-02-2016 at
12:36 hrs
Pending
Pending
TANGEDCO
1. To avoid tripping of transmission lines on transient faults, KPCL/
KPTCL is recommended to carry out periodic patrolling of lines, and
ensure their proper maintenance by carrying out jungle/ bushing
clearance and trimming of tree branches within the RoW of
transmission lines as per the SRPC transmission line patrolling
guidelines (available under the menu item "All Uploads Operation
Miscellaneous Transmission Line Patrolling Protocol /
Guidelines for Southern Region" on SRPC website).
2. KPCL/ KPTCL to review operation of SPS at NPH for
functionality (reduction of generation with tripping of evacuating
lines) and healthiness.
3. KPCL to put 220 kV Kodasalli - Nagjheri D/C lines into service if
more than 200 MW generation from Kali Complex (with Nagheri
Contribution not less than 50 MW) is ensured on sustained basis.
53/II/1
Annexure-II
Page 13 of 30
Disturbance in 220kV Tamilnadu system
43/II/5 Tripping of 400kV
Alamathy-
SVChatram line-1&2
and 400/230kV ICT
at S.V.Chatram
TANTRANSCO TANTRANSCO vide their mail dated 24.06.15 informed that different
relays in Main-I & Main-II would be ensured at the earliest.
Mail recieved on 24-07-2015 ,19-02-2016 and 24-03-2016:
Different relays in Main-I & Main-II will be ensured.
Mail received on 27-04-2016:
TANTRANSCO: Not feasible in the existing SAS sub stations. Hence,
exemption may be given for these sub stations.
Mail received on 20-05-2016 ,16-06-2016,25-07-2016 & 24-09-2016 :
As discussed in the 52nd PCSC meeting, Swapping of Relays between two
stations is not feasible in the existing SAS sub stations. Hence, exemption
may be given for these sub stations.
Status received vide mails received on 10-11-2016 & 20.12.2016 &
12.04.2017:
Different make Relays will be ensured for Main-I & II relays at Alamathy
end.
Pending29-03-2015 at
15:29 hrs
Line-2 tripped on R-phase to earth fault.
Line autoreclosed at SVChatram end and failed to
reclose at Alamathy end. Bphase to earth fault in line-
1. Line tried for A/r but due to permanent fault line
did not reclose. ICT tripped on operation of over flux
protection.
TANTRANSCO was requested to swap the relays between two
stations, so that
Main-1 and Main-2 will be of different make at each station.
Complete outage of 230kV Palladam, 230 kV
Othakalmandapam S/s, 230 kV Coimbatore S/s, 230
kV Thudialur and 230 kV Sadayapalayam S/s
05-09-2015 at
14:04 hrs
TANTRANSCO to take suitable measures like installing more stub-
towers along 230 kV OK Mandapam – Myvady line to avoid
excessive sag due to over-loading.
TANTRANSCO Mail received on 19-02-2016, 24-03-2016 and 27-04-
2016:
230kV Othakalmandapam - Myvadi feeder will be made LILO at Kongal
Nagar. Line restringing will be carried out along with the above proposal.
Mail Received on 20-05-2016 ,16-06-2016,25-07-2016 & 24-09-2016:
230kV Othakalmandapam - Myvadi feeder will be made LILO at Kongal
Nagar. Line restringing will be carried out along with the above proposal.
Status received vide mails received on 10-11-2016 & 20.12.2016 &
12.04.2017:
230kV Othakalmandapam - Myvadi feeder will be made LILO at Kongal
Nagar. Line restringing will be carried out along with the above proposal.
TANTRANSCO48/I/1 (GD) Pending
Annexure-II
Page 14 of 30
Complete outage of 230 kV
Gummidipoondi Station of TANTRANSCO
Complete outage of 230kV Mywadi
station of TANTRANSCO
50/I/3 (GD)
The issue was discussed in PCSC-58 meeting held on 18.10.2016, when
PCSC forum agreed to de-link the implementation of the Item from the
scope of Protection Audit Recommendations (PAR), and pursue it as part
of PCSC Recommendations.
Status received vide mails dated 10.01.2017 & 12.04.2017:
Different make Relays will be provided for Main-I & II relays at
Sunguvarchatram end in a phased manner.
PendingTANTRANSCODifferent type and Make of distance protection relays to be provided for Main-I & Main-II protection for 230kV feeders at 400 kV Sunguvarchathiram & 230 kV Sunguvarchathir