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75 MW Turbine-Generator Journal-Thrust Bearing Upgrade Julia Postill, PE TCE/Turbo Components & Engineering Houston, Texas Boris Drigant Lansing Board of Water & Light, Lansing, Michigan

75MW Steam Turbine Journal Thrust Bearing Upgrade

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Page 1: 75MW Steam Turbine Journal Thrust Bearing Upgrade

75 MW Turbine-Generator Journal-Thrust Bearing Upgrade

Julia Postill, PETCE/Turbo Components & Engineering

Houston, Texas

Boris DrigantLansing Board of Water & Light,

Lansing, Michigan

Page 2: 75MW Steam Turbine Journal Thrust Bearing Upgrade

ABSTRACT

This case history discusses the upgrade of the #1 combination journal-thrust bearing assembly in the front standard of a 75 MW turbine/generator set. The existing taper land thrust plates experienced frequent failures and the sleeve journal bearing was wearing prematurely. A combination journal-thrust assembly was designed and installed in the front standard of the turbine. This assembly incorporated fully equalized ball & socket tilting pad thrust bearings with directed lubrication and a ball & socket tilting pad journal bearing. The spherical support fit was replaced by a cylindrical support fit. The ring saddle supporting the journal housing was redesigned to be bolted to the thrust housing.

Page 3: 75MW Steam Turbine Journal Thrust Bearing Upgrade

The Turbine-Generator Train

Page 4: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Turbine – Front Standard

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Bearing description:

The original bearing is a combination journal-thrust, with compound taper plate thrust bearings, and a sleeve liner for the journal bearing. The thrust bearing assembly is overhung. The thrust housing is bolted to the journal bearing housing which is spherically fitted inside a saddle ring, supported by four OD pads with adjustment shims underneath.

Page 6: 75MW Steam Turbine Journal Thrust Bearing Upgrade

OEM bearing assembly without the thrust bearings

Thrust cavitySpherical fit

Sleeve journal bearing

Saddlering

Journal brg.Housing

Thrusthousing

Page 7: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Problem:The original bearings had unsatisfactory resistance to the loads, the misalignment, and the lack of effective axial movement of the front standard. Due to erosion of the sliding supports, the supports could not slide and the front standard would not properly align with the shaft. This resulted in numerous failures of the thrust and journal bearings and forced outages. The spherical fit of the bearing housing assembly did not help with the alignment. Due to alignment concerns, the journal bearing was set low, so the bearing was lightly loaded which resulted in oil whirl and oil whip, damaging the journal bearing and the shaft.

Page 8: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Damaged journal bearing

Page 9: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Active Thrust Plate with light wear and major failure.

Page 10: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Solution:A combination journal-thrust assembly was designed and installed in the front standard of the turbine. This assembly incorporated fully equalized ball & socket 56% offset pivot tilting pad thrust bearings with directed lubrication, a ball & socket tilting pad journal bearing, and a new saddle ring. The new saddle ring has a cylindrical fit for the journal bearing assembly, and it is bolted to thrust housing. This allows much simpler settings, installation, and maintenance of the whole assembly.

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Upgraded Bearing Assembly

New Saddlering

Inactive thrustbearing

Active thrust bearingJournal

bearing

Modified thrusthousing

Page 12: 75MW Steam Turbine Journal Thrust Bearing Upgrade

New design assembly drawing

Page 13: 75MW Steam Turbine Journal Thrust Bearing Upgrade

Photograph of upgraded Bearing Assembly

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The active thrust bearing after 6 years in service.

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The inactive thrust bearing after 6 years in service

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The journal bearing loaded pads, after 6 years in service.

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Conclusion:

The solution was implemented in one unit in 2000, and has run successfully with only scheduled maintenance. Same solution was implemented in two more similar units and one 170 MW unit after that.