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Paraffin Blockage Remediation In A Flexible Flowline Robert James Production Engineer

2015 Deepwater Operations_Murphy_FINAL

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Page 1: 2015 Deepwater Operations_Murphy_FINAL

Paraffin Blockage Remediation In A Flexible Flowline

Robert JamesProduction Engineer

Page 2: 2015 Deepwater Operations_Murphy_FINAL

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Outline

• Background • Remediation• Execution• Lessons Learned

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Background

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Medusa SS#5 Infrastructure

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Flow Assurance Challenges

• Uninsulated flowline• Pigging operations unavailable• Water injection tree

– Limited chemical injection points• Assumed similar fluid characteristics to offset well

– No down-hole samples obtained

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Medusa SS#5 HistoricalInitial Production

Snubbing Clean-out Operation

Paraffin Plug In Flowline

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Flowline Deposition

Bottom-hole Pressure

Boarding Pressure

Tubing Pressure

Subsea Flowline Pressure

Time Period Shown: 4 Years

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Remediation

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Remediation Options

Paraffin Deposition

Bullhead Solvent

Coil Tubing Cleanout

Snubbing Unit Cleanout

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Bullhead Operation

• Pumped 1000 gals of Xylene down flowline from platform• Impermeable paraffin blockage formed

Subsea Flowline Pressure

Boarding Pressure

Time Period Shown: 5 Months

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Remediation Options

Paraffin Deposition

Bullhead Solvent

Paraffin Blockage Formed

Coil Tubing Cleanout

Snubbing Unit Cleanout

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Coil Tubing

• Advantages– Circulation– Direct solvent

application to blockage• Disadvantages

– Potential for stuck work string

• Tractoring technology in horizontal section risky

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Remediation Options

Paraffin Deposition

Bullhead Solvent

Paraffin Blockage Formed

Coil Tubing Cleanout

High Potential For Stuck

Work String

Snubbing Unit Cleanout

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Snubbing Unit

• Advantages– Rotation capability– Circulation– Direct solvent

application to blockage– Proven industry method

• Risks– Flexible flowline integrity– Maneuverability of

curvature in flowline

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Flowline Curvature Risk - Mitigation

• Torque and drag modeling shows snubbing unit capable of operating through bend in flowline.

• Provided parameters while running in hole with work string.

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Solvent Selection• Solvent Selection:

– Diesel• HSE • Disposal• Cost Effective

– Effectiveness of diesel circulation in question at lower temperatures

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Mechanical Remediation

• Pipe in pipe modeling completed– Significant heat loss

expected • Removal of paraffin

using 3” O.D. brass nozzle

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Remediation Options

Paraffin Deposition

Bullhead Solvent

Paraffin Blockage Formed

Coil Tubing Cleanout

High Potential For Stuck Work

String

Snubbing Unit Cleanout

Execution

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Execution

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Operations SpreadSnubbing Unit

Circulation/Flowback

Heated Tanks

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Continuous Monitoring

• Snubbing parameters:– Pick Up and Slack Off Weights– Torque

• Diesel parameters:– Pour Point– Viscosity– Density

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Operational Results

Subsea Flowline Pressure

Tubing Pressure

Boarding Pressure

Time Period Shown: 3 Months

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Operational Results

• Well Test Recorded After Clean-Out• 1381 BOPD, 1223 MCFD, 213 BWPD

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Lessons Learned

• Job Execution – Accurate modeling– Multiple remediation options– Real-time monitoring

• Field Development– Accurate data acquisition– Appropriate infrastructure

• Insulation Requirements• Chemical application

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Acknowledgements

• David Mayfield• Alyce Anfang

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Contact Information

• Robert James• Murphy Oil Corporation• [email protected]• 832-319-5443

Questions?