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THE SWEDISH CLUB CASEBOOK 10 Machinery failure THE SWEDISH CLUB CASEBOOK

10 · 2021. 2. 2. · l The turbo charger revolutions had dropped from about 14,500 rpm to 12,000 rpm at 85% load as had the charge air pressure from 1.7 bar to 1.2 bar. These changes

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  • THE SWEDISH CLUB CASEBOOK

    10Machinery failure

    THE SWEDISH CLUB CASEBOOK

  • THE SWEDISH CLUB CASEBOOK

    10

    A vessel was in ballast and at anchor, awaiting furtherinstructions. After seven days the weather deterioratedand the vesseĺ s anchor dragged. The anchor washeaved up and the vessel started to slow steam in thearea. After about 24 hours the differential pressure alarmof the main engine duplex lubrication oil filter sounded inthe engine control room. The crew found aluminium andother metal inside the lubrication filter, and in thecrankcase of the main engine, metal particles werefound.

    Serious damage to the main engine

    The subsequent investigation alongside revealed that themetal particles found in the lubrication oil filtersemanated from piston rings and piston skirts. Threepistons had almost seized. The main engine, a six-cylinder medium speed type, had severe damage and thefollowing parts had to be renewed: all cylinder liners,three complete pistons, piston rings on all cylinders, allmain and connecting rod bearings.

    In addition, the turbo charger had to be overhauled as thenozzle ring was broken. The complete lubrication systemhad to be carefully cleaned and flushed. The vessel wasoff hire for almost two weeks.

    The pistons in cylinder units no.1 and 3 were melteddown in certain areas and the skirt in no.4 was torn.Liners were scuffed as a result of the above. The cylinderlubrication channels were found clogged and so cylinderlubrication had been inactive. The lubrication oil pumpwas found deteriorated due to the hard impurities in thelube oil system.

    Lubrication oil contaminated for some time

    It was obvious that the engine had been operated on ahigh thermal load for a long time and that theturbocharger efficiency had been affected by fouling. Thelubrication oil had actually been contaminated for sometime.

    There had been indications that something had gonewrong, for example it was written in the log book that theauto filter had been shooting up to 609 times a day.

    10.1 Machinery failure caused by contamination

  • THE SWEDISH CLUB CASEBOOK

    What can we learn?A first step to avoiding damage is to have alwell implemented and proper managementsystem. This implementation can only beassured with proper training and educationfor the crew and providing them with theessential knowledge and experience requiredfor ordinary daily work and maintenanceaccording to company procedures.

    Always take engine alarms seriously, forlexample oil mist detection, and investigatethoroughly. A fully functional alarm system isessential for the safe operation of the mainengine.

    Implement robust on board fuel andllubrication oil management systems.

    At regular intervals, carry out system checkslof purifiers and filters for both fuel andlubrication oil systems.

    The company states that: The follow up of all engine logs has nowlbeen improved, especially the understandingof the exhaust gas temperatures and their alarm levels.

    The scope of performance reportinglbetween vessel and office will also beintensified in the future.

    The trend logging of reported performancelparameters in shore manager’s engineperformance monitoring system has beenimplemented.

    Engineers will be sent on four stroke engineltraining courses.

    Fuel oil samples before and after purifiers wereltaken and analysed. The result indicated that thepurifiers were working satisfactorily. All fuel oilanalyses from bunkering were withinspecification.

    Several samples of the damaged piston ringslwere sent to a laboratory. The conclusion wasthat the excessive wear of liners and pistons wasnot caused by catalytic fines.

    The cylinder liner lubrication system was testedland was found to work properly.

    At the time of the casualty the main engine,lincluding turbo charger, had been running 7,300hours since its previous major overhaul. Thisoverhaul had been carried out 18 monthspreviously.

    Investigation of the maintenance records showedlthat maintenance had been carried out inaccordance with manufacturer’s instructions.

    When reviewing the monthly main engine reportslit became obvious that the main engine exhausttemperatures of all cylinder units had increased30°C – 40°C for the previous six months.

    The turbo charger revolutions had dropped fromlabout 14,500 rpm to 12,000 rpm at 85% load ashad the charge air pressure from 1.7 bar to 1.2bar. These changes also began to appear in thepast six months.

    Due to high exhaust gas temperatures, the enginelwas under a high thermal load, which finallycaused it to break down.

    10.1

    Machinery fa

    ilure caused by con

    tamination

  • THE SWEDISH CLUB CASEBOOK

    10

    The engineers on a bulk carrier were carrying outscheduled maintenance on one of the ballast pumps.They had closed all the isolating valves to the ballastpump and put up notices about the job in the engineroom and engine control room, but not on the bridge.They didn’t finish the job on the first day, so continued thenext day.

    Preparing for port state inspection

    The following day the Master asked an officer to print outthe alarm list for the ballast water management systembefore arriving at the next port, as a port state inspectionwas expected. To get the list the officer had to start theballast water management system, which he did.

    The bilge high level alarm was suddenly activated in theengine room. An oiler checked the bilges and could seewater pouring in, covering the tank top. An engineerturned off the power to the ballast water managementsystem. He also found out that two ballast system valveswere open from the main seawater crossover suctionline. He closed these valves immediately to stop theingress of the water. These valves had been openedautomatically when the ballast water managementsystem was started. The engineers pumped the waterfrom the tank top into the bilge holding tank.

    Water in the lubrication oil

    One hour later the main engine bearing wear alarm –‘water level 50%’, went off. The main engine systemlubrication oil was found to have 0.09% water content. Thesecond lubricating oil purifier was started. A couple ofhours later the main engine bearing wear alarm went offonce again. A second sample of the lubrication oil wastaken, and it was found that the oil had 0.08% water in it.

    The Chief Engineer decided to partially change 3,000litres of lubrication oil in the system.

    Afterwards a third sample was taken and the watercontent was 0.019%. The engine was stopped, and a fullchange of the lubrication oil was completed. A crossheadbearing was opened for inspection. No damage wasfound. However, one of the rubber diaphragm seals fordraining the crankcase to the system lubricating oil tankwas found to be defective. This had caused the waterflooding into the engine room to contaminate the lube oil.

    Severe engine problems through voyage

    The main engine was restarted, and the voyage resumed.The main engine was an electronic controlled model i.e.the exhaust valves and fuel injection system werepowered by hydraulics. The system lubrication oil wasused as a hydraulic medium. The following day therewere problems with some hydraulic components and themain engine had to be stopped. A couple of cylinderunits and pumps had to be dismantled, cleaned andreassembled. The main engine could not be restartedbecause of low hydraulic pressure. It was decided thatone of the cylinders had to be blanked off. The mainengine was started and stopped several times over anumber of days as the hydraulic system was leaking.Because the engine was running on low rpms, thescavenge trunking became fouled with oil deposits, sothe engine had to be stopped several times and thetrunking had to be cleaned.

    Because water contaminated the lubrication oil therewas serious damage to several crosshead bearings,crosshead pins, main engine cylinders, hydraulic pumpsand main engine turbo charger bearings.

    10.2 Maintenance job lead to flooding of engine room

  • THE SWEDISH CLUB CASEBOOK

    What can we learn?A proper risk analysis should always belcarried out before any repairs/maintenance,especially if the affected system iscomplicated and can be controlled fromdifferent locations.

    It is also worth considering physicallyldisconnecting power to components sothey cannot be activated accidently duringthe repair/maintenance.

    It is essential that the bridge and enginelcrew discuss all jobs that can affect eachother’s department. If a job on the ballastsystem is planned, the bridge need to beinformed and if the job is extended to thefollowing day the OOW needs to beinformed. The OOW has to ensure that thisinformation is written clearly and discussedduring the watch handover.

    If there are excessive quantities of water onlthe tank top there is a risk that this will enterthe main engine sump tank via a defectivediaphragm and subsequently contaminatethe main engine lubricating oil system,resulting in severe damage to the mainengine components.

    If heavy contamination of water is found inlthe system:

    (i) the lube oil in the sump tank must be transferred to a settling tank.

    (ii) the sump tank and crank case should be cleaned.

    (iii) a complete fresh oil change filled to the level recommended by the engine manufacturer.

    The design of both Wärtsilä and MAN Dieselllubricating oil outlet diaphragms are quitesimilar.

    (i) Wärtsilä recommends: Inspection/replace at 40,000 running hours or at dry dock.

    (ii) MAN Diesel recommends: Inspect the diaphragm sealing in the crankcase oil outlet every 32,000 hours of operation, and replace the diaphragm if indicated by the inspection.

    It is recommended that all diaphragms arelreplaced every five years in connection withthe vessel’s special survey.

    The exchange of rubber diaphragms shouldlbe included in the vessels PMS system.

    It is recommended to owners that spareldiaphragms are kept on board at all times, inaddition to enough system lubrication oil tocompletely replenish the system.

    10.2

    Maintenance job lead to

    floo

    ding

    of e

    ngine room

  • THE SWEDISH CLUB CASEBOOK

    10

    A vessel was berthed alongside the quay, waitingto proceed through a lock to another berth. Thepilot called on the radio and asked the Master if itwould be possible to depart in half an hour. Pre-departure checks were completed by the OOW, theradar was tuned and the ECDIS set up fordeparture. The OOW did not check the controllablepitch propeller (CPP) as the vessel had only beenalongside for twelve hours and the OOW assumedeverything should be OK. He also felt stressedabout preparing everything for departure in such ashort time. According to the company’s SMS, theCPP should always be tested before departure.

    Rapid handover

    The Master came on the bridge accompanied bythe pilot. The OOW carried out a quick handoverand then proceeded to the forward mooringstation. The Master and pilot had a short pilotbriefing and afterwards the Master gave the orderto let go all lines.

    CPP not responding

    The vessel proceeded towards the lock and was inthe final approach when the Master realised thatthe CPP was not responding correctly and thevessel was rapidly approaching the lock. TheMaster attempted to recover control of the CPPsystem, but the pitch was stuck at approximately40% ahead, causing the vessel to accelerate. TheMaster panicked and was unsure what to do, sohe shouted on the radio to the mooring parties toget the lines ashore and stop the vessel. Theforward mooring party managed to get the

    forward spring secured to a bollard but no otherlines were attached. The pilot ordered the tug thatwas standing by beside the vessel, to push thevessel towards the quay. This caused the vessel tomake heavy contact with the quay, butunfortunately did not slow it down enough. Thevessel continued towards the lock at a speed ofabout three knots, the forward spring broke with aloud bang, and finally the vessel made heavycontact with the outer lock gate.

    Forty seconds after the impact the Master pushedthe emergency stop button for propulsion, afterwhich the engine control room took control ofpropulsion.

    Important evidence destroyed

    Shortly after the incident the Chief Engineer andFirst Engineer inspected the CPP system todetermine if something was wrong. Before anythird party was able to investigate the CPP, theChief Engineer cleared the system. This destroyedany evidence of what might have caused thefailure. The vessel was boarded by port state andclass inspectors. The vessel sustained damage toits bulbous bow, the tug sustained minor damageand the lock gates sank. Fortunately there were noinjuries or pollution - however there were costlyrepairs to both the lock and vessel.

    It was also discovered that the company had hadfour similar CPP near misses reported on sistervessels. The company had not made any changesto the PMS or sent any special instructions to thevessels in the fleet.

    10.3 Machinery failure of the CPP caused heavy contact with lock gate

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    What can we learn?Ensure that the OOW understands why it islimportant to test all equipment as per thechecklist, both for departure and arrival. Thishighlights the importance of carrying out thechecks required by the SMS.

    The Master did not save the vessel’s VDR –lthis was done by a port state inspector twohours after the incident. Always save theVDR, as soon as possible after an accident.It is important to have procedures thatensure that any evidence of what may havecaused an accident is not removed orcleared in order to understand and learnwhy the accident happened.

    Always try to establish why an accidentlhappened so it can be shared with the fleet.The near misses that had been reported tothe company were never acted upon – thereis no point in having a near miss reportingsystem if nothing is then done about thereports. Near misses and best practicesshould be shared within the fleet.

    10.3

    Machinery fa

    ilure of the CPP

    caused heavy contact w

    ith lock gate

  • THE SWEDISH CLUB CASEBOOK

    10

    A vessel was in ballast and sailing about sevenmiles from land on its way to the loading port in theNW Atlantic. It was early spring with heavy windsblowing and large waves. There was also some icein the water, so the crew had to clear the lowerstarboard sea-chest which was blocked with ice.The crew changed to the upper intake and thenremoved the large cover from the lower sea suctionfilter, finding it choked with ice slush. Whileremoving the ice the main sea water valve, locatedon the side shell plate, began to leak.

    Excessive force applied

    Whilst the crew were replacing the filter cover, oneof the engineers applied a large valve wheel key tothe actuator valve, in an attempt to stop the leakage.Too much force was applied damaging the gearmechanism that operates the valve spindle andwater began leaking into the engine room at highpressure.

    The crew made attempts to stop the leakage, butthe pressure and volume of water were too great.Attempts to pump out the water entering the engineroom were also unsuccessful as electric motorsand control gear were splashed with sea watercausing short circuits which disabled the bilgepumps.

    Vessel began drifiting

    The vessel blacked out and began drifting in thesevere weather conditions approximately 6-7 NM offthe coast. The coast guard arrived at the scene andtried to attach a tow line, however the attemptsfailed. The vessel then dropped both anchors, butthis did not stop the vessel from drifting. The vesseleventually grounded, and the crew was evacuated.

    The following day a salvage team boarded thevessel by helicopter. They were assisted by twotugs. Wires were connected from the groundedvessel to the tugs. Fortunately the weatherimproved and the vessel was refloated and towed tothe nearest port.

    Cleaning operations

    An underwater inspection revealed extensivedamage to the vessel shell plating. Operationscontinued over the following days, cleaning theengine room spaces with high pressure hoses andremoving the pollutant from the vessel.

    10.4 Routine job in the engine room caused grounding

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    What can we learn?When carrying out a critical job like cleaninglthe sea suction, it is important that there areclear procedures on how the job should bedone and, as in any critical operation, it isbest to have two people check to ensurethat mistakes are detected.

    A job like this should require a work permitland risk assessment to be completed.

    It is also important to run drills on how toldeal with a salvage operation, so the crew isprepared.

    10.4

    Routine job in th

    e engine ro

    om caused grou

    nding